If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-009-22366 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":39.39,"lon":-81.99,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Athens | |
Municipality: Ames Township | |
Operator Name: PETRO QUEST INC | |
Well Pad ID: | |
Farm/Lease Name: BROWN CLINTON E | |
License Status: Producing | |
License Date: 1981-08-31 | |
Spud Date: 1981-09-15 | |
Spud Drilling Contractor: PLATEAU DRLG | |
Final Drill Date: 1981-09-16 | |
Well Total Depth: 1650.00 ft | |
Configuration: Vertical | |
Latitude: 39.390000 | |
Longitude: -81.990000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-08-31 | 288 S & S OIL CO GeoDate 8/31/81 |
Original Spud | 1981-09-15 | |
Completed | 1981-09-16 | |
Reached Total Depth | 1981-09-16 | |
Completion Report Received | 1982-06-16 | |
CO | 1994-03-11 | 2165 PETRO QUEST INC GeoDate 8/31/81 |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2003-09-17 | 1426 | 1440 | 15 |
1426 | 1440 | 15 | |
1426 | 1440 | 15 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 50000 Gal | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | S & S OIL CO | 294.00 | 0.00 | 365 |
1991 | S & S OIL CO | 214.00 | 0.00 | 365 |
1992 | S & S OIL CO | 215.00 | 68.00 | 365 |
1994 | PETRO QUEST INC | 145.00 | 71.00 | 365 |
1995 | PETRO QUEST INC | 655.00 | 0.00 | 365 |
1997 | PETRO QUEST INC | 413.00 | 0.00 | 365 |
1998 | PETRO QUEST INC | 557.00 | 78.00 | 365 |
1999 | PETRO QUEST INC | 366.00 | 0.00 | 365 |
2000 | PETRO QUEST INC | 167.00 | 0.00 | 365 |
2001 | PETRO QUEST INC | 240.00 | 72.00 | 365 |
2002 | PETRO QUEST INC | 265.00 | 0.00 | 365 |
2003 | PETRO QUEST INC | 192.00 | 0.00 | 365 |
2004 | PETRO QUEST INC | 289.00 | 0.00 | 365 |
2005 | PETRO QUEST INC | 266.00 | 74.00 | 365 |
2006 | PETRO QUEST INC | 308.00 | 0.00 | 365 |
2007 | PETRO QUEST INC | 290.00 | 0.00 | 365 |
2008 | PETRO QUEST INC | 336.00 | 74.00 | 365 |
2009 | PETRO QUEST INC | 294.00 | 0.00 | 365 |
2010 | PETRO QUEST INC | 400.00 | 0.00 | 365 |
2011 | PETRO QUEST INC | 383.00 | 0.00 | 365 |
2012 | PETRO QUEST INC | 343.00 | 106.00 | 366 |
2013 | PETRO QUEST INC | 335.00 | 0.00 | 365 |
2014 | PETRO QUEST INC | 255.00 | 76.00 | 365 |
2015 | PETRO QUEST INC | 399.00 | 0.00 | 365 |
2016 | PETRO QUEST INC | 534.00 | 0.00 | 365 |
2017 | PETRO QUEST INC | 306.00 | 0.00 | 365 |
2018 | PETRO QUEST INC | 356.00 | 77.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | S & S OIL CO | Brine | 20 | 365 |
1991 | S & S OIL CO | Brine | 0 | 365 |
1992 | S & S OIL CO | Brine | 0 | 365 |
1994 | PETRO QUEST INC | Brine | 0 | 365 |
1995 | PETRO QUEST INC | Brine | 0 | 365 |
1997 | PETRO QUEST INC | Brine | 0 | 365 |
1998 | PETRO QUEST INC | Brine | 40 | 365 |
1999 | PETRO QUEST INC | Brine | 0 | 365 |
2000 | PETRO QUEST INC | Brine | 0 | 365 |
2001 | PETRO QUEST INC | Brine | 30 | 365 |
2002 | PETRO QUEST INC | Brine | 0 | 365 |
2003 | PETRO QUEST INC | Brine | 0 | 365 |
2004 | PETRO QUEST INC | Brine | 0 | 365 |
2005 | PETRO QUEST INC | Brine | 0 | 365 |
2006 | PETRO QUEST INC | Brine | 0 | 365 |
2007 | PETRO QUEST INC | Brine | 0 | 365 |
2008 | PETRO QUEST INC | Brine | 0 | 365 |
2009 | PETRO QUEST INC | Brine | 0 | 365 |
2010 | PETRO QUEST INC | Brine | 0 | 365 |
2011 | PETRO QUEST INC | Brine | 0 | 365 |
2012 | PETRO QUEST INC | Brine | 25 | 366 |
2013 | PETRO QUEST INC | Brine | 0 | 365 |
2014 | PETRO QUEST INC | Brine | 70 | 365 |
2015 | PETRO QUEST INC | Brine | 0 | 365 |
2016 | PETRO QUEST INC | Brine | 0 | 365 |
2017 | PETRO QUEST INC | Brine | 0 | 365 |
2018 | PETRO QUEST INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1784839954 | 2013-3-5 0:00:0 | PW | No Violations | 0.50 |
0241638199 | 2007-01-31 | Production Wells | No Violations | There were no violations found at the time of inspection. |
1363025647 | 2013-03-08 | Production Wells | No Violations | Follow up to -1784839954. I witnessed the burried tank being unconnected. The lid was opened and there was roughly 4 of fluid in the bottom of the tank. |
1365427964 | 2013-04-08 | Production Wells | No Violations | Follow up to -1784839954. The tank is still buried, but has been emptied and disconnected. |
1370439777 | 2013-06-05 | Production Wells | No Violations | Follow up to -1784839954. Tank still buried. Company called. |
1380892292 | 2013-10-04 | Production Wells | No Violations | Follow up to -1784839954. The 2100 gallon poly tank has been removed and the dike rebuilt. |
1784839954 | 2013-03-05 | Production Wells | Violations Noted | The well was equipped with a pumping unit and valves on the production string and the tubing were open. The tank battery was equipped with two 100 barrel steel tanks and a seperator. A 2100 gallon poly tank was burried inside the tank battery. The burried tank does not appear to be plumbed directly into the tanks at the surface. A glass sitting tube was plumbed into the burried tank. Tank shall be immediately disconnected and emptied of all fluids. Tank shall be removed. |
241638199 | 2007-1-31 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1784839954 | US-OH-117781 | 2014-04-23 | Unlawful method of storage or disposal of brine or other wastes |
For data sources see[9]