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Well ID: 34-111-24745 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Switzerland Township | |
Operator Name: CNX GAS COMPANY LLC | |
Well Pad ID: US-OH-001469 | |
Farm/Lease Name: ROBERTS VICTOR L & LINDA G | |
License Status: Producing | |
License Date: 2017-05-05 | |
Spud Date: 2017-05-24 | |
Spud Drilling Contractor: PATTERSON DRILLING | |
Final Drill Date: 2017-07-20 | |
Well Total Depth: 21855.00 ft | |
Configuration: Horizontal | |
Latitude: 39.840000 | |
Longitude: -80.910000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2017-05-05 | Proposed Formations:POINT PLEASANT, Issued Date:5/5/2017, Expired Date:5/5/2019 12:00:00 PM, Drilling unit acres:1017.33, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2017-07-20 | |
Completion Report Received | 2018-03-27 | |
Correction to Well | 2018-03-30 | UPDATE TAKE PER AS-DRILLED PLAT |
Record Last Modified | 2018-04-03 | |
Construction Permit Expires | 2019-05-05 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2018-04-02 | 10900 | 11048 | 0 |
2018-04-02 | 21610 | 21752 | 0 |
21610 | 21752 | 0 | |
10900 | 11048 | 0 | |
10900 | 11048 | 0 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 11/16/2017 | 12/31/2017 | 10477 | 33,147,200.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Calbreak 5501 | CWS | Breaker | Listed Below Green Line | Listed Below | 0 | 0 | 0 |
DAP-103 | CWS | Iron Control | Listed Below Green Line | Listed Below | 0 | 0 | 0 | |
Hydrochloric Acid | CWS | Clean Perforations | Listed Below Green Line | Listed Below | 0 | 0 | 0 | |
Sand (Proppant) | CWS | Propping Agent | Listed Below Green Line | Listed Below | 0 | 0 | 0 | |
SANIFRAC 8844 | CWS | Biocide | Listed Below Green Line | Listed Below | 0 | 0 | 0 | |
CI-9100G | CWS | Corrosion Inhibitor | Listed Below Green Line | Listed Below | 0 | 0 | 0 | |
Water | Supplied by Operator | Base Fluid | Water | 7732-18-5 | 70 | 89.5628 | 0 | |
DWP-641 | CWS | Friction Reducer | Listed Below Green Line | Listed Below | 0 | 0 | 0 | |
Acetic acid, ammonium salt (1:1) | 631-61-8 | 10 | 0.00619 | 19115.8 | ||||
Apatite | 64476-38-6 | 0.1 | 0.00998 | 30793.5 | ||||
Vinylidene chloride-methyl acrylate copolymer | 69418-26-4 | 20 | 0.00129 | 3969.84 | ||||
Alcohols, C12-16, ethoxylated | 68551-12-2 | 3.6 | 0.00223 | 6881.67 | ||||
Ammonium chloride | 12125-02-9 | 11 | 0.00277 | 8562.12 | ||||
Ethylene glycol | 107-21-1 | 40 | 0.0001 | 305.96 | ||||
Guar gum | 9000-30-0 | 60 | 0.02339 | 72198.7 | ||||
Biotite | 1302-27-8 | 0.1 | 0.00998 | 30793.5 | ||||
Cinnamaldehyde | 104-55-2 | 10 | 0.00002000 | 76.49 | ||||
Oxirane, 2-methyl-, polymer with oxirane, monodecyl ether | 37251-67-5 | 1.5 | 0.00058 | 1804.97 | ||||
Polyethylene glycol monooleate | 9004-96-0 | 3 | 0.00076 | 2335.12 | ||||
Acrylamide | 79-06-1 | 0.1 | 0.00003000 | 77.84 | ||||
Sorbitol tetraoleate | 61723-83-9 | 2 | 0.0005 | 1556.75 | ||||
Ilmenite | 98072-94-7 | 0.1 | 0.00445 | 13726.3 | ||||
Ethoxylated alcohols | Proprietary | 10 | 0.00002000 | 76.49 | ||||
2,2-Dibromo-3-Nitrilopropionamide | 10222-01-2 | 20 | 0.0059 | 18205.9 | ||||
Tar bases, quinolone derivs, benzyl chloride-quatenized | 72480-70-7 | 10 | 0.00002000 | 76.49 | ||||
