X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-121-23780

Well Details

Well ID: 34-121-23780
Loading map...
Country: United States
State: Ohio
County: Noble
Municipality: Marion Township
Operator Name: G-R CONTRACTING INC
Well Pad ID:
Farm/Lease Name: RUBEL
License Status: Final Restoration
License Date: 2018-03-08
Spud Date: 1990-09-20
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1990-09-26
Well Total Depth: 2241.00 ft
Configuration: Vertical
Latitude: 39.820000
Longitude: -81.320000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1990-09-14 952 G-R CONTRACTING INC GeoDate 9/14/90
Oil and Gas 1990-09-14 Issued Date 9/14/90 Expired Date 9/14/91 Acres 0020000 Tool Type RTA Proposed Formation BEREA/30 FT Proposed Depth 02241 Proposed Drill Depth 02241
Original Spud 1990-09-20
Completed 1990-09-26
Reached Total Depth 1990-09-26
Completion Report Received 1990-12-12
Plugged/Abandoned 2018-02-27
APP 2018-03-08 Proposed Formations:OHIO SHALE, Issued Date:3/8/2018, Expired Date:3/7/2020 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2018-04-18
Construction Permit Expires 2020-03-07

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1866 1882 14
1862 1882 0
1997-06-29 1862 1882 0
1866 1882 14
1862 1882 0
2006-09-11 1978 1982 6
2006-09-11 2138 2147 9

