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Difference between revisions of "37-007-20377"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-007-20377
 
| Well ID: 37-007-20377
| style="height=100%; align=center" rowspan="14" | {{#display_map: 40.631583, -80.501556 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.631583, -80.501556 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
Line 13: Line 13:
 
| Municipality: [[Greene Township,_Beaver_County,_Pennsylvania|Greene Township]]
 
| Municipality: [[Greene Township,_Beaver_County,_Pennsylvania|Greene Township]]
 
|-
 
|-
| Operator Name:  
+
| Operator Name: [[FIRSTENERGY GENERATION LLC]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
Line 21: Line 21:
 
| License Status: Plugged OG Well
 
| License Status: Plugged OG Well
 
|-
 
|-
| Spud Date: 1/1/1800
+
| Spud Date: 1800-01-01
 
|-
 
|-
 
| Permit Date:  
 
| Permit Date:  
Line 49: Line 49:
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Job Start Date
 +
!scope="col" | Job End Date
 +
!scope="col" | True Vertical Depth (ft)
 +
!scope="col" | Total Water Volume (gal)
 +
!scope="col" | Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Job Number
 +
!scope="col" | Trade Name
 +
!scope="col" | Supplier
 +
!scope="col" | Purpose
 +
!scope="col" | Ingredient Name
 +
!scope="col" | CAS Number
 +
!scope="col" | Additive Percentage by Mass
 +
!scope="col" | Job Percentage by Mass
 +
!scope="col" | Mass Used (lb)
 +
|-
 +
|}-->
 +
 
<!--== Production Data ==
 
<!--== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
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{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Period
 
!scope="col" | Period
 +
!scope="col" | Operator
 
!scope="col" | Waste Type
 
!scope="col" | Waste Type
 
!scope="col" | Quantity
 
!scope="col" | Quantity
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| 2143026
 
| 2143026
 
| Primary Facility
 
| Primary Facility
| 02/01/2013
+
| 2013-02-01
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 91: Line 117:
 
| 2143031
 
| 2143031
 
| Primary Facility
 
| Primary Facility
| 01/29/2013
+
| 2013-01-29
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 98: Line 124:
 
| 2143035
 
| 2143035
 
| Primary Facility
 
| Primary Facility
| 01/24/2013
+
| 2013-01-24
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 105: Line 131:
 
| 2143038
 
| 2143038
 
| Primary Facility
 
| Primary Facility
| 02/05/2013
+
| 2013-02-05
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
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| 2143097
 
| 2143097
 
| Primary Facility
 
| Primary Facility
| 02/19/2013
+
| 2013-02-19
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
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| 2143102
 
| 2143102
 
| Primary Facility
 
| Primary Facility
| 02/12/2013
+
| 2013-02-12
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 126: Line 152:
 
| 2146586
 
| 2146586
 
| Primary Facility
 
| Primary Facility
| 03/04/2013
+
| 2013-03-04
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 133: Line 159:
 
| 2148317
 
| 2148317
 
| Primary Facility
 
| Primary Facility
| 03/13/2013
+
| 2013-03-13
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
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| 2148362
 
| 2148362
 
| Primary Facility
 
| Primary Facility
| 03/12/2013
+
| 2013-03-12
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 147: Line 173:
 
| 2148365
 
| 2148365
 
| Primary Facility
 
| Primary Facility
| 03/07/2013
+
| 2013-03-07
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
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| 2148367
 
| 2148367
 
| Primary Facility
 
| Primary Facility
| 03/07/2013
+
| 2013-03-07
 
| Drilling/Alteration
 
| Drilling/Alteration
 
| No Violations Noted
 
| No Violations Noted
Line 161: Line 187:
 
| 2149309
 
| 2149309
 
| Primary Facility
 
| Primary Facility
| 03/19/2013
+
| 2013-03-19
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
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| 2149320
 
| 2149320
 
| Primary Facility
 
| Primary Facility
| 03/13/2013
+
| 2013-03-13
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 175: Line 201:
 
| 2151185
 
| 2151185
 
| Primary Facility
 
| Primary Facility
| 03/25/2013
+
| 2013-03-25
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
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| 2156433
 
| 2156433
 
| Primary Facility
 
| Primary Facility
| 04/03/2013
+
| 2013-04-03
 
| Plugging(Includes Plugged/Mined Through)
 
| Plugging(Includes Plugged/Mined Through)
 
| No Violations Noted
 
| No Violations Noted
Line 217: Line 243:
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
<!--== Fracking Activities ==
 
==== Fracking Jobs ====
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Job Number
 
!scope="col" | Job Start Date
 
!scope="col" | Job End Date
 
!scope="col" | True Vertical Depth (ft)
 
!scope="col" | Total Water Volume (gal)
 
!scope="col" | Total Non-Water Volume (gal)
 
|-
 
|}-->
 
<!--==== Fluid Composition Data ====
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | Job Number
 
!scope="col" | Trade Name
 
!scope="col" | Supplier
 
!scope="col" | Purpose
 
!scope="col" | Ingredient Name
 
!scope="col" | CAS Number
 
!scope="col" | Additive Percentage by Mass
 
!scope="col" | Job Percentage by Mass
 
!scope="col" | Mass Used (lb)
 
|-
 
|}-->
 
 
 
==References==
 
==References==
 
<references/>
 
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Pennsylvania Wells]]
 
