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34-009-22704

Well Details

Well ID: 34-009-22704
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Country: United States
State: Ohio
County: Athens
Municipality: Alexander Township
Operator Name: CARPER WELL SERVICE INC.
Well Pad ID:
Farm/Lease Name: GINSBURG HAZEL (SWIW #2)
License Status: Active Injection
License Date: 2019-11-04
Spud Date: 1982-12-18
Spud Drilling Contractor: JD DRILLING
Final Drill Date: 1982-12-21
Well Total Depth: 3161.00 ft
Configuration: Vertical
Latitude: 39.230000
Longitude: -82.130000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1982-12-06 152 ROYAL PETROLEUM PROP INC GeoDate 12/6/82
Oil and Gas 1982-12-06 Issued Date 12/6/82 Expired Date 6/4/83 Acres 0020000 Tool Type RTF Proposed Formation ORISKANY Proposed Depth 03161 Proposed Drill Depth 03161
Reached Total Depth 1982-12-21 CONVERTED TO SWIW FROM OIL AND GAS. POSSIBLE BRIDGE PLUG IN WELL CONVERT 9-22-84
CO 1983-04-15 152 ROYAL PETROLEUM PROP INC GeoDate 4/15/83
Oil and Gas 1983-04-15 Issued Date 4/15/83 Expired Date 10/12/83 Acres 0020000 Tool Type RTA Proposed Formation OHIO SHALE Proposed Depth 02676 Proposed Drill Depth 02676
Plugged Back 1983-04-19 CONVERTED TO SWIW FROM OIL AND GAS. POSSIBLE BRIDGE PLUG IN WELL CONVERT 9-22-84
Original Spud 1984-09-18 CONVERTED TO SWIW FROM OIL AND GAS. POSSIBLE BRIDGE PLUG IN WELL CONVERT 9-22-84
CO 1984-09-20 54 TITAN ENERGY CORP GeoDate 9/20/84
Conversion to Injector 1984-09-20
Salt Water Injection Well 1984-09-20 Issued Date 9/20/84 Expired Date 3/19/85 Acres 0020000 Tool Type CRAF Proposed Formation BIG LIME Proposed Depth 03161 Proposed Drill Depth 03161
Storage Well 1984-09-20 Issued Date 9/20/84 Expired Date 3/19/85 Acres 0020000 Tool Type CRAF Proposed Formation BIG LIME Proposed Depth 03161 Proposed Drill Depth 03161
Completed 1984-11-07 CONVERTED TO SWIW FROM OIL AND GAS. POSSIBLE BRIDGE PLUG IN WELL CONVERT 9-22-84
Completion Report Received 1985-02-11 CONVERTED TO SWIW FROM OIL AND GAS. POSSIBLE BRIDGE PLUG IN WELL CONVERT 9-22-84
Construction Permit Expires 1985-03-19 CONVERTED TO SWIW FROM OIL AND GAS. POSSIBLE BRIDGE PLUG IN WELL CONVERT 9-22-84
First Injection 1985-07-08 CONVERTED TO SWIW FROM OIL AND GAS. POSSIBLE BRIDGE PLUG IN WELL CONVERT 9-22-84
Annulus Pressure Monitoring Approved 1987-11-17 CONVERTED TO SWIW FROM OIL AND GAS. POSSIBLE BRIDGE PLUG IN WELL CONVERT 9-22-84
Change of Owner 1997-12-18 Operator changed from 54, TITAN ENERGY CORP to 4540, PEOPLES PETROLEUM CORP.
