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Difference between revisions of "34-117-23833"

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| County: [[Morrow_County,_Ohio|Morrow]]
 
| County: [[Morrow_County,_Ohio|Morrow]]
 
|-
 
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| Municipality: [[Perry Township,_Morrow_County,_Ohio|Perry Township]]
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| Municipality: [[Perry_Township,_Morrow_County,_Ohio|Perry Township]]
 
|-
 
|-
 
| Operator Name: [[MARAM ENERGY INC]]
 
| Operator Name: [[MARAM ENERGY INC]]

Revision as of 16:38, 31 August 2019

Well Details

Well ID: 34-117-23833
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Country: United States
State: Ohio
County: Morrow
Municipality: Perry Township
Operator Name: MARAM ENERGY INC
Well Pad ID:
Farm/Lease Name: KRABILL J
License Status: Producing
License Date: 1995-02-23
Spud Date: 1988-04-06
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1988-04-08
Well Total Depth: 1562 ft
Configuration: Vertical
Latitude: 40.578494993
Longitude: -82.68467530

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1988-03-30 Issued Date 3/30/88 Expired Date 3/30/89 Acres 0010000 Tool Type RTAF Proposed Formation LOCKPORT Proposed Depth 01562 Proposed Drill Depth 01562
Original Spud 1988-04-06
Completed 1988-04-08
Reached Total Depth 1988-04-08
CO 1988-04-30 1283 COSHOCTON PIPE CO GeoDate 3/30/88
Completion Report Received 1988-05-02
CO 1992-12-09 3243 OHIO PRODUCTION CORP GeoDate 3/30/88
CO 1995-02-23 3243 OHIO PRODUCTION CORP GeoDate 2/23/95
Unknown 1995-02-23 Issued Date 2/23/95 Expired Date 2/23/96 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Construction Permit Expires 1996-02-23
Change of Owner 1998-03-10 Operator changed from 3243, OHIO PRODUCTION CORP to 6091, OHIO ENERGY ASSETS, INC.
Change of Owner 2010-01-11 Operator changed from 6091, OHIO ENERGY ASSETS, INC. to 476, MARAM ENERGY CO
Record Last Modified 2015-09-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 0 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NO TREATMENT

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1988 OHIO PRODUCTION CORP 35012 0 239
1989 OHIO PRODUCTION CORP 39399 0 0
1990 OHIO PRODUCTION CORP 64666 0 365
1991 REDMAN OIL CO INC 2875 0 102
1993 OHIO PRODUCTION CORP 0 0 0
1994 OHIO PRODUCTION CORP 0 0 0
1997 OHIO PRODUCTION CORP 276 0 216
1998 OHIO ENERGY ASSETS, INC. 0 0 0
1999 OHIO ENERGY ASSETS, INC. 0 0 0
2000 OHIO ENERGY ASSETS, INC. 0 0 0
2001 OHIO ENERGY ASSETS, INC. 4961 0 305
2002 OHIO ENERGY ASSETS, INC. 6024 0 226
2003 OHIO ENERGY ASSETS, INC. 1133 0 33
2004 OHIO ENERGY ASSETS, INC. 0 0 0
2005 OHIO ENERGY ASSETS, INC. 0 0 0
2006 OHIO ENERGY ASSETS, INC. 0 0 0
2007 OHIO ENERGY ASSETS, INC. 0 0 0
2008 OHIO ENERGY ASSETS, INC. 0 0 0
2009 OHIO ENERGY ASSETS, INC. 0 0 0
2010 MARAM ENERGY INC 0 0 365
2011 MARAM ENERGY INC 0 0 365
2012 MARAM ENERGY INC 0 0 0
2013 MARAM ENERGY INC 0 0 0
2014 MARAM ENERGY INC 0 0 0
2015 MARAM ENERGY INC 0 0 0
2016 MARAM ENERGY INC 0 0 0
2017 MARAM ENERGY INC 0 0 0
2018 MARAM ENERGY INC 0 0 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1988 OHIO PRODUCTION CORP Brine 200 239
1989 OHIO PRODUCTION CORP Brine 0 0
1990 OHIO PRODUCTION CORP Brine 0 365
1991 REDMAN OIL CO INC Brine 0 102
1993 OHIO PRODUCTION CORP Brine 0 0
1994 OHIO PRODUCTION CORP Brine 0 0
1997 OHIO PRODUCTION CORP Brine 0 216
1998 OHIO ENERGY ASSETS, INC. Brine 0 0
1999 OHIO ENERGY ASSETS, INC. Brine 0 0
2000 OHIO ENERGY ASSETS, INC. Brine 0 0
2001 OHIO ENERGY ASSETS, INC. Brine 0 305
2002 OHIO ENERGY ASSETS, INC. Brine 0 226
2003 OHIO ENERGY ASSETS, INC. Brine 0 33
2004 OHIO ENERGY ASSETS, INC. Brine 0 0
2005 OHIO ENERGY ASSETS, INC. Brine 0 0
2006 OHIO ENERGY ASSETS, INC. Brine 0 0
2007 OHIO ENERGY ASSETS, INC. Brine 0 0
2008 OHIO ENERGY ASSETS, INC. Brine 0 0
2009 OHIO ENERGY ASSETS, INC. Brine 0 0
2010 MARAM ENERGY INC Brine 0 365
2011 MARAM ENERGY INC Brine 0 365
2012 MARAM ENERGY INC Brine 0 0
2013 MARAM ENERGY INC Brine 0 0
2014 MARAM ENERGY INC Brine 0 0
2015 MARAM ENERGY INC Brine 0 0
2016 MARAM ENERGY INC Brine 0 0
2017 MARAM ENERGY INC Brine 0 0
2018 MARAM ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000PL9002 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0068248931 2018-05-09 Production Wells No Violations Inspected the Krabill #1 (#3833) as part of a standard production well status check. Inspect well, storage and identification. Status: ok, company evaluating future utility.
0311503339 2015-03-30 Production Wells No Violations Inspected the Krabill J #2 (#3833) as part of a standard compliance action follow up accompanied by Jeff Fry. Status: no change-in-status from previous follow up, non-compliant.
0582282980 2015-03-30 Production Wells No Violations Location Information for the Krabill #2 (#3833). WELL HEAD: Lat. 40.57865 Long. -82.58457 / CENTER-OF-STORAGE: none / ENTRANCE: Lat. 40.57955 Long. -82.68451.
0704959818 2012-01-05 Production Wells Violations Noted Inspect well. Well with 4.5 inch casing and 2 7/8 inch upset tubing, Identification is posted, meter is broken. Well shut in. Strong Hydrogen sulfide odor emanating from well head. Well is idle and incapable of production. Operator needs to plug well.
1422275383 2012-01-05 Production Wells No Violations FOLLOW UP TO NOV # 704959818 Inspect well. Well with 4.5 inch casing and 2 7/8 inch upset tubing, Identification is posted, meter is broken. Well shut in. Strong Hydrogen sulfide odor emanating from well head. Well is idle and incapable of production. Operator needs to plug well.
1749906231 2015-03-31 Production Wells No Violations This inspection was conducted with DOGRM Inspector Eric Daugstrup. See Erics report for inspection details.
1907886744 2016-04-19 Production Wells No Violations Compliance notice follow-up. Status: no change in status from previous inspection.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0704959818 US-OH-127961 2012-01-17 Well shall be plugged

For data sources see[9]

References