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Well ID: 34-067-20696 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Franklin Township | |
Operator Name: RHDK OIL & GAS LLC/DBA RED HIL | |
Well Pad ID: | |
Farm/Lease Name: BIRNEY MARV | |
License Status: Producing | |
License Date: 1984-12-11 | |
Spud Date: 1984-12-18 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1985-01-04 | |
Well Total Depth: 6221.00 ft | |
Configuration: Vertical | |
Latitude: 40.310000 | |
Longitude: -81.200000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1984-12-11 | Issued Date 12/11/84 Expired Date 6/9/85 Acres 0067150 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06221 Proposed Drill Depth 06221 |
Original Spud | 1984-12-18 | PERMIT EXPIRED. |
Completed | 1985-01-04 | PERMIT EXPIRED. |
Reached Total Depth | 1985-01-04 | PERMIT EXPIRED. |
CO | 1985-05-08 | 168 RED HILL DEVELOPMENT GeoDate 12/11/84 |
Construction Permit Expires | 1985-06-09 | PERMIT EXPIRED. |
Completion Report Received | 1987-06-24 | PERMIT EXPIRED. |
Record Last Modified | 2017-02-15 | PERMIT EXPIRED. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 6056 | 6119 | 9 |
6056 | 6119 | 9 | |
6056 | 6119 | 9 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 79800 Gal | 0 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1402392473 | 2017-10-3 0:00: | PW | No Violations | 1.00 |
-1827924020 | 2019-8-26 0:00: | PW | No Violations | 0.50 |
-942147704 | 2014-3-25 0:00: | PW | No Violations | 1.00 |
0942147704 | 2014-03-25 | Production Wells | No Violations | Check on 2 inch valve which was leaking on last inspection and found that it is not leaking at this inspection. I did notice H2S near the well head and there may be another leak. I tried to check with my meter to make sure it was H2S and it went on alarm with the O2 sensor and malfunctioned again. |
1333765885 | 2006-04-13 | Production Wells | No Violations | Routine inspection revealed no violations at this time . The tank battery consists of one 100 bbl fiberglass oil storage tank and the SPCC dike meets requirements . There is a slight H2S gas odor at the wellhead at this time . |
1400087599 | 2014-05-05 | Production Wells | No Violations | RHD has its service rig over the well today to repair the leaks in the casing coming from the Newburg and containing some amout of H2S. They have a log truck on site today to perf the 4-1/2 inch diameter casing string at 4400 ft and then circulate cement to surface as part of the repair. |
1402392473 | 2017-10-03 | Production Wells | No Violations | On the day of my inspection I found this plunger lift well equipped with 4.5 inch diameter casing, 2.375 inch diameter tubing, and a motor valve. Production equipment includes a horizontal seperator, meter box with .75 inch diameter sales line orfice, domestic gas meter, and a 140 barrel steel tank, all contained in an earthen dike. Production records are current and chart indicates well is producing. Tank is labeled. |
1445879260 | 2015-01-08 | Production Wells | No Violations | The repairs to the well have been made and there are no leaks at or around the well during this inspection. The well had been leaking H2S gas . The annulus from the Newburg to surface has been cemented and there is no H2S leaking at this time. |
1501134311 | 2014-07-09 | Production Wells | No Violations | This well has been cemented from the Newburg to surface to repair a casing problem caused by H2S gas. The repairs have been completed but today I found a leak on the casing head bowl which appears to be a crack. I contacted Chris Kimble and advised. |
1770199647 | 2014-03-18 | Production Wells | No Violations | I am on site today to check wells in the area near a water well complaint. The well has proper identification and all of the equipment is in place to produce the well. |
For data sources see[9]