Last Compliance Report 1998-12-17 CONVERTED TO SWIW FROM OIL AND GAS. POSSIBLE BRIDGE PLUG IN WELL CONVERT 9-22-84
Change of Owner 2001-02-23 Operator changed from 4540, PEOPLES PETROLEUM CORP. to 3133, PETROEL
Change of Owner 2001-06-25 Operator changed from 3133, PETROEL to 7007, CARPER WELL SERVICE
Record Last Modified 2017-02-15 CONVERTED TO SWIW FROM OIL AND GAS. POSSIBLE BRIDGE PLUG IN WELL CONVERT 9-22-84

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-04-27 2950 2980 1
2000-04-27 3039 3044 4
2950 2980 1
3039 3044 4
2950 2980 1

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
GEL 0 600 Bbl 30000 GELLED HYDROFRACTURE
GEL 0 1100 Bbl 32000 GELLED HYDROFRACTURE
H2O 0 1100 Bbl 32000 B-1M

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1025149170 2013-6-5 0:00:0 SW No Violations 1.00
-1058601064 2013-7-10 0:00: SW No Violations 0.70
-1095027798 2016-2-1 0:00:0 SW No Violations 0.50
-1116558229 2012-1-5 0:00:0 SW No Violations
-1118637362 2020-2-20 0:00: SW No Violations 4.00
-1178382363 2006-4-21 0:00: SW No Violations
-1194499994 2019-10-23 0:00 SW No Violations 3.20
-1202177929 2011-12-30 0:00 SW No Violations 1.50
-1214157965 2015-8-12 0:00: SW No Violations 6.50
-1234106812 2003-3-17 0:00: SW No Violations
-1240877622 2017-11-16 0:00 SW No Violations 4.00
-1243476525 2018-10-29 0:00 SW No Violations 3.00
-1258498324 2011-12-30 0:00 SW No Violations 1.50
-1297685562 2012-2-10 0:00: SW No Violations
-1314071047 2012-3-21 0:00: SW No Violations
-1327803523 2012-11-14 0:00 SW No Violations 5.00
-1386743778 2013-9-19 0:00: SW No Violations 1.00
-1413909378 2020-5-28 0:00: SC No Violations 1.00
-1445266752 2019-1-14 0:00: SW No Violations 1.70
-1455997141 2020-6-18 0:00: SC No Violations 10.30
-1479905247 2019-10-2 0:00: SW No Violations 8.00
-1511727036 2020-6-11 0:00: SC No Violations 2.00
-1519823646 2009-3-12 0:00: SW No Violations
-1565153251 2004-3-10 0:00: SW No Violations
-1614916539 2006-10-19 0:00 SW No Violations
-1647439260 2013-11-21 0:00 SW No Violations 1.50
-1649199664 2006-10-23 0:00 SW No Violations
-168851628 2013-6-4 0:00:0 SW No Violations 1.00
-1718896141 2012-11-15 0:00 SW No Violations 8.00
-1774366702 2020-6-16 0:00: SC No Violations 4.90
-1808822934 2019-11-27 0:00 SC No Violations 2.00
-1810284641 2015-10-19 0:00 SW No Violations 0.50
-1827357313 2012-3-14 0:00: SW No Violations 3.00
-1847380278 2006-12-15 0:00 SW No Violations
-1871237260 2006-4-4 0:00:0 SW No Violations
-1886897126 2017-2-14 0:00: SW No Violations 2.00
-1911748186 2020-6-9 0:00:0 SC No Violations 6.50
-1928223676 2012-6-13 0:00: SC No Violations
-1941781500 2013-5-21 0:00: SW No Violations 2.50
-1947677268 2012-2-10 0:00: SW No Violations 1.50
-1975458245 2005-5-9 0:00:0 SW No Violations
-1986797844 2014-1-27 0:00: SW No Violations 2.50
-1989508424 2008-10-3 0:00: SW No Violations
-1993940341 2012-3-22 0:00: SW No Violations
-2017950731 2020-6-12 0:00: SC No Violations 5.70
-2103432780 2019-2-28 0:00: SW No Violations 2.50
-2104271922 2019-10-3 0:00: SW No Violations 3.90
-211357104 2015-6-10 0:00: SW No Violations 1.00
-221408764 2017-2-14 0:00: SW No Violations 1.00
-275312583 2013-5-9 0:00:0 SW No Violations 3.50
-276695570 2012-6-28 0:00: SW No Violations
-325960936 2001-5-31 0:00: SW No Violations
-331940231 2020-6-5 0:00:0 SC No Violations 4.00
-338182091 2004-8-17 0:00: SW No Violations
-367176123 2013-4-9 0:00:0 SW No Violations 2.50
-36830505 2006-8-14 0:00: SW No Violations
-387670436 2010-11-17 0:00 SW No Violations 1.00
-410095649 2002-3-7 0:00:0 SW No Violations
-425522935 2017-7-19 0:00: SW No Violations 0.70
-440310312 2012-1-5 0:00:0 SW No Violations
-496614638 2013-9-30 0:00: SW No Violations 4.00
-525558180 2019-9-26 0:00: SW No Violations 3.10
-564290163 2003-5-8 0:00:0 SW No Violations
-580104805 2008-6-17 0:00: SW No Violations
-590782139 2000-12-14 0:00 SW No Violations
-599725272 2009-2-23 0:00: SW No Violations
-624201999 2015-1-28 0:00: SW No Violations 1.00
-644350372 2014-2-26 0:00: SW No Violations 1.20
-652143338 2017-3-3 0:00:0 SW No Violations
-701143904 2019-10-1 0:00: SW No Violations 8.20
-708413589 2013-11-21 0:00 SW No Violations 1.50
-852014890 2002-1-22 0:00: SW No Violations
-872106910 2017-3-13 0:00: SW No Violations 2.30
-876332260 2017-4-20 0:00: SW No Violations 2.00
-88373296 2005-10-4 0:00: SW No Violations
-913076490 2003-9-18 0:00: SW No Violations
-929186419 2012-1-25 0:00: SW No Violations
-932934228 2020-2-24 0:00: SW No Violations 4.00
-955454451 2012-4-2 0:00:0 SW No Violations
-967967723 2007-9-10 0:00: SW No Violations
-990366653 2008-2-27 0:00: SW No Violations
0000001250 2002-07-30 Salt Water Injection Well No Violations Injection pressure on well, annulus side 10 lbs, injection side 20 lbs. There are some filters by pump that need to be hauled out and removed from site. Need to add some pressure on annulus side of well.
