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Well ID: 34-089-24238 | Loading map...
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Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Bowling Green Township | |
Operator Name: ZENITH OIL & GAS INC | |
Well Pad ID: | |
Farm/Lease Name: EMERINE | |
License Status: Producing | |
License Date: 1985-04-03 | |
Spud Date: 1982-10-09 | |
Spud Drilling Contractor: J & V DRLG | |
Final Drill Date: 1982-12-03 | |
Well Total Depth: 3041.00 ft | |
Configuration: Vertical | |
Latitude: 39.950000 | |
Longitude: -82.270000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1982-09-09 | Issued Date 9/9/82 Expired Date 3/1/83 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 03041 Proposed Drill Depth 03041 |
Original Spud | 1982-10-09 | |
Completed | 1982-12-03 | |
Reached Total Depth | 1982-12-03 | |
CO | 1982-12-16 | 193 ZENITH OIL & GAS INC GeoDate 9/9/82 |
Completion Report Received | 1982-12-21 | |
CO | 1985-04-03 | 193 ZENITH OIL & GAS INC GeoDate 4/3/85 |
Unknown | 1985-04-03 | Issued Date 4/3/85 Expired Date 9/30/85 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Construction Permit Expires | 1985-09-30 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 2992 | 3011 | 0 |
2992 | 3011 | 0 | |
2992 | 3011 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 900 Bbl | 55000 | FRAC: 900 BBL H2O, 55M SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ZENITH OIL & GAS INC | 0.00 | 145.00 | 0 |
1985 | ZENITH OIL & GAS INC | 0.00 | 145.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ZENITH OIL & GAS INC | Brine | 0 | 0 |
1985 | ZENITH OIL & GAS INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
000PL13980 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0011874135 | 2001-11-15 | Production Wells | No Violations | INSPECTION CONDUCTED AT THE RREQUEST OF ERICA FREEMAN. Inspection revealed well is capable of production. The ID sign posted at the storage tank is faded and is not legible. Weather conditions: Sunny & 55 degrees. |
11874135 | 2001-11-15 0:00 | PW | No Violations | |
1469199740 | 2016-07-15 | Production Wells | No Violations | This inspection was conducted as a request from Tiara Simmons. The well was equipped with a pumping unit and motor. The well and pumping unit were covered in vegetation. The well did not indicate signs of recent production and is not currently in production. I observed (2) 100 barrel tanks at separate locations (N 39.95236 W -82.27110 & N 39.94959 W -82.27101). The landowner informed me that water broke in the well several years ago. He also stated that a separator was associated with the well. A separator was not observed during the inspection. The landowner does not receive gas from the well. According to RBDMS the last year for reported commercial production was 1985. I took (8) digital photos during the inspection. Time of inspection: 12:00 PM. Weather: 82*F, Sunny |
PL13980 | PL | No Violations |
For data sources see[9]