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37-129-28672

Well Details

Well ID: 37-129-28672
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County: Westmoreland
Municipality: Derry Township
Operator Name: WPX ENERGY APPALACHIA LLC
Well Pad ID: 145142
Farm/Lease Name: DURALIA 1-6H
First Permit Date: 2011-09-12
Last Permit Date: 2011-09-12
Spud Date: 2011-11-08
Unconventional: Yes
Horizontal: Yes
Producing: Yes
Violations: None
Latitude: 40.37665
Longitude: -79.280369

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
2013962 2011-10-26 No Violations Noted Site visit was part of routine inspection.

Met with Anton Francois(Company Man). HP Flex rig 287 drilling. Currently drilling first hole. Site was well vegetated. Access road and pad were slightly rutted and muddy. E&S and BMPs were installed as per E&S plan and were working adequately. Performing closed looped drilling practice (ie no pits) Impoundment in place with small amount of water. No violations noted at this time.

2019646 2011-11-16 No Violations Noted Fred Webb and Jimmy Ballew were the company men on site. AP was tool pusher for HP.

On Friday (11-11-11) a pump plugged near the well head. The hoses spilled there contents (oil based drilling mud) when an attempt was made to correct the situation. The contents of the hose(s) spilled on to the pad liner. Mr. Webb estimated that about 20 gallons of mud was spilled on the containment. This mud was immediately vac'ed from the spill area. No mud traveled from containment to the pad. PPC plan, E&S plan and site drawings were available at the head of the access road. BMPs were installed and maintained. There continued to be steady rain at the time of inspection. Some sedimentaion was occuring along the ditching around the pad. Considering the precipitation, the sedimentation was minimal. The discharge entered a rock line channel, followed by sed socks. No sedimentation was leaving the site. No violations noted at this time.

2026854 2011-12-14 No Violations Noted Site visit was part of routine inspection.

Rig had been removed from site. Three holes had been drilled. Water trucks were actively hauling water to site and filling impoundment. BMPs were in place and functioning properly. No violations noted at this time.

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-2 0.0 0.0 0.0 0.0 0.0 0.0
2012-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2011-2 DRILLING FLUID WASTE 1200.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0254185 RESERVED ENVIRONMENTAL SERVICES MOUNT PLEASANT PA
2011-2 DRILL CUTTINGS 2707.35 Tons LANDFILL 100277 WESTMORELAND WASTE, LLC BELLE VERNON PA

References