If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-005-23601 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.88,"lon":-82.15,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Perry Township | |
Operator Name: DEEP RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: SMALLEY ELLEN | |
License Status: Active Injection | |
License Date: 1983-06-07 | |
Spud Date: 1983-06-20 | |
Spud Drilling Contractor: WALTZ BROS DRLG | |
Final Drill Date: 1983-06-22 | |
Well Total Depth: 718.00 ft | |
Configuration: Vertical | |
Latitude: 40.880000 | |
Longitude: -82.150000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Enhanced Recovery | 1983-06-07 | Issued Date 6/7/83 Expired Date 12/4/83 Acres 0081510 Tool Type RTAF Proposed Formation BEREA Proposed Depth 00718 Proposed Drill Depth 00718 |
Original Spud | 1983-06-20 | LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED. |
Completed | 1983-06-22 | LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED. |
Reached Total Depth | 1983-06-22 | LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED. |
CO | 1983-10-07 | 133 QUAKER STATE OIL REF CORP GeoDate 6/7/83 |
First Injection | 1983-10-07 | LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED. |
Completion Report Received | 1983-10-19 | LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED. |
Construction Permit Expires | 1983-12-04 | LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED. |
Annulus Pressure Monitoring Approved | 1994-10-13 | LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED. |
CO | 1995-10-18 | 182 BELDEN & BLAKE CO GeoDate 6/7/83 |
Last Compliance Report | 1999-12-16 | LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED. |
Change of Owner | 2002-02-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER |
Change of Owner | 2008-04-24 | Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC |
Record Last Modified | 2017-02-15 | LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-05-23 | 598 | 662 | 0 |
598 | 662 | 0 | |
598 | 662 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 108 Qts | 0 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1065194201 | 2017-1-9 0:00:0 | ER | No Violations | |
-1108021305 | 2008-2-20 0:00: | ER | No Violations | 0.50 |
-1143315354 | 2018-1-8 0:00:0 | ER | No Violations | |
-1147436128 | 2009-4-23 0:00: | ER | No Violations | 0.50 |
-1280596676 | 2004-4-22 0:00: | ER | No Violations | |
-1329781778 | 2017-7-13 0:00: | ER | No Violations | |
-1410217102 | 2019-7-2 0:00:0 | ER | No Violations | |
-1441805501 | 2005-11-29 0:00 | ER | No Violations | 0.50 |
-1508340346 | 2017-4-13 0:00: | ER | No Violations | |
-1510854277 | 2016-7-8 0:00:0 | ER | No Violations | |
-1551496399 | 2007-10-26 0:00 | ER | No Violations | 0.50 |
-1555793123 | 2015-5-20 0:00: | ER | No Violations | |
-1716055686 | 2014-5-6 0:00:0 | ER | No Violations | |
-1742028763 | 2007-4-3 0:00:0 | ER | No Violations | 0.50 |
-2061390353 | 2011-2-1 0:00:0 | ER | No Violations | 1.00 |
-2099654859 | 2017-11-14 0:00 | ER | No Violations | |
-21267004 | 2011-10-17 0:00 | ER | No Violations | |
-222250617 | 2016-1-5 0:00:0 | ER | No Violations | |
-292204169 | 2006-4-13 0:00: | ER | No Violations | 0.50 |
-299118057 | 2008-11-26 0:00 | ER | No Violations | 0.50 |
-299343543 | 2018-5-1 0:00:0 | ER | No Violations | |
-328860660 | 2013-3-4 0:00:0 | ER | No Violations | |
-419743991 | 2018-10-10 0:00 | ER | No Violations | |
-518762959 | 2016-4-19 0:00: | ER | No Violations | |
-564435075 | 2016-11-2 0:00: | ER | No Violations | |
-671047079 | 2006-12-13 0:00 | ER | No Violations | 0.50 |
-696318318 | 2012-11-27 0:00 | ER | No Violations | |
-758772465 | 2014-10-29 0:00 | ER | No Violations | |
0016498865 | 2018-08-13 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0021267004 | 2011-10-17 | Enhanced Recovery Project | No Violations | Inspect well. |
0222250617 | 2016-01-05 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0292204169 | 2006-04-13 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. Constructed with 2 tubing cemented at Berea cap and 1 tubing on a packer used for injection. |
0299118057 | 2008-11-26 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. Pressures equal. Reset packer and test. |
0299343543 | 2018-05-01 | Enhanced Recovery Project | No Violations | Inspect well with operator to preform monthly pressure test of the annulus on the well. |
0328860660 | 2013-03-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0401873504 | 2003-08-14 | Enhanced Recovery Project | No Violations | |
0419743991 | 2018-10-10 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0456522508 | 2011-07-12 | Enhanced Recovery Project | No Violations | inspect well. |
0518762959 | 2016-04-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0564435075 | 2016-11-02 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0654773820 | 2014-07-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Well head has a slight leak. |
0671047079 | 2006-12-13 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0696318318 | 2012-11-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Injector line has slow leak at nipple. |
0758772465 | 2014-10-29 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0830675422 | 2018-04-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0833564665 | 2004-11-18 | Enhanced Recovery Project | No Violations | Injection pressure test. |
0885235978 | 2011-04-12 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1033430420 | 2013-12-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Pump shut down during inspection. A line leak had occurred near the well head and appears to have plugged itself. Operator will excavate line and make appropriate repairs. |
1065194201 | 2017-01-09 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1108021305 | 2008-02-20 | Enhanced Recovery Project | No Violations | Annulus and injection pressure test. |
1138919076 | 2010-03-30 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1143315354 | 2018-01-08 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1147436128 | 2009-04-23 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1214647425 | 2005-04-27 | Enhanced Recovery Project | No Violations | Injection well test. |
1228250584 | 2008-12-02 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1235914788 | 2012-05-24 | Enhanced Recovery Project | No Violations | Inspect Well. |
1280596676 | 2004-04-22 | Enhanced Recovery Project | No Violations | Injection pressure test. |
1308300743 | 2009-10-20 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1329781778 | 2017-07-13 | Enhanced Recovery Project | Violations Noted | Upon arrival at location the operator located leak with the flexible injection line. The supply trunk line was shut off and a replacement flexible injection flow line was installed at the well head. The operator determined less than 42 gallons of water was released and incident notification was not required. The well was put back into operation. The well was inspected for integrity and pressure. 1501:9-5-06 Prevention of contamination and pollution.