0000UIC240 1987-06-03 Salt Water Injection Well No Violations 1501:9-3-07(E)(F)
0000UIC325 1987-09-14 Salt Water Injection Well No Violations 1501:9-3-07 (E)(F)
0000UIC330 1987-03-09 Salt Water Injection Well No Violations ACTION Legal 1501:9-3-07 (E)(F) Memo to Ralph M.
001269i209 2000-12-14 Salt Water Injection Well Violations Noted THIS WELL IS IDLE AND INCAPABLE OF INJECTING BRINE . THIS IS NO PRESSURE ON THE INJEC. OR ANNULUS OF WELL , WEEDS ARE GROWING UP IN THE STORAGE PIT AREA . POOR EQUIPMENT AT SITE , TALKED TO LEO ALTIER , HE SAID WELL WAS GOING TO SOLD AT THE SHERIFFS OFFICE IN ATHENS CO. ON 12/13/2000 AT 10:00AM .
001269i707 2002-01-22 Salt Water Injection Well Violations Noted An inspection of the well revealed that the pressure on the injection and annulus stillthe same, 85 lbs. Last inspection both sides where 40 lbs. Need a mini test done on this well. John Puterbaugh, also on site.
001269i854 2002-03-07 Salt Water Injection Well Violations Noted An inspection of the well revealed some oily soil around a storage tank and below the storage impoudment, and a bare area below the well. NEED TO CLEAN UP ALL OILY SOIL AROUND TANK, AND STORAGE IMPOUNDMENT. SEED , MULCH, AND LIME BARE AREA BELOW WELL, ON WELL SITE.
001269i984 2002-04-22 Salt Water Injection Well No Violations Follow-up on NOV, In-Compliance.
0036830505 2006-08-14 Salt Water Injection Well No Violations No action has been taken to remedy violation.
0036892046 2013-02-27 Salt Water Injection Well No Violations Truck delivery at time of inspection. Carper well service, UIC-161. Good manifest, 125 bbl coming from CI McGowan Shattuck Pad 33.
0038099222 2011-08-03 Salt Water Injection Well No Violations No violations at this time.
005609i205 2001-05-31 Salt Water Injection Well Violations Noted An inspection revealed the 1/4 valve at the well on the injection side is in non working condition , the valve needs to be replaced.
005609i245 2001-07-12 Salt Water Injection Well No Violations Folloe - up on N.O.V. , Non - Compliance , 1/4 valve has not been replaced or repaired on the injection side of the line at the well head. Also there is some oily soil that needs cleaned up below storage impoundment.
0059773602 2012-06-28 Salt Water Injection Well No Violations Witnessed and assisted with the sampling of brine from the open pit.
0088373296 2005-10-04 Salt Water Injection Well No Violations No action was taken to test the well.
0108858783 2008-06-27 Salt Water Injection Well No Violations The well failed a pressure test.
01269i1088 2002-06-03 Salt Water Injection Well No Violations Checked injection well, no violations.
01269i1413 2002-10-01 Salt Water Injection Well No Violations No violations.
01269i1524 2002-11-13 Salt Water Injection Well No Violations No violations at this time.
0137993657 2017-12-04 Salt Water Injection Well No Violations My inspection revealed the well has a legible and accurate identification. This satisfies the compliance notice.
