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Well ID: 34-065-20138 | Loading map...
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Country: United States | |
State: Ohio | |
County: Hardin | |
Municipality: Jackson Township | |
Operator Name: KNOX ENERGY INC. | |
Well Pad ID: | |
Farm/Lease Name: KELLOGG | |
License Status: Final Restoration | |
License Date: 2012-03-20 | |
Spud Date: 1999-03-18 | |
Spud Drilling Contractor: G & H DRLG | |
Final Drill Date: 1999-03-20 | |
Well Total Depth: 1729.00 ft | |
Configuration: Vertical | |
Latitude: 40.750000 | |
Longitude: -83.540000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 1999-03-06 | Proposed Formations:TRENTON, Issued Date:3/6/99, Expired Date:3/5/00 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Original Spud | 1999-03-18
WELL INSPECTED 10/11/2002 BY SAM FAUST. | |
Reached Total Depth | 1999-03-20
WELL INSPECTED 10/11/2002 BY SAM FAUST. | |
Correction to Well | 1999-03-26 | CHANGE IN PTD: 1900'. CHANGE IN WELL CLASS: EDPW. CHANGE IN FORMATION: TRENTON-GULL RIVER |
Completion Report Received | 2000-01-24
WELL INSPECTED 10/11/2002 BY SAM FAUST. | |
Completed | 2000-03-20
WELL INSPECTED 10/11/2002 BY SAM FAUST. | |
APP | 2000-07-03 | Proposed Formations:GULL RIVER, Issued Date:07/03/2000, Expired Date:07/03/2001 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2004-11-22 | Operator changed from 5728, MEDICINE BOW OPERATING CO to 6295, KNOX ENERGY INC. |
APP | 2012-03-20 | Proposed Formations:TRENTON, Issued Date:3/20/2012, Expired Date:3/20/2014 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-05-07
WELL INSPECTED 10/11/2002 BY SAM FAUST. | |
Construction Permit Expires | 2014-03-20
WELL INSPECTED 10/11/2002 BY SAM FAUST. | |
Record Last Modified | 2014-07-25
WELL INSPECTED 10/11/2002 BY SAM FAUST. |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 0 | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2009 | KNOX ENERGY INC. | 0.00 | 0.00 | 0 |
2010 | KNOX ENERGY INC. | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2009 | KNOX ENERGY INC. | Brine | 0 | 0 |
2010 | KNOX ENERGY INC. | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0489528420 | 2002-09-10 | Final Restoration | No Violations | Final restoration done. |
1172714467 | 2012-11-13 | Production Wells | No Violations | At the time of my inspection the well was located in a farm field with no access lane or production equipment. The well is scheduled to be plugged sometime after Thanksgiving. At this time the well has a FR Status and needs to be changed. |
1367932119 | 2013-05-07 | Plug / Plug Back | No Violations | At the time of the inspection plugging operations were completed by Berry Well Service/Knox Energy and Petroset Cementing. All plugs were set through 2 3/8 tubing with good circulation throughout the job. See Plug Report for details. |
489528420 | 2002-9-10 0:00: | FR | No Violations |
For data sources see[8]