1,2-Propanediol | 57-55-6 | 10 | 0.00215 | 6629.3 | ||||
Alcohols, C10-16, ethoxylated | 68002-97-1 | 3.6 | 0.00223 | 6881.67 | ||||
Hydrochloric acid | 7647-01-0 | 37 | 0.17835 | 550492 | ||||
Amines, tallow alkyl, ethoxylated | 61791-26-2 | 1 | 0.00025 | 778.37 | ||||
Distillates (petroleum), hydrotreated light | 64742-47-8 | 30 | 0.02305 | 71140.6 | ||||
Isopropanol | 67-63-0 | 30 | 0.00002000 | 67.52 | ||||
Alkyloxypolyethyleneoxyethanol | 84133-50-6 | 0.5 | 0.00013 | 389.19 | ||||
Dibromoacetonitrile | 3252-43-5 | 3 | 0.00088 | 2730.88 | ||||
Amines, coco alkyl dimethyl | 61788-93-0 | 5 | 0.00001000 | 4.88 | ||||
Diethylene glycol (mono) methyl ether | 34590-94-8 | 20 | 0.00005000 | 152.98 | ||||
Alcohols, C12-14, ethoxylated | 68439-50-9 | 3.6 | 0.00223 | 6881.67 | ||||
Diethylene glycol | 111-46-6 | 1 | 0.00001000 | 7.65 | ||||
Citric acid | 77-92-9 | 60 | 0.00161 | 4983.98 | ||||
Sodium bromide | 7647-15-6 | 4 | 0.00118 | 3641.18 | ||||
Illite | 12173-60-3 | 1 | 0.04447 | 137263 | ||||
2-Propenoic acid, homopolymer, sodium salt | 9003-04-7 | 40 | 0.00859 | 26517.2 | ||||
Substituted ammonium chloride | Proprietary | 5 | 0.00001000 | 4.88 | ||||
Distillates (petroleum), hydrotreated middle | 64742-46-7 | 60 | 0.02339 | 72198.7 | ||||
Polyethylene glycol mixture | 25322-68-3 | 54.5 | 0.01607 | 49611 | ||||
Calcite | 471-34-1 | 1 | 0.05529 | 170672 | ||||
Crystalline silica (Quartz) | 14808-60-7 | 100 | 9.97832 | 30,799,500.0 | ||||
Polymer | 26100-47-0 | 45 | 0.01135 | 35026.9 | ||||
Ammonium Persulfate | 64742-47-8 | 100 | 0.00643 | 19849.2 | ||||
Dimethylcocoamine, bis(chloroethyl)
ether, diquaternary ammonium salt |
68607-28-3 | 20 | 0.00001000 | 19.52 | ||||
Formic Acid | 64-18-6 | 10 | 0.00002000 | 76.49 | ||||
Methanol | 67-56-1 | 10 | 0.00001000 | 9.76 | ||||
Quaternary ammonium compounds,
bis(hydrogenated tallow alkyl)dimethyl, salts with bentonite |
68953-58-2 | 5 | 0.00195 | 6016.56 | ||||
Tar bases, quinolone derivs | 68513-87-1 | 1 | 0.00001000 | 7.65 | ||||
Sorbitan monooleate | 1338-43-8 | 4 | 0.00101 | 3113.5 | ||||
Goethite | 1310-14-1 | 0.1 | 0.00998 | 30793.5 | ||||
DWP-NE1 | CWS | Non-Emulsifier | Listed Below Green Line | Listed Below | 0 | 0 | 0 | |
Silver FR 350 | Silverback Chemical | Friction Reducer | Listed Below Green Line | Listed Below | 0 | 0 | 0 | |
Other Chemical(s) | Listed Above | See Trade Name(s) List | Listed Below | |||||
DWP-111 | CWS | Gel Slurry | Listed Below Green Line | Listed Below | 0 | 0 | 0 | |
DAP-902 | CWS | Scale Inhibitor | Listed Below Green Line | Listed Below | 0 | 0 | 0 |
For data sources see[4]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2017-11-16 | H2O | 15 | 16823 Bbl | 700100 | CalFrac | STAGE 1 OF 56 |
2017-12-31 | H2O | 15 | 11436 Bbl | 704320 | CalFrac | STAGE 56 OF 56 SEE IMAGES FOR STAGES 2-55 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | CNX GAS COMPANY LLC | 5354039 | 0 | 331 |
2019 | CNX GAS COMPANY LLC | 886815 | 0 | 88 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | CNX GAS COMPANY LLC | Brine | 122335 | 331 |
2019 | CNX GAS COMPANY LLC | Brine | 15031 | 88 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-668999842 | 2019-1-22 0:00: | PL | No Violations | 0.20 |