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 0 0 FRAC:WATER/SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1996 G-R CONTRACTING INC 447.00 0.00 365
1997 G-R CONTRACTING INC 389.00 0.00 365
1998 G-R CONTRACTING INC 335.00 0.00 365
2000 G-R CONTRACTING INC 96.00 0.00 365
2001 G-R CONTRACTING INC 399.00 0.00 365
2002 G-R CONTRACTING INC 0.00 0.00 365
2003 G-R CONTRACTING INC 0.00 0.00 365
2004 G-R CONTRACTING INC 174.00 0.00 365
2005 G-R CONTRACTING INC 0.00 0.00 365
2006 G-R CONTRACTING INC 0.00 0.00 365
2007 G-R CONTRACTING INC 2322.00 37.00 365
2008 G-R CONTRACTING INC 0.00 65.00 365
2009 G-R CONTRACTING INC 116.00 14.00 365
2010 G-R CONTRACTING INC 109.00 0.00 365
2011 G-R CONTRACTING INC 106.00 0.00 365
2012 G-R CONTRACTING INC 123.00 0.00 366
2013 G-R CONTRACTING INC 92.00 0.00 365
2014 G-R CONTRACTING INC 73.00 0.00 365
2015 G-R CONTRACTING INC 29.00 0.00 365
2016 G-R CONTRACTING INC 0.00 0.00 365
2017 G-R CONTRACTING INC 90.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1996 G-R CONTRACTING INC Brine 0 365
1997 G-R CONTRACTING INC Brine 0 365
1998 G-R CONTRACTING INC Brine 0 365
2000 G-R CONTRACTING INC Brine 0 365
2001 G-R CONTRACTING INC Brine 0 365
2002 G-R CONTRACTING INC Brine 0 365
2003 G-R CONTRACTING INC Brine 0 365
2004 G-R CONTRACTING INC Brine 0 365
2005 G-R CONTRACTING INC Brine 0 365
2006 G-R CONTRACTING INC Brine 0 365
2007 G-R CONTRACTING INC Brine 0 365
2008 G-R CONTRACTING INC Brine 0 365
2009 G-R CONTRACTING INC Brine 0 365
2010 G-R CONTRACTING INC Brine 0 365
2011 G-R CONTRACTING INC Brine 0 365
2012 G-R CONTRACTING INC Brine 0 366
2013 G-R CONTRACTING INC Brine 0 365
2014 G-R CONTRACTING INC Brine 0 365
2015 G-R CONTRACTING INC Brine 0 365
2016 G-R CONTRACTING INC Brine 0 365
2017 G-R CONTRACTING INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1128248051 2018-2-27 0:00: PB No Violations 6.00
-1253623478 2018-3-1 0:00:0 FR No Violations 1.00
-1928506167 2018-2-22 0:00: PW No Violations 1.00
-627660335 2017-8-21 0:00: PW No Violations 1.00
0000005670 Preliminary Restoration No Violations PASSED Y WITNESSED 9/14/94 INSPECTOR TED DOBBIN DATE 09/1419/94 DATA FROM OLD VAX INFO
0000005671 Preliminary Restoration No Violations PASSED Y WITNESSED 6/16/93 INSPECTOR TED DOBBIN DATE 06/1619/93 DATA FROM OLD VAX INFO
0627660335 2017-08-21 Production Wells No Violations The purpose of my inspection was a status check on a production well. During my inspection the well was equipped with 4.5 inch diameter casing with a tubing head, 1.5 inch diameter tubing, rods, and a pumping unit. The production valves were in the open position. The production equipment consisted of one 100 barrel tank, one vertical separator, and one meter run with a 2 inch diameter line, .1875 inch orifice plate, and chart meter with a chart dated 7/31/17. Identification was posted at the wellhead and on the 100 barrel tank.
1128248051 2018-02-27 Plug / Plug Back No Violations Formations Cementing hooked up to the 4.5 inch diameter casing, circulated the hole clean, and set a 300 foot bottom of surface plug from 278 feet to 578 feet with 60 sacks of class A cement weighing 15.6 pounds per gallon with a yield of 1.18. G-R tripped the 4.5 inch diameter casing up to 125 feet and set a surface plug with 25 sacks of class A cement, 15.6 pounds per gallon, and 1.18 yield. The plug remained at surface.
1253623478 2018-03-01 Final Restoration No Violations The purpose of my inspection was a status check on a final restoration. The wellsite was located within an American Electric Power construction site that consisted of a gravel pad around the wellhead and a gravel road to the well. American Electric Power plans to set a transmission electric pole near the plugged well. The location of the plugged well did not have any erosion issues and there were not any remains or debris left behind from plugging operations.
1520620732 2018-02-26 Plug / Plug Back No Violations G-R Contracting was rigged up on location with their derrick service rig to complete plugging operations. Formation Cementing set up on location and pumped a bottom plug through the 1.5 inch diameter tubing from 2170 feet to 1770 with 30 sacks of class A cement with 1.18 yield. G-R tripped the 1.5 inch diameter tubing out of the hole. Following the plug Appalachian Well Surveys set up on location to bond log the 4.5 inch casing and shoot the casing off in order to retrieve the casing. Appalachian ran a bond log on the 4.5 inch diameter casing and found that the 6.25 inch diameter hole had caved in from 950 feet to 1050 feet in depth creating a 100 percent bond on the 4.5 inch diameter casing. Appalachian shot the casing off at 900 feet in depth and tripped out of hole. G-R attempted to pull up on the 4.5 inch diameter casing but could not do so. Appalachian and G-R reviewed the Bond log again and decided on shooting the casing at 610 feet. Appalachian tripped back in hole with the casing cutter and successfully shot the 4.5 inch diameter casing at 610 feet in depth. G-R tripped one 32 foot joint of casing from the well.
1928506167 2018-02-22 Production Wells No Violations The purpose of my inspection was a status check. During my inspection G-R Contracting was rigged up on location with their derrick service rig. I spoke with Jordan Jones with G-R Contracting and he stated that the well shall be plugged due to an American Electric Power electric transmission line being placed directly over the well. G-R Contracting tripped the tubing out of the hole and ran back in the well open ended preparing to plug. No further action will be taken until a plugging permit is received from ODNRs permitting section.
5670 PL No Violations
5671 PL No Violations

For data sources see[9]

References