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Well ID: 34-121-23025 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Center Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: LYONS GARY W | |
License Status: Producing | |
License Date: 2015-07-20 | |
Spud Date: 1983-06-24 | |
Spud Drilling Contractor: [[JL COATS [COATS-GOFF]]] | |
Final Drill Date: 1983-06-29 | |
Well Total Depth: 5784.00 ft | |
Configuration: Vertical | |
Latitude: 39.770000 | |
Longitude: -81.500000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1983-06-13 | 122 TIGER OIL INC GeoDate 6/13/83 |
Oil and Gas | 1983-06-13 | Issued Date 6/13/83 Expired Date 12/10/83 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05784 Proposed Drill Depth 05784 |
Original Spud | 1983-06-22 | PB WRC 12/21/15 35 MCF from Devonian Sh. |
Completed | 1983-06-29 | PB WRC 12/21/15 35 MCF from Devonian Sh. |
Reached Total Depth | 1983-06-29 | PB WRC 12/21/15 35 MCF from Devonian Sh. |
Completion Report Received | 1983-07-08 | PB WRC 12/21/15 35 MCF from Devonian Sh. |
CO | 1994-11-28 | 2680 ENERGY CONTRACTORS INC GeoDate 6/13/83 |
Change of Owner | 1998-09-28 | Operator changed from 2680, ENERGY CONTRACTORS INC to 56, BUCKEYE OIL PRODUCING CO |
Change of Owner | 2001-10-22 | Operator changed from 56, BUCKEYE OIL PRODUCING CO to 201, GREEN GAS CO |
Last Compliance Report | 2013-04-25 | PB WRC 12/21/15 35 MCF from Devonian Sh. |
Change of Owner | 2013-08-14 | Operator changed from 201, GREEN GAS CO to 1634, NORTHWOOD ENERGY CORP |
APP | 2015-07-20 | Proposed Formations:BEREA/DEVONIAN/ORISKANY, Issued Date:7/20/2015, Expired Date:7/19/2017 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Plugged Back | 2015-10-05 | PB WRC 12/21/15 35 MCF from Devonian Sh. |
Record Last Modified | 2017-02-15 | PB WRC 12/21/15 35 MCF from Devonian Sh. |
Construction Permit Expires | 2017-07-19 | PB WRC 12/21/15 35 MCF from Devonian Sh. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2015-12-21 | 1638 | 2432 | 138 |
5642 | 5708 | 0 | |
1997-06-29 | 5642 | 5708 | 0 |
5650 | 5680 | 15 | |
1638 | 2432 | 138 | |
1638 | 2432 | 138 | |
2006-09-11 | 5650 | 5680 | 15 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1200 Bbl | 30000 | FRAC;1200BBL H2O,30M# SD,500GAL ACID | ||
2015-10-28 | H2O | 8 | 7773 Bbl | 80000 | Producers Service Corporation | 138 SHOTS |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | TIGER OIL INC | 8948.00 | 0.00 | 0 |
1985 | TIGER OIL INC | 3389.00 | 0.00 | 365 |
1986 | TIGER OIL INC | 2292.00 | 0.00 | 365 |
1987 | TIGER OIL INC | 4315.00 | 0.00 | 365 |
1989 | TIGER OIL INC | 5850.00 | 0.00 | 365 |
1990 | TIGER OIL INC | 3508.00 | 0.00 | 365 |
1991 | TIGER OIL INC | 2535.00 | 0.00 | 365 |
1992 | TIGER OIL INC | 1885.00 | 0.00 | 365 |
1993 | TIGER OIL INC | 1649.00 | 0.00 | 360 |
1994 | TIGER OIL INC | 1741.00 | 0.00 | 365 |
1995 | ENERGY CONTRACTORS INC | 1507.00 | 0.00 | 365 |
1996 | ENERGY CONTRACTORS INC | 1459.00 | 0.00 | 365 |
1997 | ENERGY CONTRACTORS INC | 5430.00 | 0.00 | 365 |
1998 | ENERGY CONTRACTORS INC | 26.00 | 0.00 | 365 |
1999 | BUCKEYE OIL PRODUCING CO | 2432.00 | 0.00 | 0 |
2000 | BUCKEYE OIL PRODUCING CO | 1766.00 | 0.00 | 0 |
2001 | BUCKEYE OIL PRODUCING CO | 751.00 | 0.00 | 365 |
2002 | GREEN GAS CO | 1602.00 | 0.00 | 365 |
2003 | GREEN GAS CO | 1282.00 | 0.00 | 365 |
2004 | GREEN GAS CO | 1350.00 | 0.00 | 365 |
2005 | GREEN GAS CO | 38.00 | 0.00 | 365 |
2006 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2007 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2008 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2009 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2011 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2012 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2013 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2014 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2015 | NORTHWOOD ENERGY CORP | 411.00 | 0.00 | 365 |
2016 | NORTHWOOD ENERGY CORP | 782.00 | 70.00 | 365 |
2017 | NORTHWOOD ENERGY CORP | 1770.00 | 154.00 | 365 |
2018 | NORTHWOOD ENERGY CORP | 1402.00 | 117.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | TIGER OIL INC | Brine | 0 | 0 |
1985 | TIGER OIL INC | Brine | 0 | 365 |
1986 | TIGER OIL INC | Brine | 0 | 365 |
1987 | TIGER OIL INC | Brine | 0 | 365 |
1989 | TIGER OIL INC | Brine | 0 | 365 |
1990 | TIGER OIL INC | Brine | 0 | 365 |
1991 | TIGER OIL INC | Brine | 0 | 365 |
1992 | TIGER OIL INC | Brine | 0 | 365 |
1993 | TIGER OIL INC | Brine | 0 | 360 |
1994 | TIGER OIL INC | Brine | 0 | 365 |
1995 | ENERGY CONTRACTORS INC | Brine | 0 | 365 |
1996 | ENERGY CONTRACTORS INC | Brine | 0 | 365 |
1997 | ENERGY CONTRACTORS INC | Brine | 0 | 365 |
1998 | BUCKEYE OIL PRODUCING CO | Brine | 141 | |
