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Well ID: 34-169-20897 | Loading map...
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Country: United States | |
State: Ohio | |
County: Wayne | |
Municipality: Wayne Township | |
Operator Name: HARLEY DRILLING & PRODUCING LT | |
Well Pad ID: | |
Farm/Lease Name: LEATHERMAN CLYDE | |
License Status: Producing | |
License Date: 1959-03-04 | |
Spud Date: 1959-08-19 | |
Spud Drilling Contractor: | |
Final Drill Date: 1959-10-06 | |
Well Total Depth: 3380.00 ft | |
Configuration: Vertical | |
Latitude: 40.890000 | |
Longitude: -81.980000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1959-08-19 | |
Completed | 1959-10-06 | |
Reached Total Depth | 1959-10-06 | |
Completion Report Received | 1959-10-22 | |
Change of Owner | 2003-05-21 | Operator changed from 513, DALTON & HANNA CO to 337, HARLEY DRILLING & PRODUCI |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1160575562 | 2003-7-31 0:00: | PW | No Violations | 1.50 |
-1628763453 | 2003-7-30 0:00: | PW | No Violations | 3.50 |
-1709356607 | 2003-7-11 0:00: | PW | No Violations | 1.20 |
-1710170437 | 2004-2-27 0:00: | PW | No Violations | 0.50 |
-238644576 | 2003-8-7 0:00:0 | PW | No Violations | 1.00 |
-393785075 | 2016-11-2 0:00: | PW | No Violations | |
0238644576 | 2003-08-07 | Production Wells | No Violations | clean up complete and area backfilled . |
0372406651 | 2003-07-21 | Production Wells | No Violations | Most all of the contaminated soil has been removed but no clean fill has been put back in its place. Talk to Don Harley on clean up and advised on fill. |
0393785075 | 2016-11-02 | Production Wells | No Violations | Inspected production well on 11/02/2016. The tank battery consists of 2-210 bbl steel tanks, 1-100 bbl steel tank, 1-550 gal plastic tank, 1-vertical separator, and 1-compressor, located within an earthen dike. The tank battery is used by multiple wells (4); well identification is clearly displayed for all wells utilizing it. The well is equipped with a pump jack with an electric motor. Well identification is posted at the wellhead as required. No problems were noted at the time of the inspection. |
0463498712 | 2012-11-28 | Production Wells | No Violations | This is a producing pump jack well. There were no problems noted at the time of the inspection. |
0669835444 | 2018-07-09 | Production Wells | No Violations | Inspected production well on 07/09/2018. The tank battery consists of 2-210 bbl steel tanks, 1-100 bbl steel tank, 1-diesel tank, and 1-vertical separator, located within an earthen dike. The tank battery is used by multiple wells (4); well identification is clearly displayed for all wells utilizing it. The well is equipped with a pump jack with an electric motor. Well identification is posted at the wellhead as required. The well is located ~755 from its RBDMS location. A map showing the location discrepancy, as well as a request for the location to be updated in RBDMS was sent to Gregg Miller and Aaron Lantz (DOGRM Columbus). No other problems were noted at the time of the inspection. |
1060024476 | 2003-07-30 | Production Wells | No Violations | Check this well and found that tank battery has oil inside . The oil is more than it was before the last inspection. I contacted Don and advised that he has a leak which needs corrected.Wait on operator to arrive and begin clean up and also measure between tanks. |
1060611708 | 2003-07-29 | Production Wells | Violations Noted | In Harley Drilling office to meet with Don on clean up and distance between wells.Advise that tank battery needs clean up and that correct I.D. be placed at well and tanks. Set up meeting to measure wells Tueday. |
1160575562 | 2003-07-31 | Production Wells | No Violations | Clean up continues today with dike and well . There was a small amount of oil at the well which needed cleaned up also.The amount was around a gallon or two . I.D. has been posted. |
1433361342 | 2014-08-07 | Production Wells | No Violations | This pumping unit well has no apparent problems at this time. |
1628763453 | 2003-07-30 | Production Wells | No Violations | Met operator on site and began cleanup of tank area. There is oil and brine saturated soil that needs removed and clean fill put back in its place . There has been a new leak which has just occurred Monday and is being cleaned up today.Also measured distance between wells and found that it appears to be 653ft. Between them and is not a violation . I had measured between another well that I thought was this well because the I.D. are not properly posted.I had operator to place the correct signs on the well and tank battery. |
1709356607 | 2003-07-11 | Production Wells | No Violations | No clean up has been done and the letter or phone call to Tom Tugend about the distance violation has not been sent . Don is to have clean up done this next week. |
1710170437 | 2004-02-27 | Production Wells | No Violations | |
1983229547 | 2015-12-02 | Production Wells | No Violations | Inspected production well on 12/02/2015. The tank battery consists of 2-210 bbl steel tanks, 1-100 bbl steel tank, 1-550 gal plastic tank, 1-vertical separator, and 1-compressor located within an earthen dike. The tank battery is used by multiple wells (4); well identification is clearly displayed for all wells utilizing it. The well is equipped with a pump jack with an electric motor. Well identification is posted at the wellhead as required. The well is not located in its RBDMS location. No other problems were noted at the time of the inspection. |
372406651 | 2003-7-21 0:00: | PW | No Violations | 1.50 |
463498712 | 2012-11-28 0:00 | PW | No Violations | |
669835444 | 2018-7-9 0:00:0 | PW | No Violations | |
899315722 | 2020-7-2 0:00:0 | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1060611708 | US-OH-101176 | 2003-08-11 | Well operation causing pollution and contamination |
For data sources see[7]