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Well ID: 34-031-24304 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Bethlehem Township | |
Operator Name: BRILEX LLC | |
Well Pad ID: | |
Farm/Lease Name: SPECKMAN JAMES & LEULLA | |
License Status: Producing | |
License Date: 1983-11-17 | |
Spud Date: 1984-01-11 | |
Spud Drilling Contractor: CVAS DRLG | |
Final Drill Date: 1984-01-15 | |
Well Total Depth: 3686.00 ft | |
Configuration: Vertical | |
Latitude: 40.320000 | |
Longitude: -81.940000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1983-11-17 | 278 PRICE GREGG CORP GeoDate 11/17/83 |
Oil and Gas | 1983-11-17 | Issued Date 11/17/83 Expired Date 5/15/84 Acres 0020000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 03686 Proposed Drill Depth 03686 |
Original Spud | 1984-01-11 | R.I. 11-19-83 |
Completed | 1984-01-15 | R.I. 11-19-83 |
Reached Total Depth | 1984-01-15 | R.I. 11-19-83 |
CO | 1984-02-17 | 278 PRICE GREGG CORP GeoDate 9/16/81 |
Construction Permit Expires | 1984-05-15 | R.I. 11-19-83 |
Completion Report Received | 1984-09-07 | R.I. 11-19-83 |
Change of Owner | 2014-07-21 | Operator changed from 278, PRICE GREGG CORP to 9252, BRILEX LLC |
Record Last Modified | 2014-07-21 | R.I. 11-19-83 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3477 | 3510 | 60 |
3480 | 3510 | 0 | |
1997-06-29 | 3480 | 3510 | 0 |
3477 | 3510 | 60 | |
3477 | 3510 | 60 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 72000 Gal | 0 | FRAC;H2O |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | OHIO NATURAL FUEL CO | 6069.00 | 317.00 | 365 |
1985 | OHIO NATURAL FUEL CO | 4089.00 | 160.00 | 365 |
1986 | EAGLE EXPL CO/JOHNSON J | 3260.00 | 53.00 | 150 |
1988 | EAGLE EXPL CO/JOHNSON J | 1567.00 | 43.00 | 60 |
1989 | DIAMOND ENERGY RESOUR INC | 1157.00 | 0.00 | 153 |
1990 | DIAMOND ENERGY RESOUR INC | 2568.00 | 44.00 | 365 |
1991 | GREGG PRICE CORP | 21.00 | 40.00 | 365 |
1992 | GREGG PRICE CORP | 1361.00 | 26.00 | 365 |
1993 | GREGG PRICE CORP | 1450.00 | 20.00 | 365 |
1994 | GREGG PRICE CORP | 1356.00 | 0.00 | 365 |
1995 | GREGG PRICE CORP | 1100.00 | 0.00 | 365 |
1996 | GREGG PRICE CORP | 541.00 | 0.00 | 365 |
1997 | GREGG PRICE CORP | 234.00 | 0.00 | 365 |
1998 | GREGG PRICE CORP | 455.00 | 0.00 | 365 |
1999 | GREGG PRICE CORP | 336.00 | 22.00 | 365 |
2000 | GREGG PRICE CORP | 258.00 | 0.00 | 365 |
2001 | GREGG PRICE CORP | 169.00 | 10.00 | 365 |
2002 | GREGG PRICE CORP | 174.00 | 0.00 | 365 |
2003 | GREGG PRICE CORP | 89.00 | 0.00 | 365 |
2004 | GREGG PRICE CORP | 228.00 | 16.00 | 365 |
2005 | GREGG PRICE CORP | 165.00 | 17.00 | 365 |
2006 | GREGG PRICE CORP | 162.00 | 0.00 | 365 |
2007 | GREGG PRICE CORP | 216.00 | 15.00 | 365 |
2008 | GREGG PRICE CORP | 403.00 | 0.00 | 365 |
2009 | GREGG PRICE CORP | 493.00 | 8.00 | 365 |
2010 | GREGG PRICE CORP | 282.00 | 0.00 | 365 |
2011 | GREGG PRICE CORP | 383.00 | 6.00 | 365 |
2012 | GREGG PRICE CORP | 338.00 | 0.00 | 366 |
2013 | GREGG PRICE CORP | 226.00 | 7.00 | 365 |
2014 | GREGG PRICE CORP | 0.00 | 0.00 | 365 |
2015 | BRILEX LLC | 108.00 | 12.00 | 365 |
2016 | BRILEX LLC | 233.00 | 0.00 | 365 |
2017 | BRILEX LLC | 291.00 | 9.00 | 365 |
2018 | BRILEX LLC | 135.00 | 20.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | OHIO NATURAL FUEL CO | Brine | 0 | 365 |