0156246569 2012-08-02 Salt Water Injection Well No Violations The gauge was too tight to remove, even with a back-up. When I attempted to remove the gauge from the 1/4 valve to check the annular space between the 2 tubing and the injection tubing I noticed it too was especially tight. In an attempt to apply enough pressure to remove the gauge I broke the 1/4 nipple at the point where it threads into the bull plug reducer. A 2 ball valve was closed behind the broken nipple so no pressurized fluids escaped the well. I called the company and they will be replacing the equipment tomorrow.
0168851628 2013-06-04 Salt Water Injection Well No Violations Unable to remove company gauge to check injection tubing pressure.
0211357104 2015-06-10 Salt Water Injection Well No Violations No noted violations
0212813321 2009-02-18 Salt Water Injection Well No Violations The pit was found completely full. Notified operator via telephone.
0221408764 2017-02-14 Salt Water Injection Well No Violations Identification faded but legible at the unloading pad. Identification is completely blank at the wellhead. Identification tag at the wellhead will be filled out completely and legibly.
0247974618 2018-07-20 Salt Water Injection Well No Violations My inspection today was to witness the injection pump in operation. I witnessed the pump in operation. I check the injection tubing and the annulus pressure. The containment dike was down approximately 16 inches from the top of the containment dike.
0275312583 2013-05-09 Salt Water Injection Well No Violations Inspected injection tubing pressure, annulus pressure, containment pit, injection pump, and unloading pad. Injection operations are shut down by Carper Well Service to allow safe replacement of injection line fittings.
0276695570 2012-06-28 Salt Water Injection Well No Violations Water samples were taken from a Brine Tanker, BD Oil Gathering Corporation. UIC # 306. (Tanker had 143 barrels of produced water from Wilhelm Water tank Lease # 0004, Doddridge County West Virginia. Produced water was pulled from a 210 barrel tank.) Information taken from the Tanker log sheet. Took water samples from the concrete pit. Coordinated with ODNR Lab for pickup of samples in Marietta. Andy Thomas MRI 2 and Josh Garland MRI 2 assisted with the sampling.
0325960936 2001-05-31 Salt Water Injection Well Violations Noted FOLLOW UP TO NOV # 5609i205 An inspection revealed the 1/4 valve at the well on the injection side is in non working condition , the valve needs to be replaced.
0338182091 2004-08-17 Salt Water Injection Well No Violations No violations at this time.
0367176123 2013-04-09 Salt Water Injection Well No Violations Inspected containment pit, injection pressure and annulus pressure. Good identification on well. Updated GPS locations for well, lease road and containment pit (coordinates recorded in tank Lat and Long.)
0384159073 2018-07-10 Salt Water Injection Well No Violations Compliance Notice # 1529591563 follow up inspection. The identification at the well and unloading pad have not been corrected, they still list the wrong API number. The injection pump is not on location. Inspected the containment pit, injection pressure and annulus pressure. The containment pit level is 10 inches from the top. The injection tubing master valve is closed.
0387670436 2010-11-17 Salt Water Injection Well No Violations Inspection this day found pump running, tubing has 20#, 0# on annulus. Water storage area/dike full but pump is running, should be lower. Good IDs.
0410095649 2002-03-07 Salt Water Injection Well Violations Noted FOLLOW UP TO NOV # 1269i854 An inspection of the well revealed some oily soil around a storage tank and below the storage impoudment, and a bare area below the well. NEED TO CLEAN UP ALL OILY SOIL AROUND TANK, AND STORAGE IMPOUNDMENT. SEED , MULCH, AND LIME BARE AREA BELOW WELL, ON
0425522935 2017-07-19 Salt Water Injection Well No Violations I inspected the unloading pad, containment dike, annulus pressure and injection pressure. The fluid level in the containment dike was approximately 38 inches down from the top of the dike. The annulus pressure was 54 PSI, the injection tubing pressure was 48 PSI.
0440310312 2012-01-05 Salt Water Injection Well No Violations Met Josh Garland at well site, checked injection and annulus pressures on well. 1/4 nipple needs replaced on injection side of well.
0496614638 2013-09-30 Salt Water Injection Well No Violations Inspected unloading pad, containment pit, injection pump, injection line, annulus pressure and injection pressure. There were no trucks on site during my inspection.
0558786308 2014-07-03 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, annulus pressure, and injection pressure. Identification is posted at the unloading pad and the well. Witnessed unloading of a Carper Well Brine Truck UIC # 25-161. Checked the brine hauler log sheet.
