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Well ID: 34-147-20402 | Loading map...
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Country: United States | |
State: Ohio | |
County: Seneca | |
Municipality: Thompson Township | |
Operator Name: FRANKLIN GAS & OIL CO LLC | |
Well Pad ID: | |
Farm/Lease Name: KISTLER UNIT | |
License Status: Final Restoration | |
License Date: 2006-04-04 | |
Spud Date: 2006-05-06 | |
Spud Drilling Contractor: CAPSTAR DRILLING | |
Final Drill Date: 2006-05-13 | |
Well Total Depth: 2711.00 ft | |
Configuration: Vertical | |
Latitude: 41.240000 | |
Longitude: -82.880000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2006-04-04 | Proposed Formations:TRENTON THRU TREMPEALEAU, Issued Date:4/4/2006, Expired Date:4/4/2007 6:00:00 AM, Drilling unit acres:41.7194, Proposed Well Type:OG, Proposed Well Class:EW |
Original Spud | 2006-05-06 | RBDMS Rec |
Completed | 2006-05-13 | RBDMS Rec |
Reached Total Depth | 2006-05-13 | RBDMS Rec |
Plugged/Abandoned | 2006-05-14 | RBDMS Rec |
Completion Report Received | 2006-12-15 | RBDMS Rec |
Construction Permit Expires | 2007-04-04 | RBDMS Rec |
Record Last Modified | 2013-03-14 | RBDMS Rec |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1371409136 | 2007-8-30 0:00: | DD | No Violations | |
-391729404 | 2006-5-8 0:00:0 | DD | No Violations | |
-674991151 | 2007-9-4 0:00:0 | DD | No Violations | |
0016816559 | 2006-06-28 | Final Restoration | No Violations | Inspect site. Site graded, final restoration. |
0391729404 | 2006-05-08 | Drill / Deepen / Reopen | No Violations | Called out for Surface casing. Drilled for surface pipe to about 650 feet. Attempt to run surface pipe, obstructions about 234 feet. Pull pipe and run bit in hole. Leave site. |
0674991151 | 2007-09-04 | Drill / Deepen / Reopen | No Violations | Inspect location. Drill cable under tension. In process of retrieving bit. |
1150715427 | 2006-05-14 | Plug / Plug Back | No Violations | Plug well on rig through drill pipe. |
1153488879 | 2006-05-06 | Drill / Deepen / Reopen | No Violations | Inspect Drill site.Rig broke down. Conductor set to 30 feet. Working on Surface casing hole. |
1159539123 | 2006-05-09 | Drill / Deepen / Reopen | No Violations | Inspect location. Jim Dixon onsite to coordinate activities. Mix mud and attempt to obtain circulation. |
1371409136 | 2007-08-30 | Drill / Deepen / Reopen | No Violations | Inspect location. Drilling continues. Drill bit currently lost in hole. |
1558287129 | 2006-05-10 | Drill / Deepen / Reopen | No Violations | Surface casing. 8.625 inch casing became plugged and was drilled out. Circulation to the surface was not established. Wiper plug sent down hole on wireline. Baskets set at 4th and 6th joints. Water zones present at 130 feet and 334 feet. Cobble size material was washed to the surface from the 334 foot zone. Installation of surface pipe was complicated by trap door type situation. Upon completion of cementing the upper portion of the surface casing was attempted to be cemented. One bag of hulls was poured into the annulus from the surface, four bags of bentonite gel were poured into annulus from surface, cement was pumped from the surface into the annulus. Total depth of surface casing was 688 feet. |
16816559 | 2006-6-28 0:00: | FR | No Violations |
For data sources see[3]