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34-155-22451

Well Details

Well ID: 34-155-22451
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Country: United States
State: Ohio
County: Trumbull
Municipality: Hartford Township
Operator Name: VORTEX ENERGY LLC
Well Pad ID:
Farm/Lease Name: TOROK UNIT
License Status: Producing
License Date: 1983-12-13
Spud Date: 1984-01-16
Spud Drilling Contractor: ARMSTRONG DRLG
Final Drill Date: 1984-01-22
Well Total Depth: 5125.00 ft
Configuration: Vertical
Latitude: 41.280000
Longitude: -80.520000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1983-12-13 Issued Date 12/13/83 Expired Date 6/10/84 Acres 0043660 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05125 Proposed Drill Depth 05125
Original Spud 1984-01-14
Completed 1984-01-22
Reached Total Depth 1984-01-22
Construction Permit Expires 1984-06-10
CO 1984-06-15 54 TITAN ENERGY CORP GeoDate 12/13/83
Completion Report Received 1984-09-14
CO 1995-09-20 1639 BASS ENERGY CO INC GeoDate 12/13/83
Change of Owner 2000-10-21 Operator changed from 1639, BASS ENERGY CO INC to 1333, BARR ROBT/dba BIG SKY PET
Change of Owner 2017-06-22 Operator changed from 1333, BIG SKY ENERGY INC to 9841, VORTEX ENERGY LLC
Record Last Modified 2017-06-22

