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Well ID: 34-085-20169 | Loading map...
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Country: United States | |
State: Ohio | |
County: Lake | |
Municipality: Madison Township | |
Operator Name: BUCKEYE RESOURCES INC | |
Well Pad ID: | |
Farm/Lease Name: MIKLICH UNIT | |
License Status: Orphan Well - Ready | |
License Date: 1973-05-09 | |
Spud Date: 1973-08-21 | |
Spud Drilling Contractor: | |
Final Drill Date: 1973-10-11 | |
Well Total Depth: 3061.00 ft | |
Configuration: Vertical | |
Latitude: 41.770000 | |
Longitude: -81.090000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1801-01-02 | 1192 TIMBERLINE OIL CO |
Oil and Gas | 1802-01-01 | |
Original Spud | 1973-08-21 | REV. LOC. 8-15-73, C.S. Orphan Well Case #2017 03 007 |
Completed | 1973-10-11 | REV. LOC. 8-15-73, C.S. Orphan Well Case #2017 03 007 |
Reached Total Depth | 1973-10-11 | REV. LOC. 8-15-73, C.S. Orphan Well Case #2017 03 007 |
Change of Owner | 1997-11-28 | Operator changed from 1192, TIMBERLINE OIL CO to 693, BUCKEYE RESOURCES INC |
Record Last Modified | 2019-04-03 | REV. LOC. 8-15-73, C.S. Orphan Well Case #2017 03 007 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 2886 | 2930 | 16 |
2886 | 2930 | 16 | |
2886 | 2930 | 16 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 3000 Bbl | 35000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | TIMBERLINE OIL CO | 1137.00 | 46.00 | 365 |
1988 | TIMBERLINE OIL CO | 884.00 | 0.00 | 365 |
1989 | TIMBERLINE OIL CO | 647.00 | 65.00 | 365 |
1990 | TIMBERLINE OIL CO | 710.00 | 0.00 | 365 |
1991 | TIMBERLINE OIL CO | 954.00 | 0.00 | 365 |
1993 | TIMBERLINE OIL CO | 618.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | TIMBERLINE OIL CO | Brine | 125 | 365 |
1988 | TIMBERLINE OIL CO | Brine | 240 | 365 |
1989 | TIMBERLINE OIL CO | Brine | 145 | 365 |
1990 | TIMBERLINE OIL CO | Brine | 290 | 365 |
1991 | TIMBERLINE OIL CO | Brine | 320 | 365 |
1993 | TIMBERLINE OIL CO | Brine | 151 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-577189278 | 2016-1-5 0:00:0 | UP | No Violations | 1.00 |
0577189278 | 2016-01-05 | UrbanProduction Wells | No Violations | I inspected this well location as part of an evaluation of current site conditions. The well and battery are located on an otherwise undeveloped parcel. Much of the parcel is overgrown with tall, grassy, wetland-type vegetation. At the time of this inspection, the following elements were present: a wellhead with 8 5/8-inch surface casing, 3.5-inch production casing, and mechanical plunger lift. I observed gas leaking from the around the 8 5/8-inch casing. There was a battery with one 210-barrel steel production tank, one 100-barrel steel, horizontal brine tank, and separator unit. The various elements show significant corrosion and lack of maintenance. I observed numerous perforating holes in the production tank. To date, the owner of record has not responded to attempts to contact them. Liability insurance coverage has lapsed. |
0941009314 | 2017-08-23 | Orphan | No Violations | My inspection found no changes since my last inspection. |
1259170136 | 2017-02-21 | Orphan | No Violations | I inspected this well as part of an evaluation for possible inclusion into the Idle & Orphan Well Program. At the time of this inspection, I observed the following: The production system was comprised of a wellhead and associated tank battery located in an otherwise undeveloped parcel with low-lying and poorly-drained areas surrounding. I observed gas leaking from the surface casing, which was submerged under standing surface water within a thicket of tall, wetlands-type grassy vegetation. The supply-line and domestic connections were closed. There was an associated tank battery comprised of one 210-barrel steel production tank, one 100-barrel steel tank (laying on its side), and a horizontal separator located adjacent to the main roadway. The fittings and connections at the wellhead and battery exhibited severe corrosion with no signs of recent maintenance. The gravel-paved access road was rutted and displayed some ponded areas but was drivable to the wellhead. |
1488914772 | 2017-03-07 | Orphan | No Violations | My inspection found the well to be equipped with 8.625 and 3.5 casing. The 3.5 well casing is plumbed up above ground and has a wellhead tree in place. There is natural gas leaking up around the base of the well that is under water. There is a domestic supply that is currently shut in, plumbed into the 3.5 casing. There is a 2 flow line plumbed from the wellhead to the tank battery. The tank battery consists of a 210 BBL production tank, a 100 BBL brine tank, and a mechanical separator. There are no overhead obstructions above the tank battery or the well. The well is easily accessed from a previous lease road. |
1570630682 | 2019-10-9 0:00: | OR | No Violations | |
941009314 | 2017-8-23 0:00: | OR | No Violations |
For data sources see[9]