0668999842 | 2019-01-22 | Preliminary Restoration | No Violations | On this day, I am conducting a preliminary restoration inspection. Site meets 1509.072 (A) Vegetation is established with no substantial erosion. I found the pad gated with signage at the entrance. There are (3) producing wells, (3) gas processing units (GPU), (3) 400-barrel and (1) 50-barrel steel production tanks within polymer lined steel containment, and an Emergency Shutdown (ESD) button is present at the pad entrance. Additionally, concrete barriers surround the perimeter of the wellheads and the GPUs. Each well has identification and annular pressure monitoring devices equipped. The 9.625 inch diameter intermediate casing has a pressure of 950 pounds per square inch (psi), and the 13.375 inch diameter surface casing has a pressure of 0 psi. |
1495738224 | 2017-05-25 | Casing String Witnessed | No Violations | On site inspection to witness the conductor casing cement job with Express Energys top hole rig and cement service. The auger rig has drilled a 36 diameter borehole to a measured depth of 100 and inserted 100 of 30 diameter .375 wall 118 pound per foot conductor. Express then cemented the casing with a 48.9 barrel cement mix consisting of 275 sacks of class A cement with the cement weight verified by weight of scale at 15.6 pounds per gallon. Cement returns were witnessed to surface inside the cellar at 50 barrels into a total of 75 barrels of fresh water dissplaceent.1 of cement was left in the cellar causing a liquid tight seal. No fresh water was encountered in the borehole while drilling. |
1499096847 | 2017-06-30 | Casing String Witnessed | No Violations | During my inspection I witnessed Patterson Drilling Rig 803 land the 18.625 inch diameter casing at a depth of 651 feet within a 24 inch diameter hole. BJ services arrived on location to cement the casing string in two stages with a packer set at a depth of 399 feet. A coal seam was encountered during the drilling process from 596 feet to 604 feet. Cement calculations were discussed with the CNX company man. BJ services rigged up and held a pre-job safety meeting with all personnel on location. I was unable to be present for the total duration of the job. |
1576112886 | 2018-01-18 | Completion Testing | No Violations | Status check inspection on the well completion process found the well has been stimulated in a total of 57 stages. The production well head assembly is installed and Deep Well Service tubing snubbing unit # 9 is on location completing a adjoining well. The well support production equipment is present on location consisting of a gas processing unit and production tank farm. 3 wells are total on location. |
1761021447 | 2020-6-4 0:00:0 | PW | No Violations | 1.00 |
2123698199 | 2018-02-04 | Completion Testing | No Violations | On site inspection found the well drilling and stimulation process is complete. The completion plugs have been drilled out and production tubing hung in the well. TETRA flow back services are on site and rigged up to the said well, they will begin the initial well bore production flow back on this day. |
For data sources see[10]