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Difference between revisions of "34-167-28011"

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| State: Ohio
 
| State: Ohio
 
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| County: [[Washington_County,_Ohio|Washington]]
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| County: <County>
 
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| Municipality: [[Newport Township,_Washington_County,_Ohio|Newport Township]]
 
| Municipality: [[Newport Township,_Washington_County,_Ohio|Newport Township]]

Revision as of 14:26, 13 August 2019

Well Details

Well ID: 34-167-28011
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Country: United States
State: Ohio
County: <County>
Municipality: Newport Township
Operator Name: HUNTERS RUN CORP
Well Pad ID:
Farm/Lease Name: GREENWOOD ROCKOIL
License Status: Producing
License Date: 1985-01-28
Spud Date: 1985-02-11
Spud Drilling Contractor: CT DRILLING
Final Drill Date: 1985-02-18
Well Total Depth: 3302 ft
Configuration: Vertical
Latitude: 39.391826626
Longitude: -81.24625257

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1985-01-28 2178 HUNTERS RUN CORP GeoDate 1/28/85
Oil and Gas 1985-01-28 Issued Date 1/28/85 Expired Date 7/27/85 Acres 0020000 Tool Type RTA Proposed Formation OHIO SHALE Proposed Depth 03302 Proposed Drill Depth 03302
Original Spud 1985-02-13
Completed 1985-02-18
Reached Total Depth 1985-02-18
Construction Permit Expires 1985-07-27
Completion Report Received 1985-10-11
Record Last Modified 2019-04-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 1448 0
2006-09-11 2501 3215 79

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 2000 Mscf 0 FRAC;N2

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 HUNTERS RUN CORP 110 161 307

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 HUNTERS RUN CORP Brine 0 307

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000PL1599 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0150057246 2013-01-10 Orphan No Violations My inspection this day was to begin the process for entering the well into the Orphan Well Program. Columbus had instructed me to put all Hunters Run Corp wells into orphan program (There were Chiefs Orders issued in 2005 for a Bond Forfeiture.). The well is equipped with rods, tubing, a small separator and 100 bbl tank. There is a fair dike around the tank with no identification. There is low-hanging electric lines that will be crossed under to get to the well with a service rig. This well was drilled in 1985 into the Ohio Shale. According to our database, it was perforated in the Berea Ss and the Ohio Shale and possibly fracted - there is no indication that the well ever produced. ODNR has no completion report or well records. This well should not be difficult to plug and all the equipment will need to be removed. Pictures taken, SEM is 101, ROE has been signed by Frank Greenwood.
0189660582 2005-04-11 Production Wells No Violations Inspection found well still not in production. Consists of rods and tubing, 1 100 bbl tank and meter run with no meter. Will send on for chiefs orders
0569173706 2005-01-04 Production Wells Violations Noted Inspection this day found well not in production - hasnt produced in years. Tank has no IDs or does well, separator and lines present. Well has rods and tubing - jack has been removed, no meter found. Not capable of producing. Pictures 3/14/2005 - No response - will send for C.O.s. 1/16/2007 Chris Greenwood has legal arrangement with landowner -- has deal with his uncle, if we are willing to let him have well. I said YES! Plug or produce. Post IDs. Turn in annual production 12/7/2010 - Will resolve NOV - this well is idle/orphan well now.
1045060080 2009-03-30 Production Wells No Violations Inspection this day found well still has rods, tubing, not producing, idle for some time now. Chris Greenwood has said he will probably take it as his uncle owns land but he has not adopted yet. Tank is still on location, separator has been removed, well hooked into tank but not producing, no IDs. No change from last time inspected.
1064517599 2003-09-25 Orphan No Violations Inspection this day found well not producing, 4 1/2 casing with tubing? And polish rod, tank area has dike, no IDs, no meter in meter run - well has not produced in very long time. I believe this be orphan well - Hunters Run no more!
1109175198 2013-01-10 Orphan No Violations My inspection this day was to begin process for entering well into Orphan well program. Columbus had instructed me to put all Hunters Run Corp wells into orphan program. The well is equipped with rods, tubing, a small separator and 100 bbl tank. There is a fair dike around tank with no identification. There is low-hanging electric lines that will be crossed under to get to well. This well was drilled in 1985 into the Ohio Shale. It was perforated in the Berea Ss and the Shale and probably fracted - no indication that the well ever produced. The well should not be difficult to plug and all equipment will need to be removed. Pictures taken, ROE signed by Frank Greenwood.
1211995867 2008-05-23 Production Wells No Violations Talked to Chris Greenwood - he says if we will give him the well, he will get it going - can work a lease from his uncle, Sam Greenwood. Told him I felt he could have well.
1319267901 2010-12-28 Orphan No Violations Inspection found this well still idle - hoping that someone will adopt but no interest in it. Well is shut-iu with valve, 100 bbl tank and small little joe - all other equipment has been removed. Joe Flarety still around, cant be tied to well legally. Needs to go in orphan well program, Triad has rest of adjoining acerage.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0569173706 US-OH-126396 2005-01-04 Failure to legibly identify well
0569173706 US-OH-126397 2005-01-04 Well shall be plugged

For data sources see[9]

References