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Well ID: 34-151-23315 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: MORELLI | |
License Status: Producing | |
License Date: 1980-11-25 | |
Spud Date: 1980-12-05 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-12-09 | |
Well Total Depth: 4461.00 ft | |
Configuration: Vertical | |
Latitude: 40.810000 | |
Longitude: -81.500000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-11-25 | 139 MB OPERATING CO INC GeoDate 11/25/80 |
Oil and Gas | 1980-11-25 | Issued Date 11/25/80 Expired Date Acres 0071600 Tool Type RTA Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1980-12-05 | R.L. 11/21/80 |
Completed | 1980-12-09 | R.L. 11/21/80 |
Reached Total Depth | 1980-12-09 | R.L. 11/21/80 |
Completion Report Received | 1981-01-20 | R.L. 11/21/80 |
Change of Owner | 2000-06-30 | Operator changed from 139, MB OPERATING CO INC to 6674, GREAT LAKES ENERGY PTNSHP LLC |
Change of Owner | 2010-08-25 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2019-06-14 | R.L. 11/21/80 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4270 | 4340 | 19 |
4270 | 4340 | 19 | |
4270 | 4340 | 19 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 4628 Bbl | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | MB OPERATING CO INC | 12475.00 | 204.00 | 0 |
1985 | MB OPERATING CO INC | 13837.00 | 195.00 | 365 |
1986 | MB OPERATING CO INC | 9144.00 | 71.00 | 365 |
1987 | MB OPERATING CO INC | 4285.00 | 0.00 | 365 |
1988 | MB OPERATING CO INC | 3181.00 | 66.00 | 366 |
1989 | MB OPERATING CO INC | 2706.00 | 0.00 | 365 |
1990 | MB OPERATING CO INC | 1758.00 | 85.00 | 365 |
1991 | MB OPERATING CO INC | 3127.00 | 0.00 | 365 |
1992 | MB OPERATING CO INC | 9762.00 | 172.00 | 366 |
1993 | MB OPERATING CO INC | 18717.00 | 100.00 | 365 |
1994 | MB OPERATING CO INC | 19753.00 | 198.00 | 365 |
1995 | MB OPERATING CO INC | 20844.00 | 83.00 | 365 |
1996 | MB OPERATING CO INC | 19282.00 | 70.00 | 366 |
1999 | MB OPERATING CO INC | 12029.00 | 93.00 | 273 |
2000 | RANGE RESOURCES-APPALACHIA LLC | 13871.00 | 74.00 | 335 |
2001 | RANGE RESOURCES-APPALACHIA LLC | 12535.00 | 0.00 | 365 |
2002 | RANGE RESOURCES-APPALACHIA LLC | 10853.00 | 62.00 | 365 |
2003 | RANGE RESOURCES-APPALACHIA LLC | 11879.00 | 47.00 | 365 |
2004 | RANGE RESOURCES-APPALACHIA LLC | 13929.00 | 84.00 | 365 |
2005 | RANGE RESOURCES-APPALACHIA LLC | 12460.00 | 73.00 | 365 |
2006 | RANGE RESOURCES-APPALACHIA LLC | 10597.00 | 20.00 | 365 |
2007 | RANGE RESOURCES-APPALACHIA LLC | 6309.00 | 59.00 | 365 |
2008 | RANGE RESOURCES-APPALACHIA LLC | 8461.00 | 60.00 | 365 |
2009 | RANGE RESOURCES-APPALACHIA LLC | 9819.00 | 77.00 | 365 |
2010 | ENERVEST OPERATING LLC | 10091.00 | 95.00 | 365 |
2011 | ENERVEST OPERATING LLC | 10559.00 | 41.00 | 0 |
2012 | ENERVEST OPERATING LLC | 9752.00 | 53.00 | 366 |
2013 | ENERVEST OPERATING LLC | 8353.00 | 23.00 | 365 |
2014 | ENERVEST OPERATING LLC | 7140.00 | 63.00 | 365 |
2015 | ENERVEST OPERATING LLC | 7724.00 | 21.00 | 365 |
2016 | ENERVEST OPERATING LLC | 7460.00 | 14.00 | 366 |
2017 | ENERVEST OPERATING LLC | 5234.00 | 37.00 | 365 |
2018 | ENERVEST OPERATING LLC | 6401.00 | 16.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1532816408 | 2017-9-8 0:00:0 | PW | No Violations | 1.50 |
-2086641497 | 2003-11-7 0:00: | PW | No Violations | |
0212787791 | 2017-09-25 | Production Wells | No Violations | I did a complaint follow-up inspection for complaint #5699. The service rig is off location. There is no odor of gas or hissing sounds coming from the repaired well. I met with Bob Everly (Enervest pumper) he advised me the tubing may need to be swab again. With that, I contacted the Mr. Chalsfant (complainant) and advised him field findings and told him I would recommend closing the complaint. Mr. Chalsfant concurred with the closing of complaint #5699. |
1119370851 | 2005-06-20 | Production Wells | No Violations | NO VIOLATIONS. |
1505913170 | 2017-09-19 | Production Wells | No Violations | I did a follow-up complaint inspection for complaint# 5699. Bishop Well Service is on location making repairs to the well. I met with Bob Whaley (Enervest) he advised me the repairs and the rig should be off location by Friday 09-22-17. I called and spoke with Mr. Chalsfant (Landowner). I updated the complaint log. |
1532816408 | 2017-09-08 | Production Wells | No Violations | I did a complaint inspection on this well for complaint # 5699. The complaint was received on 9-8-17. The complainant said there hissing sound coming from the well and an odor of gas. I contacted the complainant and advised him I had contacted Robert Whaley (Enervest Foreman) and he was sending the pumper to the location. I met with Robert Whaley on location. The well is equipped with a plunger-lift system. The wells hissing was barely audible at the time of my inspection and it was coming from production wellhead where the casing meets the wellhead. There is an occasional slight odor of gas. The casing at the wellhead has atmospheric corrosion. The landowner Mrs. Chalsfant arrived on location and Bob Whaley explained to her the well will need to be serviced. He explained to her what would be done and that a service rig would be used. Bob Whaley advised it should be approximately 2-3 weeks before the well is serviced. The complaint will remain open until the well has been repaired. |
2086641497 | 2003-11-07 | Production Wells | No Violations | NO VIOLATIONS. GPS WH and 1-210 bbl. |
212787791 | 2017-9-25 0:00: | PW | No Violations |
For data sources see[9]