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Well ID: 34-121-23364 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Jackson Township | |
Operator Name: G-R CONTRACTING INC | |
Well Pad ID: | |
Farm/Lease Name: BOYD WAGNER | |
License Status: Final Restoration | |
License Date: 2012-08-09 | |
Spud Date: 1984-10-27 | |
Spud Drilling Contractor: MID ATLANTC DRLG | |
Final Drill Date: 1984-11-02 | |
Well Total Depth: 6366.00 ft | |
Configuration: Vertical | |
Latitude: 39.640000 | |
Longitude: -81.490000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1984-10-22 | Issued Date 10/22/84 Expired Date 4/20/85 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06366 Proposed Drill Depth 06366 |
Original Spud | 1984-10-26 | FDT=RED SHALE |
Completed | 1984-11-02 | FDT=RED SHALE |
Reached Total Depth | 1984-11-02 | FDT=RED SHALE |
CO | 1985-01-01 | 1530 CNG PRODUCING COMPANY GeoDate 10/22/84 |
Completion Report Received | 1986-02-20 | FDT=RED SHALE |
CO | 1991-08-19 | 28 CGAS EXPLORATION,INC GeoDate 10/22/84 |
Change of Owner | 1998-01-21 | Operator changed from 28, CGAS EXPLORATION to 5352, ARTEX OIL COMPANY |
Change of Owner | 2003-05-06 | Operator changed from 5352, ARTEX OIL COMPANY to 952, G-R CONTRACTING INC |
APP | 2012-08-09 | Proposed Formations:CLINTON/MEDINA, Issued Date:8/9/2012, Expired Date:8/9/2014 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Plugged/Abandoned | 2012-12-21 | FDT=RED SHALE |
Construction Permit Expires | 2014-08-09 | FDT=RED SHALE |
Record Last Modified | 2017-02-15 | FDT=RED SHALE |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 6074 | 6122 | 0 |
6074 | 6122 | 0 | |
2006-09-11 | 6088 | 6121 | 22 |
6088 | 6121 | 22 | |
6074 | 6122 | 0 | |
2006-09-11 | 6222 | 6236 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 170 Mscf | 0 | CLINTON | ||
H2O | 0 | 45000 Gal | 50000 | CLINTON | ||
H2O | 0 | 30000 Gal | 32800 | FRAC;H2O,SAND,N2,CO2 | ||
CO2 | 0 | 15 Tons | 0 | MEDINA |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | CNG PRODUCING COMPANY | 2896.00 | 143.00 | 365 |
1988 | CNG PRODUCING COMPANY | 59003.00 | 0.00 | 290 |
1989 | CNG PRODUCING COMPANY | 1019.00 | 0.00 | 365 |
1990 | CNG PRODUCING COMPANY | 403.00 | 0.00 | 365 |
1991 | CGAS EXPLORATION | 639.00 | 0.00 | 365 |
1992 | CGAS EXPLORATION | 1565.00 | 0.00 | 366 |
1993 | CGAS EXPLORATION | 407.00 | 50.00 | 366 |
1994 | CGAS EXPLORATION | 669.00 | 0.00 | 365 |
1995 | CGAS EXPLORATION | 305.00 | 0.00 | 365 |
1996 | CGAS EXPLORATION | 510.00 | 0.00 | 365 |
1997 | CGAS EXPLORATION | 265.00 | 0.00 | 365 |
1998 | ARTEX OIL COMPANY | 544.00 | 37.00 | 0 |
1999 | ARTEX OIL COMPANY | 778.00 | 0.00 | 0 |
2000 | ARTEX OIL COMPANY | 500.00 | 0.00 | 365 |
2001 | ARTEX OIL COMPANY | 289.00 | 0.00 | 365 |
2002 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2003 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2004 | G-R CONTRACTING INC | 106.00 | 0.00 | 365 |
2005 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2006 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2007 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2008 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2009 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2010 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
2011 | G-R CONTRACTING INC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | CNG PRODUCING COMPANY | Brine | 33 | 365 |
1988 | CNG PRODUCING COMPANY | Brine | 915 | 290 |
1989 | CNG PRODUCING COMPANY | Brine | 80 | 365 |
1990 | CNG PRODUCING COMPANY | Brine | 90 | 365 |
1991 | CGAS EXPLORATION | Brine | 80 | 365 |
1992 | CGAS EXPLORATION | Brine | 239 | 366 |
1993 | CGAS EXPLORATION | Brine | 0 | 366 |
1994 | CGAS EXPLORATION | Brine | 0 | 365 |
1995 | CGAS EXPLORATION | Brine | 0 | 365 |
1996 | CGAS EXPLORATION | Brine | 0 | 365 |
1997 | CGAS EXPLORATION | Brine | 0 | 365 |
1998 | ARTEX OIL COMPANY | Brine | 50 | |
1999 | ARTEX OIL COMPANY | Brine | ||
2000 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2001 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2002 | G-R CONTRACTING INC | Brine | 0 | 365 |
2003 | G-R CONTRACTING INC | Brine | 0 | 365 |
2004 | G-R CONTRACTING INC | Brine | 0 | 365 |
2005 | G-R CONTRACTING INC | Brine | 0 | 365 |
2006 | G-R CONTRACTING INC | Brine | 0 | 365 |
2007 | G-R CONTRACTING INC | Brine | 0 | 365 |
2008 | G-R CONTRACTING INC | Brine | 0 | 365 |
2009 | G-R CONTRACTING INC | Brine | 0 | 365 |
2010 | G-R CONTRACTING INC | Brine | 0 | 365 |
2011 | G-R CONTRACTING INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1584743337 | 2013-9-17 0:00: | FR | No Violations | 2.00 |
-1873258866 | 2012-6-7 0:00:0 | PW | No Violations | |
-2072794813 | 2012-6-7 0:00:0 | PW | No Violations | |
0000PL7458 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0100979902 | 2012-11-19 | Production Wells | No Violations | My inspection today finds that the status of the well has not changed. There is still a slight smell of sulfur. The well is not producing. I called G-R Contracting at 8:27 am. Dick Shulzberger was not available, I left a message with the receptionist for him to call me back. |
100979902 | 2012-11-19 0:00 | PW | No Violations | 0.50 |
1339106476 | 2012-06-07 | Production Wells | Violations Noted | Upon inspecting wellsite found well to be idle there is a slight sulpur ordor at wellhead and well is equipped with 8 surface casing and 4.5 production casing and 1.5 tubing and 1-100 bbl tank and all valves at wellhead were shut and last production reported on well was back in 2006 .
