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Well ID: 34-121-23494 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Adams Township | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: JOLLES UNIT | |
License Status: Final Restoration | |
License Date: 2016-04-26 | |
Spud Date: 1985-11-30 | |
Spud Drilling Contractor: DYNAMIC DRILLING | |
Final Drill Date: 1985-12-05 | |
Well Total Depth: 5818.00 ft | |
Configuration: Vertical | |
Latitude: 39.580000 | |
Longitude: -81.560000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1985-11-05 | 1264 ROCKWELL RESOURCES INC GeoDate 11/5/85 |
Oil and Gas | 1985-11-05 | Issued Date 11/5/85 Expired Date 11/5/86 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05818 Proposed Drill Depth 05818 |
Original Spud | 1985-11-30 | |
Completed | 1985-12-05 | |
Reached Total Depth | 1985-12-05 | |
Completion Report Received | 1985-12-20 | |
APP | 2007-04-02 | Proposed Formations:CLINTON/MEDINA, Issued Date:4/2/2007, Expired Date:4/1/2008 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2007-04-11 | Operator changed from 1264, ROCKWELL RESOURCES INC to 8172, APPALACHIAN ENERGY RES LLC |
Change of Owner | 2007-11-08 | Operator changed from 1264, ROCKWELL RESOURCES INC to 8172, APPALACHIAN ENERGY RES LLC |
Change of Owner | 2008-08-27 | Operator changed from 8172, APPALACHIAN ENERGY RES LLC to 1634, NORTHWOOD ENERGY CORP |
APP | 2016-04-26 | Proposed Formations:, Issued Date:4/26/2016, Expired Date:4/26/2018 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2016-06-09 | |
Record Last Modified | 2017-02-15 | |
Construction Permit Expires | 2018-04-26 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5555 | 5588 | 32 |
5556 | 5606 | 0 | |
1997-06-29 | 5556 | 5606 | 0 |
5555 | 5588 | 32 | |
5555 | 5588 | 32 | |
2006-09-11 | 5672 | 5684 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1350 Bbl | 40000 | FRAC;H2O,SAND,N2 | ||
N2 | 0 | 170 Mscf | 0 | CLINTON | ||
H2O | 0 | 950 Bbl | 40000 | MEDINA | ||
N2 | 0 | 160 Mscf | 0 | MEDINA |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | DERBY OIL & GAS CORP | 9140.00 | 0.00 | 270 |
1987 | CHRISTA OIL CO | 13462.00 | 0.00 | 362 |
1988 | BAUGHMAN ELEANOR | 7850.00 | 0.00 | 322 |
1993 | ROCKWELL RESOURCES INC | 4214.00 | 0.00 | 365 |
1994 | ROCKWELL RESOURCES INC | 3536.00 | 0.00 | 365 |
2002 | ROCKWELL RESOURCES INC | 545.00 | 0.00 | 365 |
2008 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2009 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2010 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2011 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2012 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2013 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2014 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2015 | NORTHWOOD ENERGY CORP | 0.00 | 0.00 | 0 |
2016 | NORTHWOOD ENERGY CORP | 0.00 | 12.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | DERBY OIL & GAS CORP | Brine | 226 | 270 |
1987 | CHRISTA OIL CO | Brine | 175 | 362 |
1988 | BAUGHMAN ELEANOR | Brine | 40 | 322 |
1993 | ROCKWELL RESOURCES INC | Brine | 0 | 365 |
1994 | ROCKWELL RESOURCES INC | Brine | 0 | 365 |
2002 | ROCKWELL RESOURCES INC | Brine | 0 | 365 |
2008 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2009 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2010 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2011 | NORTHWOOD ENERGY CORP | Brine | 0 | |
2012 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2013 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2014 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2015 | NORTHWOOD ENERGY CORP | Brine | 0 | 0 |
2016 | NORTHWOOD ENERGY CORP | Brine | 116 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1325169294 | 2016-5-25 0:00: | PB | No Violations | 3.00 |
-1474859461 | 2016-5-24 0:00: | PB | No Violations | 4.00 |
-1586292202 | 2006-11-16 0:00 | PW | No Violations | |
-1643376446 | 2016-6-6 0:00:0 | PB | No Violations | 3.50 |
-1841737501 | 2014-2-28 0:00: | AM | No Violations | |
-384141204 | 2016-5-31 0:00: | PB | No Violations | 5.00 |
