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Well ID: 34-121-24566 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Marion Township | |
Operator Name: CNX GAS COMPANY LLC | |
Well Pad ID: US-OH-000706 | |
Farm/Lease Name: RESERVE COAL PROPERTIES CO | |
License Status: Not Drilled | |
License Date: 2015-01-06 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 39.830000 | |
Longitude: -81.390000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2015-01-06 | Proposed Formations:UTICA, Issued Date:1/6/2015, Expired Date:1/5/2017 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
Construction Permit Expires | 2017-01-05 | |
Record Last Modified | 2018-11-01 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1920119559 | 2016-08-26 | Casing String Witnessed | No Violations | I am onsite to witness the surface casing remedial cementing operations. A one inch parasite string was inserted in the annulus of the surface casing. The company reported that the tubing sat down at 300 and believed this was the cement top. Forty barrels of cement were pumped through the one inch tubing. While waiting for the cement to gel it was discovered that the wrong cement was delivered and pumped by Allied. The proper cement blend will be utilized for the remainder of the job. |
For data sources see[3]