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4890 4975 0
4890 4975 0
2006-09-11 4914 4973 35
4914 4973 35
4890 4975 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 56300 Gal 70000
ACID 0 500 Gal 0 FRAC: H2O,SAND,N2
N2 0 150 Mscf 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 TITAN ENERGY CORP 18887.00 0.00 0
1985 TITAN ENERGY CORP 16147.00 49.00 365
1986 TITAN ENERGY CORP 9593.00 0.00 365
1987 TITAN ENERGY CORP 3333.00 0.00 365
1988 TITAN ENERGY CORP 8560.00 0.00 365
1989 TITAN ENERGY CORP 6134.00 0.00 365
1990 TITAN ENERGY CORP 5399.00 0.00 365
1991 TITAN ENERGY CORP 2461.00 36.00 365
1992 OHIO VALLEY ENERGY SYSTEMS COR 404.00 0.00 119
1993 TITAN ENERGY CORP 3750.00 0.00 365
1994 TITAN ENERGY CORP 1146.00 0.00 365
1996 BASS ENERGY CO INC 1555.00 0.00 90
1997 BASS ENERGY CO INC 5709.00 0.00 365
1998 BASS ENERGY CO INC 1791.00 0.00 365
1999 BASS ENERGY CO INC 0.00 0.00 0
2000 BIG SKY ENERGY INC 506.00 0.00 365
2001 BIG SKY ENERGY INC 0.00 0.00 0
2002 BIG SKY ENERGY INC 0.00 0.00 365
2003 BIG SKY ENERGY INC 0.00 0.00 0
2004 BIG SKY ENERGY INC 6072.00 0.00 365
2005 BIG SKY ENERGY INC 3908.00 0.00 365
2006 BIG SKY ENERGY INC 3219.00 0.00 365
2007 BIG SKY ENERGY INC 2702.00 0.00 365
2008 BIG SKY ENERGY INC 2490.00 0.00 365
2009 BIG SKY ENERGY INC 1738.00 0.00 365
2010 BIG SKY ENERGY INC 2085.00 0.00 365
2011 BIG SKY ENERGY INC 2160.00 0.00 365
2012 BIG SKY ENERGY INC 2740.00 0.00 366
2013 BIG SKY ENERGY INC 2176.00 0.00 365
2014 BIG SKY ENERGY INC 848.00 0.00 365
2016 BIG SKY ENERGY INC 722.00 0.00 98
2017 BIG SKY ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 TITAN ENERGY CORP Brine 0 0
1985 TITAN ENERGY CORP Brine 0 365
1986 TITAN ENERGY CORP Brine 0 365
1987 TITAN ENERGY CORP Brine 0 365
1988 TITAN ENERGY CORP Brine 0 365
1989 TITAN ENERGY CORP Brine 0 365
1990 TITAN ENERGY CORP Brine 0 365
1991 TITAN ENERGY CORP Brine 0 365
1992 OHIO VALLEY ENERGY SYSTEMS COR Brine 100 119
1993 TITAN ENERGY CORP Brine 0 365
1994 TITAN ENERGY CORP Brine 0 365
1996 BASS ENERGY CO INC Brine 0 90
1997 BASS ENERGY CO INC Brine 0 365
1998 BASS ENERGY CO INC Brine 0 365
1999 BASS ENERGY CO INC Brine 0 0
2000 BIG SKY ENERGY INC Brine 0 365
2001 BIG SKY ENERGY INC Brine 0 0
2002 BIG SKY ENERGY INC Brine 0 365
2003 BIG SKY ENERGY INC Brine 0 0
2004 BIG SKY ENERGY INC Brine 0 365
2005 BIG SKY ENERGY INC Brine 0 365
2006 BIG SKY ENERGY INC Brine 0 365
2007 BIG SKY ENERGY INC Brine 0 365
2008 BIG SKY ENERGY INC Brine 0 365
2009 BIG SKY ENERGY INC Brine 0 365
2010 BIG SKY ENERGY INC Brine 0 365
2011 BIG SKY ENERGY INC Brine 0 365
2012 BIG SKY ENERGY INC Brine 0 366
2013 BIG SKY ENERGY INC Brine 0 365
2014 BIG SKY ENERGY INC Brine 0 365
2016 BIG SKY ENERGY INC Brine 0 98
2017 BIG SKY ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-95307018 2014-12-4 0:00: AM No Violations 0.20
0000PL3819 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0095307018 2014-12-04 Administrative Inspection No Violations I performed an administrative inspection for Compliance Notice #1334669823, which has been closed at this time. Operator was granted a stay in reference to Chiefs Order 2014-43.
0210742733 2016-09-06 Production Wells No Violations
0824445816 2004-08-26 Production Wells No Violations no violations .
1334669823 2014-03-04 Production Wells Violations Noted I was on location to check compliance to Chiefs Order 2014-43. My inspection found the well was equipped with a plunger lift unit. The valve leading to the flow line from the well was open. There was a domestic flow line coming off the 4.5 casing. The tank battery consisted of a 100 barrel production tank, a 50 barrel brine tank, and a heat, treated separator. The identification sign was lying on the ground. The dike was completed engulfed with shrubs, weeds, and trees. The heat, treated separator has the proper spacing. The flow line valves leading to the separator were open. There was a production chart inside the separator with no date. The lease road was in stable condition. Photos were taken of all the production equipment. The well was in production which was in non-compliance of Chiefs order #2014-43. The well needs to be shut-in immediately.
1506467305 2016-04-29 Production Wells Violations Noted I conducted this inspection to follow-up on a Temporary Restraining Order issued by the Trumbull

--105 requiring Big Sky Energy Incorporated to suspend all oil and gas operations in the State of Ohio. My inspection found the wellhead equipped with a 1.5 plunger lift system. The gate valve is open and the flow line valve and the casing valve are closed. The well is shut in as required. The domestic tap at the wellhead is open and producing house gas. The well is produces to a horizontal separator and there is currently no gas or oil moving through the separator. The well produces to a tank battery containing one (1) 100 barrel production tank and one (1) 50 barrel brine tank. There is no ID at the tank battery or wellhead. Big Sky Energy will, within 7 days of the issuance of this notice, post the proper ID at the tank battery. This well is shut-in as required by the temporary restraining order issued by the Trumbull County Court of Common Pleas, dated 4/11/2016.

210742733 2016-9-6 0:00:0 PW No Violations 0.70
565856543 2019-5-28 0:00: PW No Violations
824445816 2004-8-26 0:00: PW No Violations
PL3819 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1334669823 US-OH-109623 2015-02-06 Failure to register/obtain or maintain bond/insurance
1506467305 US-OH-114202 2016-06-13 Failure to legibly identify well

For data sources see[9]

References