X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-067-20157

Well Details

Well ID: 34-067-20157
Loading map...
Country: United States
State: Ohio
County: Harrison
Municipality: Monroe Township
Operator Name: ATLAS NOBLE LLC
Well Pad ID:
Farm/Lease Name: S W WOOD UNIT
License Status: Final Restoration
License Date: 2011-12-20
Spud Date: 1972-08-23
Spud Drilling Contractor:
Final Drill Date: 1972-08-31
Well Total Depth: 5600.00 ft
Configuration: Vertical
Latitude: 40.380000
Longitude: -81.250000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1972-08-23
Completed 1972-08-31
Reached Total Depth 1972-08-31
CO 1980-06-19 42 COLLINS-MCGREGOR OPER CO GeoDate 6/19/80 FROM SIMPSON & CROCKETT
Change of Owner 2001-05-17 Operator changed from 42, COLLINS-MCGREGOR OPER CO to 43, RESOURCE AMERICA INC
Change of Owner 2004-03-12 Operator changed from 43, RESOURCE AMERICA INC to 6867, ATLAS AMERICA INC
Change of Owner 2011-01-27 Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC
Change of Owner 2011-02-08 Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC
APP 2011-12-20 Proposed Formations:CLINTON, Issued Date:12/20/2011, Expired Date:12/19/2013 12:00:00 PM, Drilling unit acres:118.41, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2012-05-21
Construction Permit Expires 2013-12-19
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5458 5488 18
5458 5488 18
5458 5488 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1833 Bbl 48000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 COLLINS-MCGREGOR OPERATING CO 0.00 433.00 365
1985 COLLINS-MCGREGOR OPERATING CO 0.00 541.00 365
1986 COLLINS-MCGREGOR OPERATING CO 0.00 266.00 365
1987 COLLINS-MCGREGOR OPERATING CO 0.00 0.00 365
1988 COLLINS-MCGREGOR OPERATING CO 0.00 225.00 365
1989 COLLINS-MCGREGOR OPERATING CO 0.00 553.00 365
1990 COLLINS-MCGREGOR OPERATING CO 0.00 388.00 365
1991 COLLINS-MCGREGOR OPERATING CO 0.00 304.00 365
1992 COLLINS-MCGREGOR OPERATING CO 0.00 392.00 0
1993 COLLINS-MCGREGOR OPERATING CO 0.00 320.00 365
1994 COLLINS-MCGREGOR OPERATING CO 0.00 316.00 365
1995 COLLINS-MCGREGOR OPERATING CO 0.00 214.00 365
1996 COLLINS-MCGREGOR OPERATING CO 0.00 152.00 365
1997 COLLINS-MCGREGOR OPERATING CO 0.00 216.00 365
1998 COLLINS-MCGREGOR OPERATING CO 0.00 0.00 365
1999 COLLINS-MCGREGOR OPERATING CO 0.00 150.00 365
2000 COLLINS-MCGREGOR OPERATING CO 0.00 131.00 365
2001 RESOURCE AMERICA INC 0.00 15.00 365
2002 RESOURCE AMERICA INC 0.00 0.00 365
2003 RESOURCE AMERICA INC 0.00 0.00 365
2004 CHEVRON APPALACHIA LLC 0.00 0.00 365
2005 CHEVRON APPALACHIA LLC 0.00 0.00 365
2006 CHEVRON APPALACHIA LLC 0.00 0.00 365
2007 CHEVRON APPALACHIA LLC 0.00 0.00 365
2008 CHEVRON APPALACHIA LLC 0.00 0.00 366
2009 CHEVRON APPALACHIA LLC 0.00 0.00 365
2010 ATLAS NOBLE LLC 0.00 0.00 365
2011 CHEVRON APPALACHIA LLC 0.00 0.00 365
2012 ATLAS NOBLE LLC 0.00 0.00 366

