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34-005-60067

Well Details

Well ID: 34-005-60067
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Country: United States
State: Ohio
County: Ashland
Municipality: Green Township
Operator Name: COLUMBIA GAS TRANSMISSION LLC
Well Pad ID:
Farm/Lease Name: BASH BERNARD F
License Status: Storage Well
License Date: 1964-07-24
Spud Date: 1964-07-27
Spud Drilling Contractor:
Final Drill Date: 1964-08-18
Well Total Depth: 2632.00 ft
Configuration: Vertical
Latitude: 40.690000
Longitude: -82.290000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1964-07-27
Completed 1964-08-18
Reached Total Depth 1964-08-18
Change of Owner 2011-08-03 Operator changed from 9998, HISTORIC OWNER to 22, COLUMBIA GAS TRANSMISSION
Record Last Modified 2013-05-23

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0
2016-09-30 H2O 0 302 Bbl 24000 C&J Energy Services C&J conducted the fracture stimulation for Columbia Gas. The job was a nitrogen assisted fracture stimulation. C&J didn't provide sand total, nitrogen total, treating rate and pressure or 5 minute shut in pressures. The information was received from Columbia Gas. 24,000 pounds of 20/40 sand and 61,000 cubic feet of nitrogen were used in the job. The slurry component was cross linked fresh water guar gel. The well was pre loaded with 250 gallons of 10% acetic acid.

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1385037618 2014-10-7 0:00: SO No Violations 0.50
-1666606524 2016-9-27 0:00: SO No Violations 0.50
-333949061 2013-12-10 0:00 SO No Violations 0.50
-66000698 2015-7-13 0:00: SO No Violations 0.50
-929499978 2019-4-23 0:00: SO No Violations
0066000698 2015-07-13 Storage Well No Violations ID posted. The location is maintained. Valves on the well head are open. The backside valve is open.
0333949061 2013-12-10 Storage Well No Violations ID posted, location maintained. The drip is covered in frozen condensation.
0919037583 2017-05-05 Storage Well No Violations ID is posted and the location is maintained. The gate valve is open; the annulus is shut in. The well is equipped with a separator.
0929499978 2019-04-23 Storage Well No Violations Performed annual inspection for Columbia Gas Storage Well #10521 on 04/23/2019. The well is equipped with a flanged wellhead with 1-master valve and 1-wing valve, and a drip. Well identification is clearly displayed. No problems were noted at the time of the inspection.
1028930649 2016-09-09 Work Over Reconditioning No Violations Baker Hughes is logging the well. The company service rig is on the well.
1174226912 2016-09-14 Work Over Reconditioning No Violations The operator requested inspection to witness production casing cement. See the casing ticket for details.
1385037618 2014-10-07 Storage Well No Violations ID posted, location maintained.
1475500211 2016-09-30 Work Over Reconditioning No Violations The operator requested inspection to witness fracture stimulation of the storage well. See the stimulation report for details.
1538665289 2018-10-04 Storage Well No Violations ID is posted and the location is maintained. The annulus is open. The well is equipped with a separator.
1623664465 2020-1-27 0:00: SO No Violations
1666606524 2016-09-27 Storage Well No Violations The stimulation job scheduled for today was postponed until Friday.
1811689568 2016-08-31 Work Over Reconditioning No Violations The operator requested inspection to witness cementing the surface casing in the well. See the casing ticket for details.
673509759 2019-3-6 0:00:0 SO No Violations
919037583 2017-5-5 0:00:0 SO No Violations 0.50

For data sources see[4]

References