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34-121-23736

Well Details

Well ID: 34-121-23736
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Country: United States
State: Ohio
County: Noble
Municipality: Stock Township
Operator Name: NOLL LARRY
Well Pad ID:
Farm/Lease Name: NOLL LARRY
License Status: Domestic Well
License Date: 1990-02-09
Spud Date: 1990-02-23
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1990-03-03
Well Total Depth: 2315.00 ft
Configuration: Vertical
Latitude: 39.760000
Longitude: -81.340000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1989-12-27 Issued Date 12/22/89 Expired Date 12/22/90 Acres 0053450 Tool Type CRAF Proposed Formation BEREA/OH SH Proposed Depth 00000 Proposed Drill Depth 00000
CO 1990-02-09 79 OXFORD OIL CO GeoDate 2/9/90
Oil and Gas 1990-02-09 Issued Date 12/22/89 Expired Date 12/22/90 Acres 0053450 Tool Type RTAF Proposed Formation BEREA/OH SH Proposed Depth 02315 Proposed Drill Depth 02315
Original Spud 1990-02-23 R.L. 2-10-90
Completed 1990-03-03 R.L. 2-10-90
Reached Total Depth 1990-03-03 R.L. 2-10-90
Completion Report Received 1990-09-19 R.L. 2-10-90
CO 1990-09-22 79 OXFORD OIL CO GeoDate 12/27/89
Construction Permit Expires 1990-12-22 R.L. 2-10-90
CO 1995-06-21 5147 NOLL LARRY GeoDate 2/9/90
Record Last Modified 2017-02-15 R.L. 2-10-90

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1935 1937 2
1773 1776 7
2006-09-11 1886 1888 3
1886 1888 3
1773 1776 7
1997-06-29 1773 1776 7
2006-09-11 2201 2208 2
2006-09-11 2174 2178 3
2006-09-11 2044 2054 4

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1667 Bbl 25000 2 STAGE FRAC:WATER/SAND
H2O 0 262 Bbl 1250 ATR 11 BPM @ 1800 PSI, ISI 1200 PSI, BEREA -2ND STAGE.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1989 OXFORD OIL 0.00 0.00 0
1990 OXFORD OIL 1195.00 0.00 105
1991 OXFORD OIL 2171.00 0.00 365
1992 OXFORD OIL 873.00 60.00 365
1993 OXFORD OIL 612.00 40.00 365
1994 OXFORD OIL 165.00 0.00 365
1995 OXFORD OIL 42.00 27.00 146

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1989 OXFORD OIL Brine 0 0
1990 OXFORD OIL Brine 320 105
1991 OXFORD OIL Brine 120 365
1992 OXFORD OIL Brine 0 365
1993 OXFORD OIL Brine 0 365
1994 OXFORD OIL Brine 0 365
1995 OXFORD OIL Brine 25 146

