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Well ID: 34-153-22641 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: SCHREINER OIL & GAS INC | |
Well Pad ID: | |
Farm/Lease Name: PPG IND | |
License Status: Plugged and Abandoned | |
License Date: 2007-09-06 | |
Spud Date: 1990-03-04 | |
Spud Drilling Contractor: [[P&R INC [PEEK & ROWAN]]] | |
Final Drill Date: 1990-03-09 | |
Well Total Depth: 4109.00 ft | |
Configuration: Vertical | |
Latitude: 40.980000 | |
Longitude: -81.610000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1990-01-30 | Issued Date 1/30/90 Expired Date 1/30/91 Acres 0020000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 04050 Proposed Drill Depth 04050 |
Original Spud | 1990-03-04 | |
Completed | 1990-03-09 | |
Reached Total Depth | 1990-03-09 | |
CO | 1990-03-31 | 3151 SCHREINER OIL & GAS INC GeoDate 1/30/90 |
Completion Report Received | 1990-08-20 | |
Plugged/Abandoned | 2007-07-20 | |
APP | 2007-09-06 | Proposed Formations:CLINTON, Issued Date:9/6/2007, Expired Date:9/5/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Construction Permit Expires | 2008-09-05 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3866 | 3956 | 0 |
3866 | 3956 | 0 | |
2006-09-11 | 3914 | 3987 | 38 |
3914 | 3987 | 38 | |
3866 | 3956 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 82000 Gal | 40000 | FRAC:WATER/SAND/CO2 ASSIST | ||
CO2 | 0 | 20 Tons | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | SCHREINER OIL & GAS INC | 21823.00 | 641.00 | 230 |
1992 | SCHREINER OIL & GAS INC | 8334.00 | 220.00 | 365 |
1993 | SCHREINER OIL & GAS INC | 7596.00 | 184.00 | 365 |
1994 | SCHREINER OIL & GAS INC | 5831.00 | 105.00 | 365 |
1995 | SCHREINER OIL & GAS INC | 4589.00 | 68.00 | 360 |
1996 | SCHREINER OIL & GAS INC | 2304.00 | 0.00 | 365 |
1997 | KISTLER JOHN & RUTH | 1937.00 | 34.00 | 365 |
1998 | KISTLER JOHN & RUTH | 1891.00 | 0.00 | 360 |
1999 | SCHREINER OIL & GAS INC | 1733.00 | 0.00 | 279 |
2000 | SCHREINER OIL & GAS INC | 1514.00 | 0.00 | 160 |
2001 | SCHREINER OIL & GAS INC | 1278.00 | 0.00 | 365 |
2002 | SCHREINER OIL & GAS INC | 325.00 | 0.00 | 226 |
2003 | SCHREINER OIL & GAS INC | 839.00 | 0.00 | 154 |
2004 | SCHREINER OIL & GAS INC | 695.00 | 0.00 | 56 |
2005 | SCHREINER OIL & GAS INC | 1007.00 | 0.00 | 28 |
2006 | SCHREINER OIL & GAS INC | 42.00 | 0.00 | 84 |
2007 | SCHREINER OIL & GAS INC | 0.00 | 0.00 | 0 |
2008 | SCHREINER OIL & GAS INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | SCHREINER OIL & GAS INC | Brine | 1770 | 230 |
1992 | SCHREINER OIL & GAS INC | Brine | 85 | 365 |
1993 | SCHREINER OIL & GAS INC | Brine | 75 | 365 |
1994 | SCHREINER OIL & GAS INC | Brine | 69 | 365 |
1995 | SCHREINER OIL & GAS INC | Brine | 18 | 360 |
1996 | SCHREINER OIL & GAS INC | Brine | 18 | 365 |
1997 | KISTLER JOHN & RUTH | Brine | 0 | 365 |
1998 | KISTLER JOHN & RUTH | Brine | 0 | 360 |
1999 | SCHREINER OIL & GAS INC | Brine | 0 | 279 |
2000 | SCHREINER OIL & GAS INC | Brine | 42 | 160 |
2001 | SCHREINER OIL & GAS INC | Brine | 39 | 365 |
2002 | SCHREINER OIL & GAS INC | Brine | 0 | 226 |
2003 | SCHREINER OIL & GAS INC | Brine | 0 | 154 |
2004 | SCHREINER OIL & GAS INC | Brine | 0 | 56 |
2005 | SCHREINER OIL & GAS INC | Brine | 0 | 28 |
2006 | SCHREINER OIL & GAS INC | Brine | 0 | 84 |
2007 | SCHREINER OIL & GAS INC | Brine | 0 | 0 |
2008 | SCHREINER OIL & GAS INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1296956152 | 2007-8-15 0:00: | PB | No Violations | |
-1974716459 | 2007-8-1 0:00:0 | PB | No Violations | |
-221402784 | 2007-11-8 0:00: | PW | No Violations | |
-453021988 | 2009-6-16 0:00: | PB | No Violations | |
-857256525 | 2008-9-18 0:00: | PB | No Violations | |
-997504890 | 2007-9-21 0:00: | PB | No Violations | |