Plug well within 60 days. Failure to comply may result in bond forfieture. |
1348747972 | 2012-09-24 | Production Wells | No Violations | Today I called G-R Contracting, and spoke to Dick Shulzberger about plugging the well. I told him that the leak at the well head is getting worse according to the land owner, and that when I tested the gas at the leak it showed 17ppm H2S. Mr. Shulzberger said that he would call me back to further discuss a time table for plugging the well. The call took place at 10:27 sep.24, 2012 |
1355414155 | 2012-12-13 | Production Wells | No Violations | My inspection today finds that the status of the well has not changed. At 10:40am I called G-R Contracting and spoke to Mr. Shulzberger. I reminded him that the well is under a chiefs order and it must be plugged immediately. He stated that he would call me back with a time line. |
1355773428 | 2012-12-17 | Plug / Plug Back | No Violations | I am onsite to witness the rig crew pull tubing. The rig operator stated that on Sat. his H2S monitor registered a reading of 200 ppm. I asked the rig crew to gather materials to flare the 8.625 casing. Before flaring the rig crew tested the H2S level with my monitor, and it showed over 250 ppm. The rig crew lit the flare and began to burn off the gas. 80 bbl of brine was placed down the 8 pipe. |
1356094626 | 2012-12-20 | Plug / Plug Back | No Violations | I am on site to witness plugging operations. The rig crew ran the tubing to a depth of 6086. Formation cementing placed a 30 sack plug of 50/50 poz mix through the tubing. The rig crew then pulled 44 joints of tubing. The bottom of the tubing was at 4590 and the lime perforations were at 4586. Formation set a 79 sack plug of 50/50 poz mix at that point. |
1527705643 | 2012-12-14 | Plug / Plug Back | No Violations | I am onsite to witness the operator put brine down the tubing in order to kill the gas flow. 80 bbl of fluid was put down the tubing. The tubing appears to be unobstructed to the bottom. |
1584743337 | 2013-09-17 | Final Restoration | No Violations | My inspection today finds the final restoration is complete. Vegetation has been established, and all production equipment has been removed. |
1595988353 | 2008-09-09 | Production Wells | No Violations | Inspection revealed that well is shut in suspect hole in casing, well is equipped with 8 surface casing and 4.5 production casing and 1.5 tubing all valves at wellhead were shut on the day of my inspection. |
1842482210 | 2012-06-12 | Production Wells | No Violations | Follow up inspection per request of lead inspector Dave Ball , Inspection found well shut in and idle commercially but does have the domestic valve open and a meter present . Well is leaking gas from around the casing slips . No current chart is present in gas sales meter . |
1873258866 | 2012-06-07 | Production Wells | No Violations | Inspection found well shut in and no reported production since 2006 . Will refer to lead inspector for corrective action . |
2072794813 | 2012-06-07 | Production Wells | No Violations | FOLLOW UP TO NOV # 1339106476 Upon inspecting wellsite found well to be idle there is a slight sulpur ordor at wellhead and well is equipped with 8 surface casing and 4.5 production casing and 1.5 tubing and 1-100 bbl tank and all valves at wellhead were shut and last production reported on well was back in 2006 .
Plug well within 60 days. Failure to comply may result in bond forfieture. |
2131612795 | 2012-12-21 | Plug / Plug Back | No Violations | My inspection today finds that Appalachian Well Survey cut the casing at a depth of 3300. Formation set a 100 plug at 3300. The rig crew pulled the 4.5 casing up to a depth of 2001 and a 200 plug was set with 100 in the 8.625 casing. The rig crew pulled pipe and set the last plug at 200 up to surface. |
PL7458 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1339106476 | US-OH-109754 | 2012-06-07 | General Safety | |
1339106476 | US-OH-109755 | 2012-06-07 | Well insufficiently equipped to prevent escape of oil and gas | |
1339106476 | US-OH-109756 | 2012-06-07 | Well shall be plugged | |
1339106476 | US-OH-109757 | 2012-06-07 | Defective casing, leaking well | |
1339106476 | US-OH-109758 | 2012-06-07 | Statement of annual production not filed |
For data sources see[9]