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Well ID: 34-007-21362 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashtabula | |
Municipality: Orwell Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: BEER ML | |
License Status: Producing | |
License Date: 1987-07-13 | |
Spud Date: 1980-09-19 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-09-25 | |
Well Total Depth: 3662.00 ft | |
Configuration: Vertical | |
Latitude: 41.550000 | |
Longitude: -80.820000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-05-30 | 9 EDC GeoDate 5/30/80 |
Original Spud | 1980-09-19 | |
Completed | 1980-09-25 | |
Reached Total Depth | 1980-09-25 | |
CO | 1987-07-13 | 9 EDC GeoDate 7/13/87 |
Unknown | 1987-07-13 | Issued Date 7/13/87 Expired Date 7/12/88 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Construction Permit Expires | 1988-07-12 | |
Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Change of Owner | 2017-05-01 | Operator changed from 7578, ENERVEST OPERATING LLC, to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2017-05-01 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3572 | 3606 | 12 |
3572 | 3606 | 12 | |
3572 | 3606 | 12 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 85000 Gal | 60000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-525586706 | 2019-8-8 0:00:0 | PW | No Violations | |
-983437976 | 2018-7-23 0:00: | PW | No Violations | |
0983437976 | 2018-07-23 | Production Wells | No Violations | I conducted an inspection on this well. At the time of this inspection, the well was equipped with a plunger lift assembly and the gate valve on the tubing was open. The flow line valve off of the tubing was closed. The tank battery consisted of one 100 BBL tank, one 50 BBL poly tank and a mechanical separator. Valves on the separator were closed. The diked tank battery had legible signage. The lease access was stable. |
For data sources see[9]