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Well ID: 34-005-22184 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Perry Township | |
Operator Name: DEEP RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: BLAND R D | |
License Status: Active Injection | |
License Date: 1983-06-10 | |
Spud Date: 1983-08-12 | |
Spud Drilling Contractor: M&G OIL CO. | |
Final Drill Date: 1983-08-25 | |
Well Total Depth: 663.00 ft | |
Configuration: Vertical | |
Latitude: 40.880000 | |
Longitude: -82.150000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Enhanced Recovery | 1983-06-10 | Issued Date 6/10/83 Expired Date 12/7/83 Acres 0080000 Tool Type CT Proposed Formation BEREA Proposed Depth 00663 Proposed Drill Depth 00663 |
Original Spud | 1983-08-12 | CONVERT 6-11-83 |
Completed | 1983-08-25 | CONVERT 6-11-83 |
Reached Total Depth | 1983-08-25 | CONVERT 6-11-83 |
Construction Permit Expires | 1983-12-07 | CONVERT 6-11-83 |
CO | 1984-01-12 | 133 QUAKER STATE OIL REF CORP GeoDate 6/10/83 |
First Injection | 1984-01-12 | CONVERT 6-11-83 |
Completion Report Received | 1984-02-24 | CONVERT 6-11-83 |
Annulus Pressure Monitoring Approved | 1994-11-18 | CONVERT 6-11-83 |
CO | 1995-10-18 | 182 BELDEN & BLAKE CO GeoDate 6/10/83 |
Change of Owner | 2002-02-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER |
Change of Owner | 2008-04-24 | Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC |
Last Compliance Report | 2009-03-13 | CONVERT 6-11-83 |
Record Last Modified | 2017-02-15 | CONVERT 6-11-83 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-05-23 | 576 | 634 | 0 |
2000-05-23 | 580 | 630 | 0 |
576 | 634 | 0 | |
580 | 630 | 0 | |
576 | 634 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 110 Qts | 0 | FOR PRODUCTION | ||
NITR | 0 | 50 Qts | 0 | FOR ERP |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | DEEP RESOURCES LLC | 0.00 | 180.00 | 365 |
2009 | DEEP RESOURCES LLC | 0.00 | 151.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | DEEP RESOURCES LLC | Brine | 0 | 365 |
2009 | DEEP RESOURCES LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1050938084 | 2011-11-17 0:00 | ER | No Violations | |
-1067649632 | 2011-7-12 0:00: | ER | No Violations | |
-1077985550 | 2004-4-22 0:00: | ER | No Violations | |
-1086629621 | 2010-3-30 0:00: | ER | No Violations | 0.50 |
-1119895437 | 2007-5-31 0:00: | ER | No Violations | 0.50 |
-1134135772 | 2019-7-2 0:00:0 | ER | No Violations | |
-1226506260 | 2019-1-10 0:00: | ER | No Violations | |
-1228915754 | 2020-4-10 0:00: | ER | No Violations | |
-1285044654 | 2017-1-6 0:00:0 | ER | No Violations | |
-136198518 | 2008-2-20 0:00: | ER | No Violations | 0.50 |
-1471689629 | 2012-2-27 0:00: | ER | No Violations | |
-175877468 | 2016-4-19 0:00: | ER | No Violations | |
-1802992674 | 2014-5-6 0:00:0 | ER | No Violations | |
-1918178391 | 2015-5-20 0:00: | ER | No Violations | |
-1976967508 | 2016-1-6 0:00:0 | ER | No Violations | |
-2002350871 | 2016-7-6 0:00:0 | ER | No Violations | |
-2017921102 | 2014-10-29 0:00 | ER | No Violations | |
-2047388950 | 2020-2-24 0:00: | ER | No Violations | |
-2130008163 | 2018-4-19 0:00: | ER | No Violations | |
-338107849 | 2009-4-23 0:00: | ER | No Violations | 1.00 |
-354885517 | 2012-9-11 0:00: | ER | No Violations | |
-574079887 | 2004-11-18 0:00 | ER | No Violations | |
-679756636 | 2009-10-20 0:00 | ER | No Violations | 0.50 |
-744305707 | 2007-10-26 0:00 | ER | No Violations | 0.50 |
-84721502 | 2014-3-17 0:00: | ER | No Violations | |
-946002843 | 2017-7-19 0:00: | ER | No Violations | |
-970448579 | 2019-4-18 0:00: | ER | No Violations | |
-983383773 | 2013-12-4 0:00: | ER | No Violations | |
0052396312 | 2007-10-30 | Enhanced Recovery Project | No Violations | Pumped annular side to 230psi and pressure dropped 5 psi in 15 minutes. NOV in compliance. |
0084721502 | 2014-03-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0136198518 | 2008-02-20 | Enhanced Recovery Project | No Violations | Annulus and injection pressure test. |
0175877468 | 2016-04-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0329149435 | 2018-01-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0338107849 | 2009-04-23 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0354885517 | 2012-09-11 | Enhanced Recovery Project | No Violations | Inspect Well. Injection valve stripped. |
0357718328 | 2012-11-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Injection valve is bad. |
0415124570 | 2013-03-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Injector valve failed during inspection and blew out. New valve installed. |
0574079887 | 2004-11-18 | Enhanced Recovery Project | No Violations | Injection pressure test. |
0645196895 | 2014-07-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0679756636 | 2009-10-20 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0744305707 | 2007-10-26 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. 0 psi on annular side. |
0820470749 | 2017-04-13 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0946002843 | 2017-07-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0955105361 | 2016-10-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The annulus test valve is in poor condition. |
0959722586 | 2009-02-26 | Enhanced Recovery Project | No Violations | Pulled tubing and packer and replaced packer with a Butler Larkin compression packer. After several tests pressure remains equilized. Shut injection pressure down until well tests. |
0983266799 | 2012-05-30 | Enhanced Recovery Project | No Violations | Inspect Well. |
0983383773 | 2013-12-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Pump shut down during inspection. |