All persons engaged in any phase of enhanced recovery operations shall conduct such operations in a manner which will not contaminate the surface of the land, or water on the surface or in the subsurface. |
1335462194 | 2012-02-27 | Enhanced Recovery Project | No Violations | Inspect Well. |
1409055532 | 2020-7-8 0:00:0 | ER | No Violations | |
1434966692 | 2019-4-11 0:00: | ER | No Violations | |
1441805501 | 2005-11-29 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1455629763 | 2016-02-12 | Work Over Reconditioning | No Violations | In January 19, 2011 a total of 20 joints of PVC lined tubing were installed in the well at a depth of 500 feet with a Larkin packer set in compression. During the October 30, 2015 inspection of the well the tubing was observed to be deteriorated above the well head and the PVC line was visible. In February of 2016 the operator rigged up the service rig on the well and pulled the Larkin packer up-hole, 16 inches, without releasing the packer. The deteriorated tubing was cut off and the remaining tubing was threaded and the well head reconstructed. The packer is set at 498.6 feet. The well was loaded with fresh water and corrosion inhibitor and pressure tested by the operator. At the time the MIT was conducted the annulus pressure was at 305 psi. The operator was requested to pressure up the annulus above 350 psi. The annulus was pressured up to 395 psi and the pressure monitored for a period of 15 minutes with zero loss in pressure. The well passed the Mechanical Integrity test. The operator was notified that the well can be put into production. |
1508340346 | 2017-04-13 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1510854277 | 2016-07-08 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1551496399 | 2007-10-26 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1555793123 | 2015-05-20 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The annulus riser nipple is corroded. |
1610858382 | 2020-4-21 0:00: | ER | No Violations | |
1629990026 | 2010-11-26 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. Pressures are equal at 320 psi. Reset packer and test. |
16498865 | 2018-8-13 0:00: | ER | No Violations | |
1714546829 | 2020-1-23 0:00: | ER | No Violations | |
1716055686 | 2014-05-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1742028763 | 2007-04-03 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1893402429 | 2013-04-15 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Passed test. |
1992859859 | 2012-09-20 | Enhanced Recovery Project | No Violations | Inspect Well. Site ok. |
2044688293 | 2015-03-31 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
2048839956 | 2014-03-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
2061390353 | 2011-02-01 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. Replaced packer. Pumped up annulus at 415 psi. 10 psi decline in 15 minutes. Topped off annulus between 2 3/8 tubing and surface casing with 35 sacks Class A cement.120 - 0, 1-17-2011. |
2072778746 | 2019-1-10 0:00: | ER | No Violations | |
2083189440 | 2015-10-30 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The well head is in poor condition. The operator was notified the tubing has a slow leak. |
2099654859 | 2017-11-14 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
401873504 | 2003-8-14 0:00: | ER | No Violations | |
456522508 | 2011-7-12 0:00: | ER | No Violations | |
654773820 | 2014-7-17 0:00: | ER | No Violations | |
681653235 | 2019-11-18 0:00 | ER | No Violations | |
830675422 | 2018-4-27 0:00: | ER | No Violations | |
833564665 | 2004-11-18 0:00 | ER | No Violations | |
885235978 | 2011-4-12 0:00: | ER | No Violations | 0.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0299118057 | US-OH-123111 | 2008-11-26 | Failure to conduct or pass mech. integrity test | |
1329781778 | US-OH-109434 | 2017-08-18 | 9-5-06 | Pollution/Contamination |
1629990026 | US-OH-116020 | 2010-11-26 | Failure to conduct or pass mech. integrity test |
For data sources see[5]