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Well ID: 34-067-20292 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Nottingham Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: WALLACE MAX | |
License Status: Producing | |
License Date: 1974-07-08 | |
Spud Date: 1974-08-16 | |
Spud Drilling Contractor: | |
Final Drill Date: 1974-08-26 | |
Well Total Depth: 6440.00 ft | |
Configuration: Vertical | |
Latitude: 40.290000 | |
Longitude: -81.150000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1974-07-08 | 602 CARTER RESOURCES GeoDate 7/8/74 |
Original Spud | 1974-08-16 | |
Completed | 1974-08-26 | |
Reached Total Depth | 1974-08-26 | |
CO | 1991-09-17 | 4083 MIDCOAST RESOURCES CO GeoDate 7/8/74 |
CO | 1993-07-29 | 213 LOMAK OPERATING CO GeoDate 7/8/74 |
Change of Owner | 2000-06-27 | Operator changed from 213, RANGE OPERATING COMPANY to 6674, GREAT LAKES ENERGY PTNSHP LLC |
Change of Owner | 2010-04-08 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2019-06-04 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 6232 | 6332 | 2 |
6232 | 6332 | 2 | |
6232 | 6332 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 91860 Gal | 50000 | R.P. SR. |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CARTER RESOURCES | 9650.00 | 83.00 | 0 |
1985 | CARTER RESOURCES | 11161.00 | 0.00 | 365 |
1986 | CARTER RESOURCES | 10781.00 | 0.00 | 365 |
1987 | CARTER RESOURCES | 9175.00 | 76.00 | 365 |
1988 | CARTER RESOURCES | 899.00 | 0.00 | 365 |
1991 | MIDCOAST RESOURCES CO | 7011.00 | 0.00 | 365 |
1992 | MIDCOAST RESOURCES CO | 4839.00 | 0.00 | 365 |
1993 | RANGE OPERATING COMPANY | 2299.00 | 96.00 | 153 |
1994 | RANGE OPERATING COMPANY | 5233.00 | 0.00 | 365 |
1995 | RANGE OPERATING COMPANY | 4446.00 | 0.00 | 365 |
1996 | RANGE OPERATING COMPANY | 4507.00 | 0.00 | 365 |
1997 | RANGE OPERATING COMPANY | 4147.00 | 0.00 | 365 |
1998 | RANGE OPERATING COMPANY | 4555.00 | 0.00 | 365 |
1999 | RANGE RESOURCES-APPALACHIA LLC | 1427.00 | 0.00 | 92 |
2000 | RANGE RESOURCES-APPALACHIA LLC | 4589.00 | 0.00 | 365 |
2001 | RANGE RESOURCES-APPALACHIA LLC | 3805.00 | 58.00 | 365 |
2002 | RANGE RESOURCES-APPALACHIA LLC | 3930.00 | 0.00 | 365 |
2003 | RANGE RESOURCES-APPALACHIA LLC | 4783.00 | 0.00 | 365 |
2004 | RANGE RESOURCES-APPALACHIA LLC | 3653.00 | 0.00 | 365 |
2005 | RANGE RESOURCES-APPALACHIA LLC | 2747.00 | 0.00 | 365 |
2006 | RANGE RESOURCES-APPALACHIA LLC | 2970.00 | 0.00 | 365 |
2007 | RANGE RESOURCES-APPALACHIA LLC | 3691.00 | 0.00 | 365 |
2008 | RANGE RESOURCES-APPALACHIA LLC | 3499.00 | 0.00 | 365 |
2009 | RANGE RESOURCES-APPALACHIA LLC | 3830.00 | 0.00 | 365 |
2010 | ENERVEST OPERATING LLC | 3283.00 | 0.00 | 365 |
2011 | ENERVEST OPERATING LLC | 2149.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 2078.00 | 0.00 | 366 |
2013 | ENERVEST OPERATING LLC | 1417.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 231.00 | 0.00 | 365 |
2015 | ENERVEST OPERATING LLC | 48.00 | 0.00 | 365 |
2016 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 366 |
2017 | ENERVEST OPERATING LLC | 140.00 | 0.00 | 365 |
2018 | ENERVEST OPERATING LLC | 186.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1471986728 | 2018-6-11 0:00: | PW | No Violations | 1.00 |
-1712543289 | 2017-8-14 0:00: | PW | No Violations | 1.00 |
-213802061 | 2020-1-10 0:00: | PW | No Violations | 1.00 |
-583990439 | 2016-6-1 0:00:0 | PW | No Violations | 1.00 |
-793772178 | 2016-5-3 0:00:0 | PW | No Violations | 1.00 |
0494757701 | 2016-10-24 | Production Wells | No Violations | On the day of my inspection I witnessed the well head is still leaking gas. Call Bill Barnes (An Enervest Production Supervisor) and stated to him he needs to get the well-fixed as soon as possible. |
0583990439 | 2016-06-01 | Production Wells | No Violations | On the day of my inspection I witnessed no changes have occurred since my last inspection.The well still has a gas leak occuring by the production casing valve. |
0793772178 | 2016-05-03 | Production Wells | No Violations | On the day of my inspection, I witnessed this is a plunger- lift system well, using 2 inch diameter production tubing placed inside 4.5 inch diameter production casing. The plunger is being operated by a motor valve. Production equipment for this well includes 2 100 bbl. production tanks, a horizontal separator and a 2 inch diameter meter run; all placed inside an earth dike that measures approximately 40*50 feet at an average height of 2 foot. An order of gas was noticed coming from the well head during my inspection. I will be back accompanied by an inspector to make insure the gas coming from the well is not an H2S issue. |
1312988144 | 2016-05-04 | Production Wells | No Violations | |
1471986728 | 2018-06-11 | Production Wells | No Violations | On the day of my inspection I witnessed that the leak on this well has not been fixed. It is leaking from the 8.625 inch diameter casing. Tim McCanahey of Enervest said he needs to get a service rig out there and it will be several weeks. Well appears to be producing house gas today. Casing valve open toward domestic meter and valve on to gasline from the meter is also open. |
1712543289 | 2017-08-14 | Production Wells | No Violations | On the day of my inspection I found this plunger lift well equipped with 4.5 inch diameter casing and 2.375 inch diameter tubing. Gas is leaking from around the 4.5 inch diameter wellhead. Domestic gas hook up off of 4.5 inch wellhead. Production equipment includes two 100 barrel steel tanks, horizontal seperator, and meter box with an old chart, all in an earthen dike. No identification on well or tank. RBDMS shows well has not produced since 2015. Previous inspection reports from Joe Zollars indicates that he told the operator to fix the well starting in May of 2016. It is still leaking gas. |
1770550347 | 2016-09-19 | Production Wells | No Violations | |
1952257465 | 2018-01-10 | Production Wells | No Violations | On the day of my inspection I witnessed that the leak on this well has not been fixed. Called Tim McCaunahey of Enervest and he stated he will look into getting someone out here to repair it. Well appears to be producing house gas today. Casing valve open toward domestic meter and valve on to gasline from the meter is also open. There are barrels covering the meter so I cannot see it. |
2061889577 | 2020-1-6 0:00:0 | PW | No Violations | 1.00 |
494757701 | 2016-10-24 0:00 | PW | No Violations | 1.50 |
For data sources see[9]