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34-031-20757

Well Details

Well ID: 34-031-20757
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Country: United States
State: Ohio
County: Coshocton
Municipality: Tiverton Township
Operator Name: HELMS OIL
Well Pad ID:
Farm/Lease Name: GIAUQUE MELVILLE
License Status: Producing
License Date:
Spud Date: 1955-05-31
Spud Drilling Contractor:
Final Drill Date: 1955-07-12
Well Total Depth: 3244.00 ft
Configuration: Vertical
Latitude: 40.440000
Longitude: -82.180000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1955-05-31 165.5 ACRES FORMATION DRILLED=2ND
CO 1955-06-10 710 WISER OIL CO GeoDate 6/10/55
Completed 1955-07-12 165.5 ACRES FORMATION DRILLED=2ND
Reached Total Depth 1955-07-12 165.5 ACRES FORMATION DRILLED=2ND
Record Last Modified 2013-10-03 165.5 ACRES FORMATION DRILLED=2ND

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1989 WISER OIL CO 0.00 100.00 365
1990 WISER OIL CO 0.00 100.00 365
1991 WISER OIL CO 0.00 100.00 365
1992 WISER OIL CO 0.00 50.00 365
1993 FERENBAUGH ALBERT OR DENISE 0.00 115.00 365
1995 FERENBAUGH ALBERT OR DENISE 0.00 243.00 365
1996 FERENBAUGH ALBERT OR DENISE 0.00 75.00 365
1997 HELMS OIL 0.00 78.00 365
1998 HELMS OIL 0.00 78.00 365
1999 HELMS OIL 0.00 78.00 365
2000 HELMS OIL 0.00 78.00 365
2001 HELMS OIL 0.00 78.00 365
2002 HELMS OIL 0.00 78.00 365
2003 HELMS OIL 0.00 70.00 365
2004 HELMS OIL 0.00 70.00 365
2005 HELMS OIL 0.00 70.00 365
2006 HELMS OIL 0.00 70.00 365
2007 HELMS OIL 0.00 70.00 365
2008 HELMS OIL 0.00 70.00 365
2009 HELMS OIL 0.00 164.00 365
2010 HELMS OIL 0.00 702.00 365
2011 HELMS OIL 0.00 605.00 365
2012 HELMS OIL 0.00 713.00 366
2013 HELMS OIL 0.00 244.00 365
2014 HELMS OIL 0.00 82.00 365
2015 HELMS OIL 0.00 237.00 365
2016 HELMS OIL 0.00 159.00 365
2017 HELMS OIL 0.00 186.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1989 WISER OIL CO Brine 15 365
1990 WISER OIL CO Brine 15 365
1991 WISER OIL CO Brine 17 365
1992 WISER OIL CO Brine 10 365
1993 FERENBAUGH ALBERT OR DENISE Brine 90 365
1995 FERENBAUGH ALBERT OR DENISE Brine 30 365
1996 FERENBAUGH ALBERT OR DENISE Brine 15 365
1997 HELMS OIL Brine 20 365
1998 HELMS OIL Brine 20 365
1999 HELMS OIL Brine 20 365
2000 HELMS OIL Brine 20 365
2001 HELMS OIL Brine 20 365
2002 HELMS OIL Brine 20 365
2003 HELMS OIL Brine 20 365
2004 HELMS OIL Brine 20 365
2005 HELMS OIL Brine 20 365
2006 HELMS OIL Brine 20 365
2007 HELMS OIL Brine 20 365
2008 HELMS OIL Brine 20 365
2009 HELMS OIL Brine 60 365
2010 HELMS OIL Brine 0 365
2011 HELMS OIL Brine 0 365
2012 HELMS OIL Brine 360 366
2013 HELMS OIL Brine 60 365
2014 HELMS OIL Brine 0 365
2015 HELMS OIL Brine 0 365
2016 HELMS OIL Brine 0 365
2017 HELMS OIL Brine 70 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1196330483 2009-1-27 0:00: PW No Violations
-930913280 2008-10-28 0:00 PW No Violations
0501173567 2015-05-06 Production Wells No Violations On the day of my inspection I found that no identification was posted. I contacted Terry Helms to remind him that his well was in violation and that he needed to get the ID posted.
0560712423 2004-06-22 Production Wells No Violations Well in production . Tanks just painted . No id , THIS WELL IS OWNED BY HELMES OIL OWNER # 5725
0588194237 2015-03-03 Production Wells Violations Noted On the day of my inspection I found that the wellhead was equipped with a pumping unit. The tank battery consisted of one 100 barrel tank and one 30 barrel tank. There was no identification posted for this well. 1501:9-9-05(A)10 states that all producing leases shall be legibly identified in a conspicuous place on or near the well-head or the storage tank(s) as to owner, lease name, well number, permit number, county, and an emergency telephone number.
0930913280 2008-10-28 Production Wells Violations Noted Well capable of production . Well is using common storage tanks . No identification at well head . Oil around well head 3 sq. area . Brine tank inside dike is leaking . Brine kill area outside dike approximately 40 by 5 wide . Storage tanks are 10 fro Identify well head with all well information . Remove Brine tanks from dike area , replace if needed . Storage tanks are to be set no closer then 50 from roadway, reset storage tanks and dike to hold 110 % of storage tanks .
1066473512 2008-12-09 Production Wells No Violations Work started on violations , Storage tanks have been moved . Old storage tank area not graded . Well head not identified this inspection . Work not complete .
1078762278 2018-01-02 Production Wells No Violations On the day of my inspection I found that the well was equipped with an electric powered pumping unit. The motor, drive belts and electric were intact. The flow lines were connected at the wellhead and the valves were open. The production equipment consisted of one 100 barrel steel tank and one 30 barrel steel tank in a shallow earthen dike. Correct, legible identification was posted and I found no leaks or spills.
1176934532 2007-04-18 Production Wells No Violations Well capable of production .
1182632789 2015-05-15 Production Wells No Violations On the day of my inspection I found that there was still no identification posted. I called and left another message with Terry Helms.
1196330483 2009-01-27 Production Wells No Violations Well capable of production . Identified at storage tank , not at well head .
1401358205 2015-04-03 Production Wells No Violations On the day of my inspection I found that nothing had been done to bring this well into compliance. There was no identification posted at the tank battery or wellhead.
1575507802 2015-06-01 Production Wells No Violations On the day of my inspection I found that correct identification was posted at the wellhead and tank battery. This violation is resolved.
2057513384 2010-05-26 Production Wells No Violations Identification posted . Compliance .
2078789460 2005-08-04 Production Wells No Violations Well in production.
2121893757 2020-4-9 0:00:0 PW No Violations 0.50
2140613640 2015-04-15 Production Wells No Violations On the day of my inspection I found that identification was still not posted at this well. I met with Roger Helms at the well site. I told him that the well was in violation and it needs identification.
501173567 2015-5-6 0:00:0 PW No Violations
560712423 2004-6-22 0:00: PW No Violations
588194237 2015-3-3 0:00:0 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0588194237 US-OH-126614 2015-08-03 Failure to legibly identify well
0930913280 US-OH-130641 2008-10-28 Well operation causing pollution and contamination
0930913280 US-OH-130642 2008-10-28 Failure to legibly identify well
0930913280 US-OH-130643 2008-10-28 Violation of tank spacing requirements

For data sources see[7]

References