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Difference between revisions of "34-133-23851"

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| County: [[Portage_County,_Ohio|Portage]]
 
| County: [[Portage_County,_Ohio|Portage]]
 
|-
 
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| Municipality: [[Kent City,_Portage_County,_Ohio|Kent City]]
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| Municipality: [[Kent,_Ohio|Kent]]
 
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| Operator Name: [[PIN OAK ENERGY PARTNERS LLC]]
 
| Operator Name: [[PIN OAK ENERGY PARTNERS LLC]]

Revision as of 02:03, 1 September 2019

Well Details

Well ID: 34-133-23851
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Country: United States
State: Ohio
County: Portage
Municipality: Kent
Operator Name: PIN OAK ENERGY PARTNERS LLC
Well Pad ID:
Farm/Lease Name: BABLE
License Status: Producing
License Date: 1991-05-21
Spud Date: 1991-08-28
Spud Drilling Contractor: ADVENT DRLG
Final Drill Date: 1991-09-02
Well Total Depth: 4319 ft
Configuration: Vertical
Latitude: 41.124072544
Longitude: -81.37703536

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1991-05-21 2386 EXCALIBUR EXPLORATION INC GeoDate 5/21/91
Oil and Gas 1991-05-21 Issued Date 5/21/91 Expired Date 5/20/92 Acres 0040000 Tool Type RTAF Proposed Formation BE thru CL Proposed Depth 04319 Proposed Drill Depth 04319
Original Spud 1991-08-27
Completed 1991-09-02
Reached Total Depth 1991-09-02
Completion Report Received 1991-09-04
CO 1992-04-14 3442 CUTTER EXPLORATION INC GeoDate 5/21/91
Construction Permit Expires 1992-05-20
Change of Owner 2008-05-06 Operator changed from 3442, CUTTER EXPLORATION INC to 169, SMAIL JAMES R INC
Change of Owner 2018-11-29 Operator changed from 169, JAMES R SMAIL INC to 9722, PIN OAK ENERGY PARTNERS LLC
Record Last Modified 2018-11-29

