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Difference between revisions of "34-053-20997"

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| County: [[Gallia_County,_Ohio|Gallia]]
 
| County: [[Gallia_County,_Ohio|Gallia]]
 
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| Municipality: [[Harrison_Township,_Gallia_County,_Ohio|Harrison Township]]
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| Municipality: [[Harrison Township,_Gallia_County,_Ohio|Harrison Township]]
 
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| Operator Name: [[CONTINENTAL RESOURCES INC]]
 
| Operator Name: [[CONTINENTAL RESOURCES INC]]
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| Configuration: Horizontal
 
| Configuration: Horizontal
 
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| Latitude: 38.755215652
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| Latitude: <Latitude>
 
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| Longitude: -82.30583422
 
| Longitude: -82.30583422

Revision as of 22:07, 14 August 2019

Well Details

Well ID: 34-053-20997
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Country: United States
State: Ohio
County: Gallia
Municipality: Harrison Township
Operator Name: CONTINENTAL RESOURCES INC
Well Pad ID:
Farm/Lease Name: MASSIE KATHRYN N & NOEL F
License Status: Final Restoration
License Date: 2008-07-28
Spud Date: 2008-06-22
Spud Drilling Contractor: S W JACK DRLG
Final Drill Date: 2008-08-01
Well Total Depth: 2915 ft
Configuration: Horizontal
Latitude: <Latitude>
Longitude: -82.30583422

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2008-01-02 Proposed Formations:LOWER HURON SHALE AND/OR OHIO SHALE, Issued Date:1/2/2008, Expired Date:1/1/2009 6:00:00 AM, Drilling unit acres:38.17, Proposed Well Type:OG, Proposed Well Class:EW
Change of Owner 2008-05-29 Operator changed from 7910, EPSILON ENERGY USA INC to 8380, CONTINENTAL RESOURCES INC
APP 2008-05-30 Proposed Formations:LOWER HURON/OHIO SHALE, Issued Date:5/30/2008, Expired Date:5/30/2009 6:00:00 AM, Drilling unit acres:38.17, Proposed Well Type:OG, Proposed Well Class:EW
Plugged/Abandoned 2008-07-15

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APP 2008-07-28 Proposed Formations:LOWER HURON/OHIO SHALE, Issued Date:7/28/2008, Expired Date:7/28/2009 6:00:00 AM, Drilling unit acres:51.95, Proposed Well Type:OG, Proposed Well Class:EW
Reached Total Depth 2008-08-01

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Correction to Well 2008-09-19 ADJUSTMENT TO TARGET INFORMATION (AS A RESULT OF COMPLETION OF HORIZONTAL DRILL): NEW FOOTAGE= 3019'2L & 1159'EL OF SEC. 30; NEW X= 2,053,110. NEW SURFACE Y= 275, 118.
Completion Report Received 2009-01-12

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Construction Permit Expires 2009-07-28

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Record Last Modified 2015-09-24

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For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 0 0 DUE TO INADEQUATE NATURAL SHOWS, THE WELL WAS NOT TREATED, PER PHONE CONVERSATION ON 4/23/09 W/ OPERATOR'S ENGINEER … GM