1985 | OHIO NATURAL FUEL CO | Brine | 25 | 365 |
1986 | EAGLE EXPL CO/JOHNSON J | Brine | 0 | 150 |
1988 | EAGLE EXPL CO/JOHNSON J | Brine | 0 | 60 |
1989 | DIAMOND ENERGY RESOUR INC | Brine | 9 | 153 |
1990 | DIAMOND ENERGY RESOUR INC | Brine | 0 | 365 |
1991 | GREGG PRICE CORP | Brine | 0 | 365 |
1992 | GREGG PRICE CORP | Brine | 0 | 365 |
1993 | GREGG PRICE CORP | Brine | 0 | 365 |
1994 | GREGG PRICE CORP | Brine | 0 | 365 |
1995 | GREGG PRICE CORP | Brine | 0 | 365 |
1996 | GREGG PRICE CORP | Brine | 0 | 365 |
1997 | GREGG PRICE CORP | Brine | 0 | 365 |
1998 | GREGG PRICE CORP | Brine | 0 | 365 |
1999 | GREGG PRICE CORP | Brine | 0 | 365 |
2000 | GREGG PRICE CORP | Brine | 0 | 365 |
2001 | GREGG PRICE CORP | Brine | 0 | 365 |
2002 | GREGG PRICE CORP | Brine | 0 | 365 |
2003 | GREGG PRICE CORP | Brine | 0 | 365 |
2004 | GREGG PRICE CORP | Brine | 0 | 365 |
2005 | GREGG PRICE CORP | Brine | 0 | 365 |
2006 | GREGG PRICE CORP | Brine | 0 | 365 |
2007 | GREGG PRICE CORP | Brine | 0 | 365 |
2008 | GREGG PRICE CORP | Brine | 0 | 365 |
2009 | GREGG PRICE CORP | Brine | 0 | 365 |
2010 | GREGG PRICE CORP | Brine | 0 | 365 |
2011 | GREGG PRICE CORP | Brine | 0 | 365 |
2012 | GREGG PRICE CORP | Brine | 0 | 366 |
2013 | GREGG PRICE CORP | Brine | 0 | 365 |
2014 | GREGG PRICE CORP | Brine | 0 | 365 |
2015 | BRILEX LLC | Brine | 0 | 365 |
2016 | BRILEX LLC | Brine | 0 | 365 |
2017 | BRILEX LLC | Brine | 2 | 365 |
2018 | BRILEX LLC | Brine | 3 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1178385408 | 2002-12-11 0:00 | PW | No Violations | |
-1261141076 | 2002-12-11 0:00 | PW | No Violations | |
-1714503666 | 2016-2-29 0:00: | PW | No Violations | 0.30 |
-1829168784 | 2013-4-3 0:00:0 | PW | No Violations | |
-623012440 | 2004-7-30 0:00: | PW | No Violations | |
-789777968 | 2003-3-18 0:00: | PW | No Violations | |
000VER1359 | 1996-10-11 | Production Wells | No Violations | |
0043962653 | 2017-04-07 | Production Wells | No Violations | On the day of my inspection I found that the wellhead was equipped with a plunger lift system. The flow line was connected and the tubing valve was open. There were no leaks at the wellhead. The tank battery consisted of one 140 barrel steel tank, one 70 barrel steel tank and one horizontal separator in an earthen dike. There were no leaks or spills around the production equipment. The tank battery is shared with permits 4301, 4302, 4303, 4243 and 4245. Identification signs were posted at the tank battery and at the wellheads, but they were all blank. I met Frank Riggle in the field and spoke with him about getting all of the ID signs correctly filled out. He said that they would get it taken care of. |
0402037382 | 2003-10-27 | Production Wells | No Violations | Non compliance for well head identification . Request permit hold list . |
0623012440 | 2004-07-30 | Production Wells | No Violations | 7/30/04 Storage tank id no id at well head . |
0729841091 | 2008-12-22 | Production Wells | No Violations | ID posted , compliance . |
0789777968 | 2003-03-18 | Production Wells | Violations Noted | line inside dike leaked oil . Line has been repaired . REMOVE OIL INSIDE DIKE . IDENTIFY ALL WELLS ON LEASE AT WELL .Notified Mark Clark by phone 2/6/04 to have ids posted within 30 days . Called Mark Clarke 4/27/04 requested 2 week extension . 7/30/0 |