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1027009722 2019-2-20 0:00: PW No Violations 0.50
-1628399716 2019-3-21 0:00: PW No Violations 1.00
-452791228 2019-1-22 0:00: PW No Violations
0000PL7258 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0160057681 2019-01-23 Production Wells No Violations The purpose of my inspection was a follow up to an incident that happened on 1/21/2019 where a Enbridge pipeline had failed and caught fire causing damage to multiple resident dwellings and out buildings. There were multiple locations that were on fire, including several hay bales near the well head. On the day of my inspection I witnessed production equipment included a 100-barrel steel production fluid storage tanks, and vertical separator enclosed within an earthen dike. There was a domestic gas line attached to the flow line near the separator, and the gauge on the separator was leaking at the time of my inspection. The well was equipped with 4.5-inch diameter production casing, 1.5 inch diameter tubing with rods and National pumping unit, there appeared to be another domestic gas line off of the 4.5 inch diameter casing, the 1 inch diameter line was equipped with a tee, it appeared that one side of the tee had provided natural gas for a motor on the pumping unit, there was no longer a motor on the unit, the other side of the tee appeared to have plastic line attached that had been melted. There was a small leak on the 2-inch diameter check valve that was equipped on the tubing. At the time of my inspection all valves were shut.
0452791228 2019-01-22 Production Wells No Violations Accompanied ODNR Inspector Bill Stolarik, reference his report for further details.
0848003928 2005-09-26 Production Wells No Violations No violations noted, well is equipped with pump jack and 1-25bbl tank,I.D. was posted on separator.
1027009722 2019-02-20 Production Wells No Violations On this day, I accompanied ODNR Inspector William Stolarik. Please reference his comments for a detailed report. We are conducting an inspection in regard to the pipeline issue that compromised the well.
1548171641 2019-01-22 Production Wells No Violations On site inspection as a follow up to a pipe line failure that occurred on 01/21/2019 when a 30 inch diameter gas line reportedly owned by a Midstream operator identified as Enbridge failed in close proximity to the well head and the escaping product caught fire. The resulting fire and radiant heat damaged or destroyed multiple structures in the affected area and the said well head along with the pumping unit showed signs of heat exposure from the event. The well was observed to be equipped with a 4.5 inch diameter casing head with 1.900 inch diameter production tubing inserted into the well head. The well is set up to be produced by the means of a pumping unit with a polish rod liner installed into the 1.900 production tubing. The internal seals on the polish rod liner appear to of been compromised by the fire, no drive motor or engine appeared to be present on the pumping unit. Both the casing and tubing well heads are equipped with 2 inch diameter production outlet ports. Installed in the 2 inch diameter outlet ports are 2 inch diameter flow lines that is equipped with both shut off and check valves. The shut off valves are closed and both check valve bodies were leaking around the upper cap area. Opposite of the commercial side of the 4.5 inch diameter well head is the service side that consists of a 2 inch diameter outlet reduced down to a 1 inch diameter sales line with a pressure reducing regulator present inline. The 1 inch diameter plastic flow lines attached to the service side have been burnt off, a 1 inch production valve is present on the service side and is in the closed position. The 4.5 inch diameter casing and surface casing well head section is not visible above ground level. On location in proximity to the well is the production facility that consists of a single 100 barrel steel production tank along with a mechanical separator. The mechanical separator is also leaking gas around the 2 inch diameter production service equipment. No gas sales m
1548962977 2019-01-31 Production Wells No Violations On site inspection as a follow up to a pipe line failure that occurred on 01/21/2019 accompanied on this day by ODNR Inspector Ryan Armstrong along with a representative from Enbridge Pipeline identified as Jacob Smithingell. The well was observed to be equipped with 4.5 diameter production casing and 1.9 diameter production tubing. All production valves were closed. The well head leaks previously noted during on our last inspection on 01/22/2019 have subsided. The production facility was leaking around a pressure gauge on the mechanical separator during our last visit and that gauge has been replaced since our last visit. Inspector Armstrong and myself discussed with Mr. Smithingell the needed repairs to the well head due to heat damage from the fire during the pipeline incident. Mr. Smithingell has indicated that the pipe line company (Enbridge) will sit down with the landowner who owns the well and discuss the needed repairs and work with the landowner to address the damaged well head and equipment. They will contact me after the meeting with an update which is scheduled to take place in the next 7 days.
1550689245 2019-02-20 Production Wells No Violations On site inspection as a follow up to a pipe line failure that occurred on 01/21/2019 accompanied on this day by ODNR Inspector Tom Thomas. Upon inspection the well was observed to be equipped with 4.5 diameter production casing and 1.900 diameter production tubing. There is 2diameter flowlines present attached to the casing and tubing well heads. The flowlines are equipped with both check and shut off valves with the shut off valves in the closed position. The flowlines are joined at the well head into a single steel 2 diameter line that runs to a nearby production facility separator. Present on the separator is a pressure gauge showing 20 pounds pressure on the gauge. The domestic supply is present on the separator. There is a single 100 barrel steel tank present. Also on this day I was informed by Enbridge officials that a local well service company identified as Harmons Well Service is slated to move in on February 25 and make repairs to the well and replace any equipment damaged by the fire.
160057681 2019-1-23 0:00: PW No Violations 0.80
1628399716 2019-03-21 Production Wells No Violations The purpose of my inspection was to follow up on the previous inspection where well had been damaged. On the day of my inspection I witnessed production equipment included a 100-barrel steel production fluid storage tank, vertical separator all enclosed within earthen containment. The production equipment had been re-set and leveled as well as painted and identification was posted on the production fluid storage tank. It appeared that there was a domestic gas hookup from the separator utilizing a little joe regulator. The well was equipped with 4.5-inch diameter production casing, 1.5-inch diameter tubing with rods, a pumping unit with a natural gas motor. There was a new stuffing box, brass liner, and all new valves installed at the well head. The well head and pumping unit had also been re- painted and the pumping unit had been leveled with new timbers installed.
848003928 2005-9-26 0:00: PW No Violations
PL7258 PL No Violations

For data sources see[9]

References