0564290163 2003-05-08 Salt Water Injection Well No Violations FOLLOW UP TO NOV # 2113127346 An inspection of the well site revealed a ditch cut across the lease rd., no way of entering and unloading brine for disposal. Well appears to be idle at this time. A M.I.T. test needs to be done on this well also. CALLED MR. CARPER ABOUT VIOLATIONS HE
0566599901 2006-07-14 Salt Water Injection Well No Violations No action has been taken to comply with the Chiefs Order. The fluid level in the pit was approximately 1 1/2 feet from the top.
0580104805 2008-06-17 Salt Water Injection Well No Violations Witnessed installation of the packer and tubing.
0590782139 2000-12-14 Salt Water Injection Well Violations Noted FOLLOW UP TO NOV # 1269i209 THIS WELL IS IDLE AND INCAPABLE OF INJECTING BRINE . THIS IS NO PRESSURE ON THE INJEC. OR ANNULUS OF WELL , WEEDS ARE GROWING UP IN THE STORAGE PIT AREA . POOR EQUIPMENT AT SITE , TALKED TO LEO ALTIER , HE SAID WELL WAS GOING TO SOLD AT THE SHERIFFS OF
0599725272 2009-02-23 Salt Water Injection Well No Violations The pit was pumped down.
0624201999 2015-01-28 Salt Water Injection Well No Violations No noted violations. 2796 bbls recorded so far this year with 25 trucks.
0631574685 2019-02-11 Salt Water Injection Well Violations Noted The Division has not received the 4th quarter brine disposal fees for 2018. Please forward disposal fees and sheets to the Division by 3/12/2019.
0644350372 2014-02-26 Salt Water Injection Well No Violations No noted violations.
0652143338 2017-03-03 Salt Water Injection Well No Violations Identification sign at wellhead still not filled in.
0652212545 2008-06-10 Salt Water Injection Well No Violations Rig and bulldozer were onsite. 1 1/2 inch tubing was on the trailer.
0693552892 2005-09-16 Salt Water Injection Well No Violations Well needs tested.
0706327766 2008-06-30 Salt Water Injection Well No Violations The well passed a pressure test.
0708413589 2013-11-21 Salt Water Injection Well No Violations Accompanied Inspector Josh Garland on this inspection. Site is in good order. Spoke with company man on site. No pollution or contamination observed.
0716761238 2013-10-29 Salt Water Injection Well No Violations Inspected unloading pad, containment pit, injection pump, injection line, annulus pressure, and injection pressure. Identification is posted at the wellhead and the unloading pad.
0761390138 2011-12-20 Salt Water Injection Well Violations Noted The pump was not running at the time of inspection. The injection pressure was 10 PSI. I was unable to inspect the pressure on annulus because 1/4 needle valve was corroded and unable to accept the gauge. I spoke with the pump house operator and asked to have valve replaced by 12/21/11.
0787446481 2006-05-17 Salt Water Injection Well No Violations Conditions are the same. No evidence of recent activity.
0843845335 2012-06-28 Salt Water Injection Well No Violations Josh Garland MRI 2 Inspected injection well injection tubing pressure and annulus pressure while water sampling was ongoing.
0852014890 2002-01-22 Salt Water Injection Well Violations Noted FOLLOW UP TO NOV # 1269i707 An inspection of the well revealed that the pressure on the injection and annulus stillthe same, 85 lbs. Last inspection both sides where 40 lbs. Need a mini test done on this well. John Puterbaugh, also on site.
0868535672 2006-04-27 Salt Water Injection Well No Violations Took water sample from frac tank. Prepared sample for shipment.
0872106910 2017-03-13 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure and annulus pressure. Identification is posted at the well and unloading pad. The pit level is at 4.5 feet from the top. The injection tubing master valve and injection line valve are closed. A rebuilt injection pump has been installed.
0876332260 2017-04-20 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure and annulus pressure. Identification is posted at the unloading pad and the wellhead. The containment pit level is at 40 inches from the top of the containment.
0882152013 2008-12-03 Salt Water Injection Well No Violations There were no violations at the time of inspection.
0913076490 2003-09-18 Salt Water Injection Well No Violations No violations at the time of inspection.
0914182433 2004-02-11 Salt Water Injection Well No Violations No violations at the time of inspection.
0924835606 2003-04-22 Salt Water Injection Well No Violations No violations, county has dug a ditch across the lease rd., at this time there is no way of hauling brine into this site.
0929186419 2012-01-25 Salt Water Injection Well Violations Noted Follow-up inspection revealed 1/4 valve has not been replaced on injection side and is still plugged off. Notified pumper of violation. 1/4 valve needs replaced. Water pump running at time of inspection, checked injection pressure at water pump. Josh Garland Athens County Inspector present at inspection.
