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| State: Ohio | | State: Ohio | ||
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− | | County: | + | | County: <County> |
|- | |- | ||
| Municipality: [[Independence Township,_Washington_County,_Ohio|Independence Township]] | | Municipality: [[Independence Township,_Washington_County,_Ohio|Independence Township]] |
Well ID: 34-167-62520 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: Independence Township | |
Operator Name: VALTECH SALES LLC | |
Well Pad ID: | |
Farm/Lease Name: USA/CARROTHERS | |
License Status: Producing | |
License Date: 1997-11-13 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 39.483169661 | |
Longitude: -81.17427120 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Change of Owner | 2005-02-11 | Operator changed from 5767, CREIGHTON MACHINE COMPANY to 2460, DOUBLE D WELL SERVICE INC |
Change of Owner | 2014-11-28 | Operator changed from 4784, YODER DARRELL dba DOUBLE "D" to 9392, DOUBLE D OIL AND GAS LLC |
Change of Owner | 2016-06-22 | Operator changed from 9392, DOUBLE D OIL AND GAS LLC to 8548, VALTECH SALES LLC |
Record Last Modified | 2016-06-22 | INSPECTED BY CINDY VAN DYKE ON APRIL 20, 2004. |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | DOUBLE D OIL AND GAS LLC | 30 | 56 | 365 |
2016 | VALTECH SALES LLC | 111 | 23 | 365 |
2017 | VALTECH SALES LLC | 499 | 34 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2009 | YODER DARRELL dba DOUBLE "D" | Brine | 0 | 365 |
2010 | YODER DARRELL dba DOUBLE "D" | Brine | 0 | 365 |
2011 | YODER DARRELL dba DOUBLE "D" | Brine | 0 | 365 |
2012 | YODER DARRELL dba DOUBLE "D" | Brine | 0 | 366 |
2013 | YODER DARRELL dba DOUBLE "D" | Brine | 0 | 365 |
2014 | DOUBLE D OIL AND GAS LLC | Brine | 0 | 365 |
2016 | VALTECH SALES LLC | Brine | 0 | 365 |
2017 | VALTECH SALES LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0051895316 | 2014-10-07 | Administrative Inspection | No Violations | Mr. John Thompson of Double D Gas & Oil returned my call at 4:01 pm and stated that he will have the tank battery and well head area seeded and mulched by the beginning of next week. |
0114954461 | 2014-09-03 | Production Wells | No Violations | Upon inspection, it was observed that this well is capable of production and is producing. A new tank battery location has been established and new flow lines have been run from the well to the tank, and from the well to the production meter. Legible and correct ID information has been posted at the tank and at the well. The previously contaminated area has been cleaned up, but the area has yet to be seeded/mulched. Mr. John Thompson of Double D Gas and Oil stated that the area around the well head as well as the new tank battery will be seeded/mulched next week. |
0307204611 | 2014-12-29 | Production Wells | No Violations | Upon inspection, it was observed that the location is still void of vegetation, but it appears that dirt work is being performed in preparation for a house to be built near CR-9, which is near the lease road for the well. I will contact Mr. John Thompson of Double D Gas and Oil and inquire about the status of this location. |
0592099791 | 2014-08-14 | Production Wells | No Violations | Met with Double D Gas and Oil Well Tender Mr. John Thompson to inspect cleanup efforts at this location. Upon inspection, it was observed that the contamanated soil has been removed and the well location has been entirely re-graded. In addition, the leaking stuffing box and leaking tubing joint have been replaced. The well is shut in, but will be back in production next week after the new tank is installed at the new tank battery location by County Road 9. The entire location will be seeded and mulched next week. I will continue to monitor the progress of this location until it is fully compliant. |
0604891393 | 2014-08-12 | Administrative Inspection | No Violations | Spoke with Mr. John Thompson of Double D Oil and Gas at 10:09 am and he stated that corrective action has been taken to put this well back into compliance. Mr. Thompson stated that the kill area has been cleaned up and seeded/mulched, a new tank has been brought in and will be hooked up/diked this week, and the leaking tubing, stuffing box, and lines have all been repaired/replaced. I will be meeting with Mr. Thompson at this location this week to verify his claims and recommend any further action that may need to be taken. |
