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| County: [[Portage_County,_Ohio|Portage]] | | County: [[Portage_County,_Ohio|Portage]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Hiram Village,_Portage_County,_Ohio|Hiram Village]] |
|- | |- | ||
| Operator Name: [[EQUITY OIL & GAS FUNDS INC]] | | Operator Name: [[EQUITY OIL & GAS FUNDS INC]] |
Well ID: 34-133-23290 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Hiram Village | |
Operator Name: EQUITY OIL & GAS FUNDS INC | |
Well Pad ID: | |
Farm/Lease Name: COUCH | |
License Status: Producing | |
License Date: 1984-09-24 | |
Spud Date: 1984-10-16 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1984-10-22 | |
Well Total Depth: 4447 ft | |
Configuration: Vertical | |
Latitude: 41.304409392 | |
Longitude: -81.14581875 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1984-09-24 | 1511 NORTH COAST PETROLEUM INC GeoDate 9/24/84 |
Oil and Gas | 1984-09-24 | Issued Date 9/24/84 Expired Date 3/23/85 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04447 Proposed Drill Depth 04447 |
Original Spud | 1984-10-16 | |
Completed | 1984-10-22 | |
Reached Total Depth | 1984-10-22 | |
Completion Report Received | 1984-11-30 | |
Construction Permit Expires | 1985-03-23 | |
CO | 1994-01-26 | 3367 CRISSINGER ROBERT A INC GeoDate 9/24/84 |
CO | 1996-03-01 | 1171 EQUITY OIL & GAS FUNDS IN GeoDate 9/24/84 |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4227 | 4300 | 0 |
2006-09-11 | 4231 | 4298 | 18 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
FOAM | 0 | 41000 Gal | 10000 | FRAC: H2O,SAND |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000PL6057 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0582002429 | 2011-07-20 | Production Wells | No Violations | Pol Excavating has cleaned up the contaminated area around the tank battery. The dirt has been hauled off. The clean up is 98% complete. |
1311097740 | 2011-07-19 | Production Wells | No Violations | I received a call from the Uniontown office, Marlene Hall about a lightening strike early this morning in Hiram. The well tender Don Toth(440-478-2156) reported it to the Uniontown office. I called Don about the strike. He has Wade Pol Excavating on the way up to start the clean up. I arrived one hour later with inspectors Chris Grimm and John Brauer. The fire had burned up the oil inside the 210 barrel stock tank. There was 70 barrels of oil inside the tank. The stock tank was blown 300 feet to the northeast. The bottom of the tank was 100 feet from the dike area. The clean up had started. All the top soil 25 feet to the west was scraped off. The Complaint number is 3242. The clean up continues. |
1685961972 | 2011-07-21 | Production Wells | No Violations | The cleanup is 100% done. The new equipment will be installed next week. This complaint continues. |
1804253745 | 2011-08-04 | Production Wells | No Violations | The tank battery has been completed. The old stock tank has been cut up and hauled away. The dike area around the tank battery is complete. An ID sign is posted. This complaint is resolved. |
1898552758 | 2011-08-01 | Production Wells | No Violations | The old stock tank has been cut up but not hauled off yet. The tank battery facility is complete. This complaint continues. The Complaint number is 3242. |
2076031074 | 2011-07-25 | Production Wells | No Violations | The installing of the stock tank, separator has commenced. The clean up is complete. Lightening strike clean up. There were no violations at this time. |
For data sources see[9]