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2008 CONTINENTAL RESOURCES INC 0 0 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2008 CONTINENTAL RESOURCES INC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0203935771 2009-07-15 Preliminary Restoration No Violations Solidify pit with 140 sks cement. Mix with track hoe.
0225610146 2008-07-15 Drill / Deepen / Reopen No Violations Straight hole TD is 2915. Core samples have been taken and the hole has been logged. Plug back from 2915 to 2050. This is to be used for a kick plug during the horizontal portion of the well. The pit liner had to be replaced again due to a tear. I witnessed the liner being installed. And was able to witness the plug back at the same time.
0389346228 2008-12-19 Completion Testing No Violations A slight bubbling was noticed at the wellhead. Bubbles 1/4 inch in diameter. I took a video. All valves on the wellhead are shut off. My gas detector did not show any explosive levels of gas at the wellhead. There was a good breeze at the time of inspection.
0586192040 2008-06-19 Drill / Deepen / Reopen No Violations GPS on the well stake. Site is being built now. They are building a gravel entrance and will stone most of the location. This is an horizontal well. The same crew that did the Richfield wells is doing this well. Merl Richards, Jimmy Ray and the SW Jack rig # 8.
0881545284 2008-08-03 Drill / Deepen / Reopen No Violations Well has been drilled and is making 500psi naturally. Horizontal portion of the well is in the Rhine Street 2722 to 2793. Updated well GPS location. Drill pit is in good shape and is being currently used for drilling the 996. No violations observed during inspection.
1009898814 2009-07-10 Plug / Plug Back No Violations Pumped 1st plug on 7-9-09 from 2885 to 2485. On 7-10-09 ran back to 2885 and did not tag plug. Pump LCM and fresh water and try to achieve circulation. Took 80 bbls to circulate to surface. Pump 20 bbls. Stop circulation then re start took 120 bbls total. Pumped plug from 2885 to 2485. Ran tubing back to try and tag TOC was unable ran tubing back to 2885 and pumped another plug from 2885 to 2485. WOC.
1016848316 2014-12-04 Preliminary Restoration No Violations Preliminary Restoration requirements met.
1197458774 2008-10-30 Completion Testing No Violations Carper Well Service Rig is swabbing on the well. Talked to Shannon Stevens on location about the pit and timelines for restoration. Pit is open. Pit liner is in good shape, no tears in lining.
1214311722 2008-06-23 Drill / Deepen / Reopen No Violations Surface cement job. I arrived on location and the rig crew was still trying to get the 9 5/8 in the hole. They were having trouble with the threads and there was a slight bend in the casing which was causing it to cross thread. They hit mud and decided to drive 20 to 41 then drill 17 1/2 hole 63 for the 13 3/8 conductor. Then a 12 1/4 hole was drilled to 645. They were going to set 617 of 9 5/8 but due to the cross threading problem they set 573 of 9 5/8. I approved the change to the casing program in the field. A 1/4 stream of water was hit at 350. A basket was set at 256. The well had good circulation and good cement returns to the surface.
1241793261 2009-05-07 Preliminary Restoration Violations Noted Spud date 6-22-08, Restoration due 3-22-09. Site is rutted with standing water. No attempt to vegetate site. Site is bare ground. No identification on well. Well is equipped with a pump jack, tubing, rods, and a flare. Flare is not connected at this time. Robert Stonerock (South Region Supervisor) accompanied me on the inspection. A pool of oil around the wellhead 3 feet in diameter. I called Merl Richards (company representative) at 6:18 pm on 5-7-09 and informed him of the violations.
1262110754 2009-05-13 Preliminary Restoration No Violations No identification. Well is equipped with a flare set 95 from the well. Site is rutted and the soil is bare. No effort has been made to restore the site. Wellhead has a 3 pool of oil around it. Well is equipped with tubing, rods, pump jack, and gas motor.
1502129735 2008-11-12 Drill / Deepen / Reopen No Violations Leaking gas around the back side of the 7. Gas is bubbling up through a puddle at the surface. Can hear gas leak but it doesnt show up on the gas detector. I? Have talked to Jimmy Ray about this well.
1526835060 2009-07-07 Plug / Plug Back No Violations Cut the 4.5 casing at 2743 MD. Pulled to 2690 and swabbed the well. Fluid level at 1000. Swabbed again and it kicked off.
1673355379 2010-02-03 Final Restoration No Violations Site is graded. Have established good vegetative cover on location. Landowner will use site for hay field. Gravel pile has been left at request of landowner.
1717658445 2008-07-14 Drill / Deepen / Reopen No Violations Pit had to be relined due to a tear. An un determined amount of fluid was lost from the pit. They are preparing to log the hole. Then plug it back to drill horizontally.
1731249331 2008-06-27 Drill / Deepen / Reopen No Violations I received a call from Merl Richards and he informed me that the rig had a brine leak at their mud pump. I met Merl on location and we discussed the clean up procedures. The brine is contained in the clay soil and is pooled up in 3 areas 1.5 by 6, 3 by 2 and 2 by 5 all pools were less than 2 deep. The leak was caused by a leaking union on the mud pump. I told Merl to contain the soil and to dispose of it in the pit during restoration.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1241793261 US-OH-106455 2009-05-08 Failure to restore land surface within 9 mos. (CHANGE) (REPLACE)
1241793261 US-OH-106456 2009-05-08 Well operation causing pollution and contamination
1241793261 US-OH-106457 2009-05-08 Failure to legibly identify well

For data sources see[8]

References