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 COLLINS-MCGREGOR OPERATING CO Brine 0 365
1985 COLLINS-MCGREGOR OPERATING CO Brine 100 365
1986 COLLINS-MCGREGOR OPERATING CO Brine 50 365
1987 COLLINS-MCGREGOR OPERATING CO Brine 75 365
1988 COLLINS-MCGREGOR OPERATING CO Brine 0 365
1989 COLLINS-MCGREGOR OPERATING CO Brine 0 365
1990 COLLINS-MCGREGOR OPERATING CO Brine 100 365
1991 COLLINS-MCGREGOR OPERATING CO Brine 135 365
1992 COLLINS-MCGREGOR OPERATING CO Brine 198 0
1993 COLLINS-MCGREGOR OPERATING CO Brine 185 365
1994 COLLINS-MCGREGOR OPERATING CO Brine 235 365
1995 COLLINS-MCGREGOR OPERATING CO Brine 159 365
1996 COLLINS-MCGREGOR OPERATING CO Brine 145 365
1997 COLLINS-MCGREGOR OPERATING CO Brine 169 365
1998 COLLINS-MCGREGOR OPERATING CO Brine 165 365
1999 COLLINS-MCGREGOR OPERATING CO Brine 156 365
2000 COLLINS-MCGREGOR OPERATING CO Brine 0 365
2001 RESOURCE AMERICA INC Brine 0 365
2002 RESOURCE AMERICA INC Brine 0 365
2003 RESOURCE AMERICA INC Brine 0 365
2004 CHEVRON APPALACHIA LLC Brine 0 365
2005 CHEVRON APPALACHIA LLC Brine 0 365
2006 CHEVRON APPALACHIA LLC Brine 0 365
2007 CHEVRON APPALACHIA LLC Brine 0 365
2008 CHEVRON APPALACHIA LLC Brine 0 366
2009 CHEVRON APPALACHIA LLC Brine 0 365
2010 ATLAS NOBLE LLC Brine 0 365
2011 CHEVRON APPALACHIA LLC Brine 0 365
2012 ATLAS NOBLE LLC Brine 50 366

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1690647774 2016-6-22 0:00: FR No Violations 1.50
0001239i53 2001-06-15 Production Wells No Violations Check well status for H 2 S gas. The blocker that was placed in well seems to be holding the H 2 S in place and there are no leaks at this time.
0005369022 2002-12-04 Production Wells No Violations Check well status for H 2 S gas. The blocker that was placed in well seems to be holding the H 2 S in place and there are no leaks at this time.
0024076065 2002-04-23 Production Wells No Violations This well has a history of H 2 S leaks . Check well and did not find any leaks.
1239i53 2001-6-15 0:00: PW No Violations 75.00
1318962960 2011-10-18 Production Wells Violations Noted I conducted an inspection of this well site on a complaint by Teresa Moore of an idle well. She has stated that it has been quite sometime since the well has produced any oil or gas. Our database records indicate that the last production (15 barrels of oil and zero gas) was reported in 2001 by Resource America. Our database records also show that the well was transferred from Collins-McGregor Operating to Resource America on 5/17/01. The well was then transferred from Resource America to Atlas America on 3/12/04. On 2/08/11 Atlas America transferred the well to Atlas Noble. My inspection found that there has been no recent production activity around the well or the tank battery. The pittman arms on the pumping unit have been cut with a cuting torch, the weights have been cut off the walking beam, and the electric motor has been removed. There is an H2S gas odor around the wellhead area. I observed a 1 line near the wellhead has been corroded off and the valve is laying on the ground. This valve has turned black/green from the corrosive properties of the H2S gas. Note: There is no gas leaking from the 1 line where the valve was located. The tank battery is equipped with one 100 barrel oil storage tank, a 50 barrel brine storage tank and a production type separator. The door on the gas meter is open and there is no chart on the meter. Trees and other vegetation have grown up around the separator. The well can be classified as idle due to lack of production as required by CH. 1509.062 ORC. The well owner needs to either properly plug the well, place the well back into production, or take the appropriate steps to place the well into Temporary Inactive status. Remedial action must be completed by December 1st, 2011 or the appropriate enforcement actions will be taken.
1340904609 2012-06-22 Plug / Plug Back No Violations The well site has been graded and the pit closed.
1389840298 2014-01-15 Production Wells No Violations I am checking the status of this well today to see if the well has been plugged or is in production. I found that the well was plugged on 05/21/2013 . Shawn Murphy was the Inspector and did not complete a plug report before he left ODNR. The final restoration could not be passed today because I could not see the site due to ice and snow.
1690647774 2016-06-22 Final Restoration No Violations On the day of my inspection, I witnessed that the final restoration has been complete. The site passed final restoration according to ORC 1509.072(B).
24076065 2002-4-23 0:00: PW No Violations 1.00
5369022 2002-12-4 0:00: PW No Violations 75.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1318962960 US-OH-109098 2011-10-18 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[9]

References