1999 | BUCKEYE OIL PRODUCING CO | Brine | 260 | |
2000 | BUCKEYE OIL PRODUCING CO | Brine | 3 | |
2001 | BUCKEYE OIL PRODUCING CO | Brine | 6 | 365 |
2002 | GREEN GAS CO | Brine | 0 | 365 |
2003 | GREEN GAS CO | Brine | 0 | 365 |
2004 | GREEN GAS CO | Brine | 0 | 365 |
2005 | GREEN GAS CO | Brine | 0 | 365 |
2006 | GREEN GAS CO | Brine | 0 | 0 |
2007 | GREEN GAS CO | Brine | 0 | 0 |
2008 | GREEN GAS CO | Brine | 0 | 0 |
2009 | GREEN GAS CO | Brine | 0 | 0 |
2011 | GREEN GAS CO | Brine | 0 | |
2012 | GREEN GAS CO | Brine | 0 | 0 |
2013 | GREEN GAS CO | Brine | 0 | 0 |
2014 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2015 | NORTHWOOD ENERGY CORP | Brine | 4438 | 365 |
2016 | NORTHWOOD ENERGY CORP | Brine | 903 | 365 |
2017 | NORTHWOOD ENERGY CORP | Brine | 202 | 365 |
2018 | NORTHWOOD ENERGY CORP | Brine | 117 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1204745519 | 2015-9-18 0:00: | PB | No Violations | 5.00 |
-1948790560 | 2015-9-23 0:00: | PB | No Violations | 3.00 |
-32266069 | 2015-9-17 0:00: | PB | No Violations | 3.00 |
-571344686 | 2015-9-1 0:00:0 | PB | No Violations | 2.00 |
-648283261 | 2020-3-26 0:00: | PW | No Violations | 1.00 |
0000PL7683 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0032266069 | 2015-09-17 | Plug / Plug Back | No Violations | My inspection today finds the service rig is unable to pull the casing. Producers well service attempted to circulate the casing free. Circulation could not be established. The service rig will run tubing in the well tomorrow and spot a cement plug at the Big Lime. |
0175547882 | 2015-09-02 | Plug / Plug Back | No Violations | My inspection today finds the kick over skirt and overshot have sat down at 2240. Cemenco will be onsite tomorrow to attempt to wash the casing to bottom. |
0332619133 | 2008-07-03 | Annular Disposal | No Violations | A.D. not hooked up, well is equipped with tubing(rabbit well) and 1-100 bbl tank,well is shut in at present time will call well owner and discuss future plans for said well. |
0571344686 | 2015-09-01 | Plug / Plug Back | No Violations | My inspection today finds Davis well service is pulling the 4.5 casing out of the well. The casing pulled hard for the first nine joints. |
1168410570 | 2019-01-03 | Production Wells | No Violations | On the day of my inspection I witnessed production equipment included a 210-barrel steel production fluid storage tank, 100-barrel steel production fluid storage tank, horizontal separator, drip and a domestic gas meter all enclosed within an earthen dike. The well was equipped with 8.625-inch diameter surface casing, 4.5-inch diameter production casing, 2.375-inch diameter tubing, rods, and a pumping unit with natural gas motor. At the time of my inspection there were several small leaks on the 210-barrel production fluid storage tank, there were also leaks around the stuffing box, and back pressure regulators on the well. Oil had just been hauled off of the 210- |
1204745519 | 2015-09-18 | Plug / Plug Back | No Violations | I am onsite to witness the placement of the Big Lime plug. Cemenco place a thirty sack plug from 4122 to 4022. The service rig will tag the plug with the tubing on Monday. |
1364915405 | 2013-04-02 | Annular Disposal | No Violations | A.D. not hooked up, well is equipped with tubing (rabbit well) and 1-100 bbl tank. The well is shut in at present time will call the well owner and discuss future plans for said well. |
1385756513 | 2015-09-10 | Plug / Plug Back | No Violations | I am onsite to witness casing recovery operations. Jet Wireline Services ran a casing cutter three times before getting it to detonate. The service rig pulled on the casing, but was unable to move it. Jet Wireline tried to cut the casing again with a collar buster shot, but was unable to detonate the charge. |
175547882 | 2015-9-2 0:00:0 | PB | No Violations | 2.00 |
1948790560 | 2015-09-23 | Plug / Plug Back | No Violations | My inspection today finds Jet Wireline Service is onsite attempting to run a bond log, but they are having difficulty getting down the hole. |
2049405816 | 2015-08-31 | Plug / Plug Back | No Violations | My inspection today finds the service rig, Davis Well Service, is attempting to run 1.5 tubing to the Clinton in order to set a bottom hole plug. At 2840 the 1.5 tubing began to set down. The rig crew believes the tubing is going outside of the casing. After trying for over an hour to get back in the casing the decision was made to pull the tubing and then pull the casing. The casing will be ran back with a kick over skirt and an overshot. |
230151291 | 2020-3-9 0:00:0 | PW | No Violations | 1.00 |
332619133 | 2008-7-3 0:00:0 | AD | No Violations | |
PL7683 | PL | No Violations |
For data sources see[9]