0960112265 | 2014-10-07 | Production Wells | No Violations | Upon inspection, it was observed that this location is still not seeded/mulched around the well head area or the tank battery. I called Mr. John Thompson of Double D at 3:27 pm and left a message for him to call me about this location. |
1406902152 | 2014-07-31 | Production Wells | Violations Noted | Performed an inspection on this well in response to a landowner complaint. Upon inspection, it was observed that this well is equipped for production, but is currently shut-in. The well consists of a pumping unit with an electric motor standing over 7 surface casing with a gas escape packer and 2 production tubing with rods. The production tank for this well was not located. There is a leak in the 2 tubing that has allowed oil to contaminate the well head area as well as the area downhill from the well leading to a drainage in the ravine below. An unsuccessful attempt has been made to fix the leak with a clamp. There is a prominent vegetation kill area approximately 3 wide by 50 long leading into the drainage. An oily sheen was observed in the drainage water where the contamination enters. Photos were taken of the location to verify these issues. The contaminated area needs to be remediated immediately to prevent further ecological damage. The operator will have 14 days upon receipt of this notice to reach compliance. |
1414481659 | 2012-08-23 | Production Wells | Violations Noted | I received complaint from OEPA that landowner, Mr. Ross, had reported deep erosion on the lease road and oil running downhill below the pumping unit. I found the well located on the edge of a sharp, steep hollow with oil saturated ground 6 square around the well and oily path downhill below the well, at least 50 and possibly 100 downhill. I discussed the problem with Jason, the pumper, and he said he would get it cleaned up - said the tubing was leaking but also looked like sales/flow line was leaking. This will be difficult to clean up but oil satured dirt should be removed, hillside seeded with grass and mulched and the leak at the well corrected. Well also needs identification. Erosion on the lease road also must be fixed and deep ruts removed. Tank is a good distance north along road and have asked them to move it as it was only 10 from road. Tank is being moved back and diked, as it also had oily, barren brine kill patch going downhill from the tank. Several serious problems with contamination and brine dumping that must be taken care of soon. |
1415540560 | 2004-04-20 | Production Wells | Violations Noted | Inspection this day found well capable of producing with jack, have not turned in production for years and operator does not know if this well producing or not . JOE - update lat/long - not on map. 12/8/2004 - well now producing. |
1656504974 | 2012-08-23 | Production Wells | No Violations | FOLLOW UP TO NOV # -1414481659 I received complaint from OEPA that landowner, Mr. Ross, had reported deep erosion on the lease road and oil running downhill below the pumping unit. I found the well located on the edge of a sharp, steep hollow with oil saturated ground 6 square around the well and oily path downhill below the well, at least 50 and possibly 100 downhill. I discussed the problem with Jason, the pumper, and he said he would get it cleaned up - said the tubing was leaking but also looked like sales/flow line was leaking. This will be difficult to clean up but oil satured dirt should be removed, hillside seeded with grass and mulched and the leak at the well corrected. Well also needs identification. Erosion on the lease road also must be fixed and deep ruts removed. Tank is a good distance north along road and have asked them to move it as it was only 10 from road. Tank is being moved back and diked, as it also had oily, barren brine kill patch going downhill from the tank. Several serious problems with contamination and brine dumping that must be taken care of soon. |
2102917842 | 2015-01-15 | Production Wells | No Violations | Upon inspection, it was observed that the location has been graded, seeded, and mulched. The well is in production and all contamination has been removed from the location. The compliance notice dated 8/1/2014 can be closed. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1406902152 | US-OH-111972 | 2014-08-11 | Well operation causing pollution and contamination | |
1414481659 | US-OH-112178 | 2012-08-23 | Well operation causing pollution and contamination | |
1414481659 | US-OH-112179 | 2012-08-23 | Failure to legibly identify well | |
1415540560 | US-OH-112204 | 2004-04-21 | Well shall be plugged |
For data sources see[7]