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| County: [[Knox_County,_Ohio|Knox]] | | County: [[Knox_County,_Ohio|Knox]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Butler_Township,_Knox_County,_Ohio|Butler Township]] |
|- | |- | ||
| Operator Name: [[MARAM ENERGY INC]] | | Operator Name: [[MARAM ENERGY INC]] |
Well ID: 34-083-23248 | Loading map...
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Country: United States | |
State: Ohio | |
County: Knox | |
Municipality: Butler Township | |
Operator Name: MARAM ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: STRICKER MABEL | |
License Status: Producing | |
License Date: 1982-12-10 | |
Spud Date: 1983-06-06 | |
Spud Drilling Contractor: R I G DRILLING | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 40.362037430 | |
Longitude: -82.20781018 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1982-12-10 | 437 TRI STATE DRILLING GeoDate 12/10/82 |
Oil and Gas | 1982-12-10 | Issued Date 12/10/82 Expired Date 6/8/83 Acres 0062000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1983-06-06 | PERMIT EXPIRED. |
Construction Permit Expires | 1983-06-08 | PERMIT EXPIRED. |
CO | 1995-07-15 | 2070 HALWELL COMPANY GeoDate 12/10/82 |
Change of Owner | 2002-03-18 | Operator changed from 2070, HALWELL COMPANY to 476, MARAM ENERGY CO |
Record Last Modified | 2015-09-24 | PERMIT EXPIRED. |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | R I G DRILLING INC | 0 | 81 | 365 |
1987 | R I G DRILLING INC | 0 | 148 | 365 |
1988 | R I G DRILLING INC | 0 | 70 | 365 |
1990 | R I G DRILLING INC | 0 | 69 | 365 |
1992 | R I G DRILLING INC | 0 | 66 | 365 |
1995 | STONEBRIDGE OPERATING CO LLC | 29 | 48 | 276 |
1996 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 0 |
1997 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 0 |
1998 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 0 |
2000 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 364 |
2001 | STONEBRIDGE OPERATING CO LLC | 0 | 0 | 0 |
2002 | MARAM ENERGY INC | 0 | 0 | 0 |
2003 | MARAM ENERGY INC | 0 | 0 | 0 |
2004 | MARAM ENERGY INC | 0 | 0 | 0 |
2005 | MARAM ENERGY INC | 0 | 0 | 0 |
2006 | MARAM ENERGY INC | 0 | 0 | 0 |
2007 | MARAM ENERGY INC | 0 | 0 | 0 |
2008 | MARAM ENERGY INC | 0 | 0 | 0 |
2009 | MARAM ENERGY INC | 0 | 0 | 0 |
2010 | MARAM ENERGY INC | 0 | 0 | 0 |
2011 | MARAM ENERGY INC | 0 | 0 | 0 |
2012 | MARAM ENERGY INC | 0 | 0 | 0 |
2013 | MARAM ENERGY INC | 0 | 0 | 0 |
2014 | MARAM ENERGY INC | 0 | 0 | 60 |
2015 | MARAM ENERGY INC | 0 | 63 | 365 |
2016 | MARAM ENERGY INC | 0 | 0 | 365 |
2017 | MARAM ENERGY INC | 0 | 0 | 365 |
2018 | MARAM ENERGY INC | 0 | 62 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | R I G DRILLING INC | Brine | 0 | 365 |
1987 | R I G DRILLING INC | Brine | 0 | 365 |
1988 | R I G DRILLING INC | Brine | 0 | 365 |
1990 | R I G DRILLING INC | Brine | 0 | 365 |
1992 | R I G DRILLING INC | Brine | 0 | 365 |
1995 | STONEBRIDGE OPERATING CO LLC | Brine | 18 | 276 |
1996 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 0 |
1997 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 0 |
1998 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 0 |
2000 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 364 |
2001 | STONEBRIDGE OPERATING CO LLC | Brine | 0 | 0 |
2002 | MARAM ENERGY INC | Brine | 0 | 0 |
2003 | MARAM ENERGY INC | Brine | 0 | 0 |
2004 | MARAM ENERGY INC | Brine | 0 | 0 |
2005 | MARAM ENERGY INC | Brine | 0 | 0 |
2006 | MARAM ENERGY INC | Brine | 0 | 0 |
2007 | MARAM ENERGY INC | Brine | 0 | 0 |