1178385408 | 2002-12-11 | Production Wells | Violations Noted | FOLLOW UP TO NOV # -1261141076 no id at well head . Notified Mark Clark by phone 2/6/04 to have ids posted within 30 days . Called Mark Clarke 4/27/04 requested 2 week extension . 7/30/04 Storage tank id no id at well head . COMPLIANCE 10/19/04 ID POS |
1225207958 | 2008-10-28 | Production Wells | No Violations | Meet Mark Clarke at well site , went over violations at lease . Line at storage tank has been repaired contaminated soil from inside dike has been removed . Well head is identified , gas leak at well head has been repaired . |
1261141076 | 2002-12-11 | Production Wells | Violations Noted | no id at well head .Notified Mark Clark by phone 2/6/04 to have ids posted within 30 days . Called Mark Clarke 4/27/04 requested 2 week extension . 7/30/04 Storage tank id no id at well head . COMPLIANCE 10/19/04 ID POSTED |
1286315607 | 2008-10-20 | Production Wells | Violations Noted | Well head isnt identified at well head , well is using common storage tank . Small gas leak at well , 2 valve is leaking . 2 line going up side of storage tank is leaking , 4 area around line has oil on ground . |
1341191785 | 2004-10-19 | Production Wells | No Violations | COMPLIANCE 10/19/04 ID POSTED |
1454863452 | 2020-4-2 0:00:0 | PW | No Violations | 0.50 |
1714503666 | 2016-02-29 | Production Wells | No Violations | On the day of my inspection I found that the wellhead was equipped with a plunger lift system. The tubing valve was open. The tank battery consisted of one 140 barrel steel tank, one 70 barrel steel tank, one separator and an earthen dike. The tank battery is shared with permits 4301, 4302, 4303, 4243 and 4245. Identification was posted at the tank battery and at the wellhead. I found no leaks or spills. |
1829168784 | 2013-04-03 | Production Wells | No Violations | On the day of my inspection I found that the well head was equipped with a plunger lift system and connected to a tank battery that consisted of one 140 barrel stock tank, one 70 barrel brine tank, one separator and an earthen dike. Proper identification was posted and there were no leaks or spills. This well shares a tank battery with permits 4243, 4245, 4301, 4302 and 4303. No violations at this time. |
402037382 | 2003-10-27 0:00 | PW | No Violations | |
43962653 | 2017-4-7 0:00:0 | PW | No Violations | 0.70 |
729841091 | 2008-12-22 0:00 | PW | No Violations | |
VER1359 | 1996-10-11 0:00 | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0789777968 | US-OH-128986 | 2003-03-18 | Well operation causing pollution and contamination | |
0789777968 | US-OH-128987 | 2003-03-18 | Failure to legibly identify well | |
1178385408 | US-OH-104746 | 2002-12-11 | Failure to legibly identify well | |
1261141076 | US-OH-107029 | 2002-12-11 | Failure to legibly identify well | |
1286315607 | US-OH-107929 | 2008-10-20 | Well operation causing pollution and contamination | |
1286315607 | US-OH-107930 | 2008-10-20 | Failure to legibly identify well | |
1286315607 | US-OH-107931 | 2008-10-20 | Unlawful venting or flaring of gas |
For data sources see[9]