0000PL7389 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0250647433 | 2016-07-19 | Final Restoration | No Violations | My inspection today finds Biedenbach excavating has a bulldozer and an excavator onsite to reclaim the entry road. The pit has been filled and the location graded. |
0323077768 | 2016-03-29 | Production Wells | Violations Noted | My inspection today finds the well is currently owned by Northwood Energy. No discernible lease road was located. The well is equipped with 4.5 casing and 1.5 tubing that has broken completely in two. No gas was witnessed escaping from the defective tubing or casing; however, there is no ability to control the flow of oil or gas on the 1.5 tubing. The tank battery is comprised of one 100 barrel tank and a horizontal separator with an orifice meter. This is a re-issue of a previous Notice of Violation. Northwood Energy shall submit a written plugging schedule to Eric Conrad at 5880 Memory Road Zanesville, Ohio 43701 within 15 days, per OAC 1501:9-11-05(B), and plug the well within 90 days. Northwood Energy will be notified if the plugging schedule is approved or denied. |
0384141204 | 2016-05-31 | Plug / Plug Back | No Violations | I am onsite to witness the plugging operations. Davis Well Service pulled the casing and found 31 to 32 inches of stretch. The tubing swab tools were ran in the hole and sat down at 2614. Work was stopped for the day. |
0532224646 | 2006-06-30 | Production Wells | Violations Noted | No change in status of well(still idle) extension on Chiefs Order 2005-111 has expired,have tried to make contact with well owner with no response. |
0602216395 | 2016-06-09 | Plug / Plug Back | No Violations | My inspection today finds the well static. The cement top is down ten feet from the surface. The well has been plugged resolving the previous violations. |
0719323707 | 2006-01-18 | Production Wells | Violations Noted | Upon inspecting well site again found well to still idle,Called Mr. Darrel Cline and left message for him to call back with no response so their for Bond Forfiture Order requested. |
0763945627 | 2005-03-18 | Production Wells | No Violations
-100 bbl tank and separator,tubing.It appears this well had a domestic hookup at one time,all valves are shut and 2 nipple on tubing head is broke out venting small amount of gas. | |
0887505612 | 2009-01-08 | Production Wells | Violations Noted | No change in status of well it is still incapable of producing,tubing is broke off in wellhead and owner has no gas sales line in area to transport product to market if well was capable of producing . |
0925413632 | 2016-05-25 | Plug / Plug Back | No Violations | The purpose of my inspection today is to witness the bottom plug and the Big Lime plug. I was accompanied by ODNR Inspector LJ Parkins. During our inspection Davis Well Service was on location with Cemenco. See LJ Parkins report for further details on the plugging of this well. |
1111337069 | 2005-03-18 | Production Wells | Violations Noted
-100 bbl tank and separator,tubing.It appears this well had a domestic hookup at one time,all valves are shut and 2 nipple on tubing head is broke out venting small amount of gas. | |
1130490574 | 2005-10-25 | Production Wells | Violations Noted | Upon inspecting well site for compliance from previous violations of Idle well found no change in status of well(still idle&incapable of producing),had several conversations with well owner Darrel Cline with no results in getting well placed back into production ,recommend Chiefs Order to plug said well be issued. |
1251631532 | 2016-09-20 | Final Restoration | No Violations | My inspection today finds the well site meets the final restoration requirements of 1509.072(B). |
1325169294 | 2016-05-25 | Plug / Plug Back | No Violations | On location to witness plugging activities for this well. Davis Well Service is the plugging contractor. 1.5 tubing was hung high in the hole, so it was shot off at 5209 to allow for pumping of a bottom plug. Cemenco pumped 30 bbls of saltwater ahead and was able to establish circulation and free the tubing. Cemenco pumped a 400 bottom plug from 5209-4809 using 30 sks class A cement and 8.9 bbls saltwater displacement. Tubing was then pulled to 4150 and a 100 Newburg plug was set from 4150-4050 using 35 sks class A cement and 7.5 bbls saltwater displacement. Tubing will be pulled OOH to allow ripping of the 4.5 casing. I was accompanied on this plug job by Inspector Austin Gutridge. |