[[Category:Pennsylvania Wells]]

Revision as of 06:46, 20 August 2019

Well Details

Well ID: 37-007-20377
Loading map...
Country: United States
State: Pennsylvania
County: Beaver
Municipality: Greene Township
Operator Name: FIRSTENERGY GENERATION LLC
Well Pad ID:
Farm/Lease Name: KASTLER 1
License Status: Plugged OG Well
Spud Date: 1800-01-01
Permit Date:
Unconventional Well: N
Configuration: Vertical Well
Latitude: 40.631583
Longitude: -80.501556

For data sources see[1][2][3]


Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2143026 Primary Facility 2013-02-01 Plugging(Includes Plugged/Mined Through) No Violations Noted HYDROCARBON DUG UP WOODEN CONDUCTOR AND A POSSIBLE WATER WELL. BUBBLES FROM BOTH.
2143031 Primary Facility 2013-01-29 Plugging(Includes Plugged/Mined Through) No Violations Noted HYDROCARBON HAS EXCAVATED 5' DEEP TRENCH AND HAVE NOT FOUND CASING OR CONDUCTOR. THE TRENCH IS FULL OF WATER AND THERE ARE BUBBLES IN SEVERAL AREAS. NO PERSONEL ON THE SITE.
2143035 Primary Facility 2013-01-24 Plugging(Includes Plugged/Mined Through) No Violations Noted HYDROCARBON DIGGING TO FIND GAS WELL OR THE SOURCE OF BUBBLES IN THE SURFACE WATER.
2143038 Primary Facility 2013-02-05 Plugging(Includes Plugged/Mined Through) No Violations Noted 5" WATER WELL HAS BEEN RAISED TO SURFACE. WOODEN CONDUCTOR ALSO EXCAVATED. NEED TO DIG DEEPER.
2143097 Primary Facility 2013-02-19 Plugging(Includes Plugged/Mined Through) No Violations Noted HYDROCARBON SHUT DOWN TOCONTAIN FLOW OF SUBSTANCE COMING FROM THE WELL BORE. CONTRACTOR WILL GET EQUIPTMENT TO CEMENT OFF THE FLOW.
2143102 Primary Facility 2013-02-12 Plugging(Includes Plugged/Mined Through) No Violations Noted SERVICE RIG IS UP AND CLEANING THE WELL WITH A CHERRY PICKER. THEY ARE PICKING UP GRAVEL, WOOD, AND CLAY.
2146586 Primary Facility 2013-03-04 Plugging(Includes Plugged/Mined Through) No Violations Noted ALL CASINGS ARE CEMENTED. CONTRACTOR REBUILDING THE TOP OF 95/8" CASING FOR CONTROL.
2148317 Primary Facility 2013-03-13 Plugging(Includes Plugged/Mined Through) No Violations Noted SUPERIOR HAS CEMENTED 100' OF 7" CASING. HYDROCARBON IS DRILLING OUT CEMENT LEFT INSIDE OF THE CASING AT 65'.
2148362 Primary Facility 2013-03-12 Plugging(Includes Plugged/Mined Through) No Violations Noted WATER STILL FLOWING INTO THE WELL. SUPERIOR IS ON THE SITE TO CEMENT 100' OF 7" CASING.
2148365 Primary Facility 2013-03-07 Plugging(Includes Plugged/Mined Through) No Violations Noted DRILLING 85/8" HOLE AT 90'. A SMALL AMOUNT OF CRUDE OIL FLOWED INTO THE BORING AT 70'. CONTRACTOR PLANS TO CEMENT 7" CASING AROUND 100'.
2148367 Primary Facility 2013-03-07 Drilling/Alteration No Violations Noted NOMAC 245 IS BEING TRUCKED IN AND BUILT.
2149309 Primary Facility 2013-03-19 Plugging(Includes Plugged/Mined Through) No Violations Noted DRILLING AT 101'. THIS DEPTH IS JUST BELOW THE 7" CASING.
2149320 Primary Facility 2013-03-13 Plugging(Includes Plugged/Mined Through) No Violations Noted SUPERIOR HAS CEMENTED 7" CASING AT 100'. HYDROCARBON IS DRILLING OUT CEMENT LEFT INSIDE OF THE CASING @ 65'.
2151185 Primary Facility 2013-03-25 Plugging(Includes Plugged/Mined Through) No Violations Noted CONTRACTOR IS UNABLE TO ADVANCE THE BORING AND CUTTINGS ARE MIXED WITH METAL.HYDROCARBON HAS MADE SEVERAL ATTEMPTS, AND IS BURNING BITS AND HYDRALIC COMPONENTS ON THIER RIG. THE COAL SEAMS OUTCROP AT A HIGHER ELEVATION THAN THIS BORING, AND THERE HAS BEEN NO GAS BUBBLES SINCE THE WATER ZONES WERE CEMENTED. THE WELL WAS PROBABLY PLUGGED BEFORE AND SCRAP STEEL AND PIPE DUMPED DOWN THE HOLE. CONTRACTOR WILL GROUT THE WELL AND VENT A NEARBY WATER WELL.
2156433 Primary Facility 2013-04-03 Plugging(Includes Plugged/Mined Through) No Violations Noted THE WELL IS CEMENTED TO THE SURFACE.

For data sources see[4]

References