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Well ID: 34-115-24000 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Meigsville Township | |
Operator Name: SMITH RONALD DBA CHIPCO | |
Well Pad ID: | |
Farm/Lease Name: HOOPER HEIRS | |
License Status: Final Restoration | |
License Date: 2005-03-23 | |
Spud Date: 1987-01-21 | |
Spud Drilling Contractor: PERKINS DRLG | |
Final Drill Date: 1987-01-25 | |
Well Total Depth: 5343.00 ft | |
Configuration: Vertical | |
Latitude: 39.600000 | |
Longitude: -81.720000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1987-01-16 | 471 EAGLE MOUNTAIN ENERGY GeoDate 1/16/87 |
Oil and Gas | 1987-01-16 | Issued Date 1/16/87 Expired Date 1/16/88 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05343 Proposed Drill Depth 05343 |
Original Spud | 1987-01-21 | |
Completed | 1987-01-25 | |
Reached Total Depth | 1987-01-25 | |
Completion Report Received | 1987-02-03 | |
Annular Disposal Well | 1997-02-28 | |
Change of Owner | 2002-03-22 | Operator changed from 471, EAGLE MOUNTAIN ENERGY to 2165, PETRO QUEST INC |
Revocation | 2002-11-30 | |
Change of Owner | 2005-03-01 | Operator changed from 2165, PETRO QUEST INC to 7640, SMITH RONALD DBA CHIPCO |
APP | 2005-03-23 | Proposed Formations:CLINTON, Issued Date:3/23/2005, Expired Date:3/23/2006 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:TAAD, Proposed Well Class: |
Plugged/Abandoned | 2005-03-28 | |
Construction Permit Expires | 2006-03-23 | |
Last Compliance Report | 2013-04-24 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-10-29 | 5122 | 5217 | 42 |
5122 | 5217 | 42 | |
5122 | 5217 | 42 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2500 Bbl | 55000 | FRACTURED WITH 32 TONS OF CARBON DIOXIDE | ||
CO2 | 0 | 32 Tons | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | EAGLE MOUNTAIN ENERGY | 12634.00 | 629.00 | 307 |
1988 | EAGLE MOUNTAIN ENERGY | 21676.00 | 546.00 | 365 |
1989 | SCION ENERGY INC | 13482.00 | 418.00 | 365 |
1990 | EAGLE MOUNTAIN ENERGY | 4238.00 | 338.00 | 365 |
1991 | EAGLE MOUNTAIN ENERGY | 2983.00 | 187.00 | 365 |
1994 | CGAS EXPLORATION | 448.00 | 0.00 | 365 |
2002 | PETRO QUEST INC | 0.00 | 0.00 | 0 |
2003 | PETRO QUEST INC | 0.00 | 0.00 | 0 |
2004 | PETRO QUEST INC | 0.00 | 0.00 | 0 |
2005 | PETRO QUEST INC | 0.00 | 0.00 | 0 |
2009 | PETRO QUEST INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | EAGLE MOUNTAIN ENERGY | Brine | 4882 | 307 |
1988 | EAGLE MOUNTAIN ENERGY | Brine | 6711 | 365 |
1989 | SCION ENERGY INC | Brine | 3611 | 365 |
1990 | EAGLE MOUNTAIN ENERGY | Brine | 3630 | 365 |
1991 | EAGLE MOUNTAIN ENERGY | Brine | 3287 | 365 |
1994 | CGAS EXPLORATION | Brine | 0 | 365 |
2002 | PETRO QUEST INC | Brine | 0 | 0 |
2003 | PETRO QUEST INC | Brine | 0 | 0 |
2004 | PETRO QUEST INC | Brine | 0 | 0 |
2005 | PETRO QUEST INC | Brine | 0 | 0 |
2009 | PETRO QUEST INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000020683 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 10/27/87 INSPECTOR DATE 10/2719/87 DATA FROM OLD VAX INFO | |
0000PL9329 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
1077360638 | 2004-02-20 | Annular Disposal | No Violations | A.D. not being used nor is it hooked up brine is being stored in 100bbl tank.this well also has a domestic hookup to landowners home. |
1112051091 | 2005-03-28 | Annular Disposal | No Violations | Well needs to be removed from annular disposal list due to fact that well was plugged 3/28/05. |
1649799025 | 2007-12-31 | Final Restoration | No Violations | Final restoration work at site satisfactory,pit has been filled in and site restored. |
1999167370 | 2013-04-23 | Annular Disposal | No Violations | Well is not equipped for annular disposal. Landowner stated well is providing only house gas. Identification is for previous company and needs to be corrected to reflect Chipco. I called Chipco to explain issue. CORRECTION: This well inspection was for 22400 not 24000. This well was plugged and abandoned in 2005. |
20683 | PL | No Violations | ||
PL9329 | PL | No Violations |
For data sources see[9]