1459270770 | 2016-03-29 | Administrative Inspection | No Violations | The previous violation was written to Appalachian Energy and never re-issued to Northwood Energy after they took ownership. The violation will be re-issued. |
1461115839 | 2016-04-14 | Administrative Inspection | No Violations | I received a return call today from Mr. Bill Arnholt with Northwood Energy at 10:50 AM to discuss the well status of Permit Numbers 3494 and 3495. Mr. Arnholt was informed that both wells had contained a prior enforcement history of being idle with a previous owner, Rockwell Resources which included Bond Forfeiture. I discussed the recent issuance of Compliance Notices on both wells and emphasized that Mr. Arnholt meet the deadlines to avoid any further enforcement action. Mr. Arnholt stated the following: The wells would be plugged; Applications for plugging permits were filed this week; Cody McCuddon (sp?) is working on a plugging schedule. |
1464279173 | 2016-05-26 | Production Wells | No Violations | I am onsite to witness the plugging operations. Davis Well Service pulled the remaining tubing out of the well. They then blew down the 8.625 section, carefully monitoring for H2S. The rig crew then ran a wire line casing knife and set down at 2614. |
1474859461 | 2016-05-24 | Plug / Plug Back | No Violations | My inspection today finds the rig crew attempted to pull the 1.5 tubing. The tubing was stuck and Appalachian Well Surveys were dispatched to cut the tubing. The tubing was cut at 5209. The rig crew began pulling tubing. |
1586292202 | 2006-11-16 | Production Wells | Violations Noted | |
1643376446 | 2016-06-06 | Plug / Plug Back | No Violations | My inspection today finds Davis Well Service ripped the casing at 3195. The casing will be removed from the well and 2 tubing ran back to the same depth before spotting a 200 cement plug. |
1841737501 | 2014-02-28 | Administrative Inspection | No Violations | At 12:01 PM I called Bill Arnholt. I discussed the violation against the well with Mr. Arnholt. Bill stated that he intends to plug the well; however, no timeline exists to due so. |
250647433 | 2016-7-19 0:00: | FR | No Violations | 0.50 |
323077768 | 2016-3-29 0:00: | PW | No Violations | 2.00 |
532224646 | 2006-6-30 0:00: | PW | No Violations | |
602216395 | 2016-6-9 0:00:0 | PB | No Violations | 1.00 |
719323707 | 2006-1-18 0:00: | PW | No Violations | |
763945627 | 2005-3-18 0:00: | PW | No Violations | |
887505612 | 2009-1-8 0:00:0 | PW | No Violations | |
925413632 | 2016-5-25 0:00: | PB | No Violations | 4.00 |
PL7389 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0323077768 | US-OH-123381 | 2016-06-16 | General Safety | |
0323077768 | US-OH-123382 | 2016-06-16 | Failure to legibly identify well | |
0323077768 | US-OH-123383 | 2016-06-16 | Well shall be plugged | |
0323077768 | US-OH-123384 | 2016-06-16 | Defective casing, leaking well | |
0532224646 | US-OH-125818 | 2005-03-20 | Well insufficiently equipped to prevent escape of oil and gas | |
0532224646 | US-OH-125819 | 2005-03-20 | Well shall be plugged | |
0719323707 | US-OH-128170 | 2005-03-20 | Well insufficiently equipped to prevent escape of oil and gas | |
0719323707 | US-OH-128171 | 2005-03-20 | Well shall be plugged | |
0887505612 | US-OH-130117 | 2005-03-20 | Well insufficiently equipped to prevent escape of oil and gas | |
0887505612 | US-OH-130118 | 2005-03-20 | Well shall be plugged | |
1111337069 | US-OH-102782 | 2005-03-20 | Well insufficiently equipped to prevent escape of oil and gas | |
1111337069 | US-OH-102783 | 2005-03-20 | Well shall be plugged | |
1130490574 | US-OH-103313 | 2005-03-20 | Well insufficiently equipped to prevent escape of oil and gas | |
1130490574 | US-OH-103314 | 2005-03-20 | Well shall be plugged | |
1586292202 | US-OH-115515 | 2005-03-20 | Well insufficiently equipped to prevent escape of oil and gas | |
1586292202 | US-OH-115516 | 2005-03-20 | Well shall be plugged |
For data sources see[9]