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34-111-24068

Well Details

Well ID: 34-111-24068
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Country: United States
State: Ohio
County: Monroe
Municipality: Wayne Township
Operator Name: HOWELLS OIL & GAS
Well Pad ID:
Farm/Lease Name: SMITH BERNARD
License Status: Final Restoration
License Date: 2006-11-21
Spud Date: 2006-11-21
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 2007-04-04
Well Total Depth: 1930.00 ft
Configuration: Vertical
Latitude: 39.740000
Longitude: -81.230000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2006-11-21 Proposed Formations:GORDON, Issued Date:11/21/2006, Expired Date:11/21/2007 6:00:00 AM, Drilling unit acres:60, Proposed Well Type:OG, Proposed Well Class:POOL
Completed 2007-04-04

-4-07. PLUG REPORT INDICATES THAT 7" CASING COLLAPSED, AND WELL WAS PLUGGED AFTER 2 WEEKS OF UNSUCCESSFULLY ATTEMPTING TO OPEN UP THE CASING.

Plugged/Abandoned 2007-04-04

-4-07. PLUG REPORT INDICATES THAT 7" CASING COLLAPSED, AND WELL WAS PLUGGED AFTER 2 WEEKS OF UNSUCCESSFULLY ATTEMPTING TO OPEN UP THE CASING.

Reached Total Depth 2007-04-04

-4-07. PLUG REPORT INDICATES THAT 7" CASING COLLAPSED, AND WELL WAS PLUGGED AFTER 2 WEEKS OF UNSUCCESSFULLY ATTEMPTING TO OPEN UP THE CASING.

Completion Report Received 2007-05-21

-4-07. PLUG REPORT INDICATES THAT 7" CASING COLLAPSED, AND WELL WAS PLUGGED AFTER 2 WEEKS OF UNSUCCESSFULLY ATTEMPTING TO OPEN UP THE CASING.

Construction Permit Expires 2007-11-21

-4-07. PLUG REPORT INDICATES THAT 7" CASING COLLAPSED, AND WELL WAS PLUGGED AFTER 2 WEEKS OF UNSUCCESSFULLY ATTEMPTING TO OPEN UP THE CASING.

Record Last Modified 2015-09-24

-4-07. PLUG REPORT INDICATES THAT 7" CASING COLLAPSED, AND WELL WAS PLUGGED AFTER 2 WEEKS OF UNSUCCESSFULLY ATTEMPTING TO OPEN UP THE CASING.

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 0 0 LOST HOLE @ 1930 AND PLUGGED WELL W/ 30 TONS OF PREPARED CLAY FROM 1020' TO SURFACE… GM

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0600744567 2007-08-08 Final Restoration No Violations Final restoration work at site satisfactory, well was drilled and lost due too casing failure was plugged solid from 1020-0 on 4/4/07.
1186839566 2007-08-08 Preliminary Restoration No Violations Restoration work at site satisfactory.
600744567 2007-8-8 0:00:0 FR No Violations

For data sources see[4]

References