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4114 4176 55

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 800 Gal 0 FE
H2O 0 100000 Gal 40000 FRAC W/100M GAL H20,400 SX SAN AND
CO2 0 20 Tons 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1991 CUTTER EXPLORATION INC 10350 474 90
1992 CUTTER EXPLORATION INC 41619 1144 365
1993 CUTTER EXPLORATION INC 23076 305 365
1994 CUTTER EXPLORATION INC 11555 488 365
1995 CUTTER EXPLORATION INC 7011 380 365
1996 CUTTER EXPLORATION INC 4366 234 365
1997 CUTTER EXPLORATION INC 3311 243 365
1998 CUTTER EXPLORATION INC 2768 119 365
1999 CUTTER EXPLORATION INC 2049 133 365
2000 CUTTER EXPLORATION INC 1144 204 365
2001 CUTTER EXPLORATION INC 1052 37 365
2002 CUTTER EXPLORATION INC 883 147 365
2003 CUTTER EXPLORATION INC 2389 108 365
2004 CUTTER EXPLORATION INC 1496 135 365
2005 CUTTER EXPLORATION INC 1931 67 365
2006 CUTTER EXPLORATION INC 934 68 365
2008 JAMES R SMAIL INC 144 28 150
2009 JAMES R SMAIL INC 939 69 150
2010 JAMES R SMAIL INC 1033 84 150
2011 JAMES R SMAIL INC 1057 95 365
2012 JAMES R SMAIL INC 886 95 366
2013 JAMES R SMAIL INC 1204 96 365
2014 JAMES R SMAIL INC 2018 77 365
2015 JAMES R SMAIL INC 1430 130 365
2016 JAMES R SMAIL INC 896 48 365
2017 JAMES R SMAIL INC 616 63 365
2018 JAMES R SMAIL INC 598 34 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1991 CUTTER EXPLORATION INC Brine 756 90
1992 CUTTER EXPLORATION INC Brine 1044 365
1993 CUTTER EXPLORATION INC Brine 624 365
1994 CUTTER EXPLORATION INC Brine 557 365
1995 CUTTER EXPLORATION INC Brine 420 365
1996 CUTTER EXPLORATION INC Brine 490 365
1997 CUTTER EXPLORATION INC Brine 350 365
1998 CUTTER EXPLORATION INC Brine 350 365
1999 CUTTER EXPLORATION INC Brine 270 365
2000 CUTTER EXPLORATION INC Brine 185 365
2001 CUTTER EXPLORATION INC Brine 181 365
2002 CUTTER EXPLORATION INC Brine 255 365
2003 CUTTER EXPLORATION INC Brine 360 365
2004 CUTTER EXPLORATION INC Brine 195 365
2005 CUTTER EXPLORATION INC Brine 235 365
2006 CUTTER EXPLORATION INC Brine 235 365
2008 JAMES R SMAIL INC Brine 20 150
2009 JAMES R SMAIL INC Brine 189 150
2010 JAMES R SMAIL INC Brine 146 150
2011 JAMES R SMAIL INC Brine 222 365
2012 JAMES R SMAIL INC Brine 195 366
2013 JAMES R SMAIL INC Brine 187 365
2014 JAMES R SMAIL INC Brine 189 365
2015 JAMES R SMAIL INC Brine 104 365
2016 JAMES R SMAIL INC Brine 107 365
2017 JAMES R SMAIL INC Brine 131 365
2018 PIN OAK ENERGY PARTNERS LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000010168 Preliminary Restoration No Violations PASSED Y WITNESSED 6/1/92 INSPECTOR KEITH WHITE DATE 06/0119/92 DATA FROM OLD VAX INFO
0094826428 2018-04-10 UrbanProduction Wells No Violations Status check inspection of this Clinton Sandstone well. My inspection found the wellhead fenced and locked, equipped with 2.375 tubing and rods, and operating with the aid of an electric powered pumping unit. This well produces to a diked, fenced, and locked tank battery to the east and contains one (1) 100 barrel tank, a 30 barrel poly tank, and a horizontal separator. The required ID is posted at the wellhead and at the tank battery. No violations.
1382558910 2013-10-23 UrbanProduction Wells No Violations I was on location at the request of Jeff Schonauer (JR Smail) to investigate possible contamination of a water well located by this oil and gas well. Jeff responded to the landowner the previous day (10-22-13) and his gas meter was triggered by running hot water in the shop restroom. His meter did not have the capability of distinguishing the source of the alarm and he contacted me asked if I could investigate. I met with Jeff and the landowner this morning to investigate. I calibrated the PHD6 gas meter prior to entering the premises. I spoke with the landowner and he indicated to me that the well water had a strong odor and was not sure if it was gas or oilfield substances and smelled like sulfur. He was not sure how long it has been like that and that he only notices it when he is not around the shop for awhile and returns. He said several customers have also noticed the smell. He took me into the restroom where he showed me the water softner, pressure tank, and sediment filter that were installed. The sediment filter appeared black and he told me he changes it once every week. There was an obvious sulfur odor around the equipment, but I did not detect any methane. I began running cold water in the sink and analyzing with the meter. I ran the water for several minutes and registered a reading of 0.05ppm on the CH4 (methane) gauge for several seconds and it returned to 0ppm. No LEL (lower explosive limit), H2S (hydrogen sulfide), or CO (carbon monoxide) was detected. I began testing the hot water and in about 30 seconds the CO levels were at 35ppm and triggered the alarm on the PHD6. The meter reading topped out at 63ppm of carbon monoxide and the LEL reached a reading of 2%. Methane was detected at a concentration of 0.10ppm and no H2S was detected during the hot water test. The hot water had an obvious sulfur smell during the test. I ran a low-level Quantab to test for chlorides and registered a 1.6 on the strip which equates to 43ppm of chlori

For data sources see[9]

References