2008 | MARAM ENERGY INC | Brine | 0 | 0 |
2009 | MARAM ENERGY INC | Brine | 0 | 0 |
2010 | MARAM ENERGY INC | Brine | 0 | 0 |
2011 | MARAM ENERGY INC | Brine | 0 | 0 |
2012 | MARAM ENERGY INC | Brine | 0 | 0 |
2013 | MARAM ENERGY INC | Brine | 0 | 0 |
2014 | MARAM ENERGY INC | Brine | 40 | 60 |
2015 | MARAM ENERGY INC | Brine | 0 | 365 |
2016 | MARAM ENERGY INC | Brine | 0 | 365 |
2017 | MARAM ENERGY INC | Brine | 120 | 365 |
2018 | MARAM ENERGY INC | Brine | 40 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
000PL14767 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
001287i586 | 2002-02-06 | Production Wells | Violations Noted | not properly identified |
0017482786 | 2012-09-05 | Production Wells | No Violations | Met with Shawn Baldridge with Maram Energy at this location. Informed him that the well is idle and needs to be placed into production or plugged. He said they would begin work immediately on placing well into production. |
0368778406 | 2012-09-14 | Production Wells | No Violations | I inspected this location today. The brush has been cleared from the lease road making it accessible. The well was equipped with a pumping unit. It was not connected to a tank. |
0592331439 | 2012-06-12 | Production Wells | Violations Noted | Today I conducted an inspection on this well. I arrived at approximately 12:30 pm. The inspection revealed that the well is equipped with a pumping unit but is not capable of production. Thick brush and vegetation surrounded the well. The flow lines connecting the well to the tank have been disconnected. The access road to the well is not accessible. There was no legible identification at the well or at the tank. This well shall be plugged or put back into production. |
0915587111 | 2002-02-06 | Production Wells | Violations Noted | FOLLOW UP TO NOV # 1287i586 not properly identified NOV TERMINATED BASED ON COMPLINACE INSPECTION BY ROCKY KING ON 10/23/2002. |
1014920987 | 2002-10-23 | Production Wells | No Violations | compliance |
1018942825 | 2012-06-12 | Production Wells | Violations Noted | FOLLOW UP TO NOV # -592331439 Today I conducted an inspection on this well. I arrived at approximately 12:30 pm. The inspection revealed that the well is equipped with a pumping unit but is not capable of production. Thick brush and vegetation surrounded the well. The flow lines connecting the well to the tank have been disconnected. The access road to the well is not accessible. There was no legible identification at the well or at the tank. This well shall be plugged or put back into production. |
1374671905 | 2013-07-24 | Production Wells | Violations Noted | I inspected this well today well has proper Id and is capable of production. |
1704080414 | 2012-11-29 | Production Wells | No Violations | I inspected this well today. Marams service rig is on the well. Doug with Maram Energy was on location. He informed me that the well is back to pumping. A new flow line will be placed from the well to the tank. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
001287i586 | US-OH-108082 | 2002-02-06 | Failure to legibly identify well | |
0592331439 | US-OH-126669 | 2012-06-27 | Failure to legibly identify well | |
0592331439 | US-OH-126670 | 2012-06-27 | Statement of annual production not filed | |
0915587111 | US-OH-130468 | 2002-02-06 | Failure to legibly identify well | |
1018942825 | US-OH-100269 | 2013-10-23 | Failure to legibly identify well | |
1374671905 | US-OH-111102 | 2014-01-27 | Failure to legibly identify well |
For data sources see[7]