0000PL4147 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0221402784 | 2007-11-08 | Production Wells | No Violations | Wyldwood Contracting (330-723-1877) is on site removing what is left of the standing dead trees and the previously cut logs. After the trees and stumps have been removed, Wyldwood will grade, lime, seed and mulch the affected area. |
0453021988 | 2009-06-16 | Plug / Plug Back | No Violations | Approximately 1/3 of the impacted area has growing vegetation. The remainder will need to be reseeded, mulched and fertilized. |
0857256525 | 2008-09-18 | Plug / Plug Back | No Violations | The affected area has been cleared, graded, seeded and mulched. The seed has been slow to germinate and will need to be re-applied this fall. This information will be relayed to Mike Schreiner. |
0997504890 | 2007-09-21 | Plug / Plug Back | No Violations | Spill remediation has progressed very slowly. The main area of affected soil and vegetation has been calculated to be 5.1 acres. Salt crystals have started developing as the exposed soils dry out. The soils that are brine saturated enough to grow salt crystals will have to be removed and properly disposed. Mike Schreiner said that he is waiting for a response from his insurance company regarding coverage. |
1002029992 | 2008-12-10 | Plug / Plug Back | No Violations | The site has been graded and seeded but a majority of the seed did not take. The entire area will need to be reseeded as soon as the weather permits. This information has been given to both Mike Schreiner and his insurance adjuster. |
1185279060 | 2007-07-16 | Production Wells | Violations Noted | I received a call from Mike Schreiner reporting brine flow to surface at this well. The 1-1/2 tubing failed just above the tubing head and was spraying brine into the air. The leak was discovered by a PPG crew clearing brush along a fence line. The leak has apparently gone undetected for a while. Approximately 10 acres of vegetation, downslope of the well, has been killed or impacted. Interden Well Service was on site to remove the bad joint of tubing and stop the brine release. Work will then begin on plugging and abandoning the well. |
1189172161 | 2007-08-29 | Plug / Plug Back | No Violations | A cutting crew is on site dropping trees and burning brush. According to Schreiner, they received a temporary agricultural burning permit from Barberton to burn the tops and brush. Approximately 50% of the affected area has been cleared. |
1296956152 | 2007-08-15 | Plug / Plug Back | No Violations | Work on clearing the dead vegetation is progressing very slowly. Numerous trees and brush still needs to be removed before lime can be applied to the affected area. I called and left a voice mail message for Mike Schreiner regarding the pace of the cleanup. |
1749547856 | 2010-05-24 | Plug / Plug Back | No Violations | The brine scald violation has finally been corrected. Vegetation has established across the impacted area and appears to be self-sustaining. |
1843123576 | 2009-11-12 | Plug / Plug Back | No Violations | The impacted area has been reseeded and mulched. The new seed appears to be taking and hopefully will sufficiently cover the area. The site will be checked again in early 2010. |
1850972914 | 2008-06-11 | Plug / Plug Back | No Violations | Met on site with Schreiner Oil & Gas and discussed completing the site remediation. The dead trees have been cut and removed and the area rough graded. The site needs limed, finish graded, seeded and mulched. Schreiner indicated that this work would be completed by the middle of July. |
1974716459 | 2007-08-01 | Plug / Plug Back | No Violations | A work crew is on site to continue removing trees which will be chipped and stockpiled on site. |
PL4147 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1185279060 | US-OH-104900 | 2007-07-24 | Well operation causing pollution and contamination |
For data sources see[9]