1000210287 | 2017-11-14 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1046605082 | 2008-12-02 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. Pressures are equal. |
1050938084 | 2011-11-17 | Enhanced Recovery Project | No Violations | Inspect well. |
1067649632 | 2011-07-12 | Enhanced Recovery Project | No Violations | Inspect well. |
1070301798 | 2015-05-15 | Enhanced Recovery Project | No Violations | The well is an injection well in the waterflood enhanced recovery project. ID posted. The well is in use. |
1077985550 | 2004-04-22 | Enhanced Recovery Project | No Violations | Injection pressure test. |
1081466762 | 2009-01-27 | Enhanced Recovery Project | No Violations | Rig over well setting packer. Fluid will flow thru annulus. Shut in annulus. |
1086629621 | 2010-03-30 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1110743117 | 2005-11-29 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1119895437 | 2007-05-31 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1144333868 | 2006-04-06 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. Constructed with 2 tubing cemented at Berea cap. 1 tubing on a packer used for injection. |
1183168374 | 2005-04-27 | Enhanced Recovery Project | No Violations | Injection well test. |
1228945328 | 2008-12-10 | Enhanced Recovery Project | No Violations | Pressure dropped and equalizied in 5 minutes. Reset packer at a later date. |
1233596210 | 2009-02-02 | Enhanced Recovery Project | No Violations | Trouble releasing packer. Parted 1 tubing at 3. Packer needs replaced. Advised Len Rex to shut off water flow out of well. |
1234286612 | 2006-12-29 | Enhanced Recovery Project | No Violations | Annulus pressure was at 0 psi. Pressured up on annulus at 200 psi and pressure held for 15 minutes. |
1235483835 | 2009-02-23 | Enhanced Recovery Project | No Violations | Pulling injection tubing and found one joint collapsed at 500. Tripped out to check packer. Packer needs replaced. |
1251484495 | 2016-02-03 | Work Over Reconditioning | No Violations | The well is constructed with 2 3/8 inch tubing at a depth of 568 feet cemented to the surface. The well is open hole to the total depth of 663 feet. The packer was released and the top most five foot long joint was determined to have failed and was replaced. The entire tubing string and packer was not removed from the borehole. Total of 19 joints of 25 foot sections of PVC lined one Inch tubing with one five foot joint were run in the hole on 3/4/2009 with a Butler Larkin packer set in compression. Approximately 300 gallon of fresh water were pumped through the annulus and circulated to the surface throught the tubing prior to setting the packer. The packer was set and the annulus was pressured up to 368 psi. The pressure was monitored for 15 minutes with 5.4% pressure loss. The test was performed a second time pressuring the well up to 420 psi. The pressure was monitored for 15 minutes with a 2.3% loss. This is within the stated margin of 5% pressure loss. The well passes the Mechanical Integrity Test. The well head was reconstructed with new parts and put into production. |
1285044654 | 2017-01-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1395118696 | 2015-03-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Main flow line valves shut off during inspection. |
1443620635 | 2003-08-07 | Enhanced Recovery Project | No Violations | |
1464733866 | 2018-10-02 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1471689629 | 2012-02-27 | Enhanced Recovery Project | No Violations | inspect well. |
1484735193 | 2018-07-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1545831476 | 2018-12-18 | Enhanced Recovery Project | No Violations | Inspect well for pressure and integrity. |
1653647426 | 2020-1-27 0:00: | ER | No Violations | |
1659063752 | 2010-11-26 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1791325337 | 2013-05-22 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Valve for annulus leaks. |
1802992674 | 2014-05-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1813333572 | 2006-12-13 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1918178391 | 2015-05-20 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1976967508 | 2016-01-06 | Enhanced Recovery Project | Violations Noted | Inspect well for integrity and pressure. Well has equalized. Operator conducted pressure test and verified failure. |
2002350871 | 2016-07-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
2017921102 | 2014-10-29 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
2063770954 | 2015-10-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The well head is in poor condition. The operator was notified the flow line shut off valve stem has a slow leak. The operator subsequently replaced fittings. No leaks. |
2114206956 | 2019-11-18 0:00 | ER | No Violations | |
2130008163 | 2018-04-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
329149435 | 2018-1-4 0:00:0 | ER | No Violations | |
357718328 | 2012-11-27 0:00 | ER | No Violations | |
415124570 | 2013-3-4 0:00:0 | ER | No Violations | |
445285454 | 2020-7-8 0:00:0 | ER | No Violations | |
52396312 | 2007-10-30 0:00 | ER | No Violations | 1.00 |
645196895 | 2014-7-17 0:00: | ER | No Violations | |
820470749 | 2017-4-13 0:00: | ER | No Violations | |
955105361 | 2016-10-19 0:00 | ER | No Violations | |
959722586 | 2009-2-26 0:00: | ER | No Violations | 4.00 |
983266799 | 2012-5-30 0:00: | ER | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1046605082 | US-OH-100731 | 2008-11-26 | Failure to conduct or pass mech. integrity test | |
1976967508 | US-OH-119981 | 2016-02-12 | Mechanical failure/contamination |
For data sources see[9]