0937334548 2019-04-18 Salt Water Injection Well No Violations Inspection with ODNR DOGRM UIC Supervisor. Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure and annulus pressure. Identification is posted.
0955454451 2012-04-02 Salt Water Injection Well No Violations Opened 4 1/2 annulus and released pressure. 2 7/8 annulus dropped at the same rate. Left 4 1/2 annulus valve open and pressured up the 2 7/8 annulus, both annulus spaces have communication. Put gauge on the 8 5/8 annulus gauge read 590 psi. Closed 4 1/2 annulus and tested to 310 psi for 15 minutes no loss. 1 1/2 injection tubing was pressurized with 500 psi. Contacted Tom Tomastik Underground Injection Control Geologist. Tom said to monitor the well at this time. There is no evidence of communication out side of the 4 1/2 casing.
0967967723 2007-09-10 Salt Water Injection Well No Violations No action has been taken to plug or operate the well.
0976706387 2017-12-01 Salt Water Injection Well No Violations My inspection revealed the well was not in compliance. I issued a compliance notice for identification not being legible. I contacted Aaron Mace with well owner Carper Well Service. Aaron told me the identification would be on the well by 12.3.17.
0988178787 2008-09-30 Salt Water Injection Well No Violations No violations were found at the time of inspection.
0990366653 2008-02-27 Salt Water Injection Well No Violations Service rig was on the well.
1016606269 2018-02-07 Salt Water Injection Well No Violations My inspection revealed the salt water injection well consists of a open pit that is divided into 3 sections. The fluid in the pit was approximately 20 inches down from the top of the pit. The injection pump and electric motor are present. The injection tubing feeding the well was in the off position. The well had a legible identification. The last time the operator of the well reported injecting fluid was in the first quarter of 2016. New pictures were taken during my inspection.
1025149170 2013-06-05 Salt Water Injection Well No Violations Met the company well supervisor and checked pressures on the injection tubing and annular space. No violations at well or pits. Year to date brine and truck totals reviewed.
1032961619 2016-06-14 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection line, injection pressure and annulus pressure. Identification posted. The injection pump is not on site. The pit fluid level is 1.5 from the top.
1045144359 2003-02-06 Salt Water Injection Well No Violations No violations at this time.
1058601064 2013-07-10 Salt Water Injection Well No Violations Dike is in good shape and unloading pad is good shape.
1073326304 2003-07-16 Salt Water Injection Well No Violations No violations at the time of inspection.
1081069386 2013-04-17 Salt Water Injection Well No Violations Inspected unloading pad, containment pit, injection pump, injection pressure and annulus pressure. While on site a Carper Well Service truck arrived and unloaded brine from Grenadier leases Sizemore and Kuhn. Located in Wetzel County, West Virginia. I collected a brine sample from the Carper truck.
1081945350 2004-04-14 Salt Water Injection Well No Violations No violations at the time of inspection.
1083856599 2004-05-05 Salt Water Injection Well No Violations No violations at the time of inspection.
108858783 2008-6-27 0:00: SW No Violations
1089895241 2004-07-15 Salt Water Injection Well No Violations Fluid level, in the pit, approx. 1 1/2 feet below the top. Slight vacuum on tubing.
1090208574 2004-06-17 Salt Water Injection Well No Violations No violations at the time of inspection.
1093501225 2019-9-11 0:00: SW No Violations 8.00
1095027798 2016-02-01 Salt Water Injection Well No Violations Review of site with inspector Matt Fulk. The pump has been removed, the site is not in operation.
1105062582 2019-04-16 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure and annulus pressure. The access road chain has been removed. The pit fluid level is 30 inches from the top. The injection tubing valves are open. The injection tubing master valve is open. I called Aaron Mace to schedule an annulus test. Aaron stated that he will have to talk to his management. I asked him if they removed the chain on the access road. He replied no they did not.
1106058474 2005-01-12 Salt Water Injection Well No Violations The pit appears to have been recently pumped down. The fluid level is 1.5 ft from the top.
1116558229 2012-01-05 Salt Water Injection Well Violations Noted Met with Dan Goins to review history of this well. Valve on injection was inoperable. Annulus had zero psi. functioning valves shall be put into place on injection tubing. Mini test will be performed in the near future to ensure Mechanical Integrity.
1145218342 2006-04-05 Salt Water Injection Well No Violations The fluid level was about a foot below the top of the pit.

The well needs a MIT. Suspension order was issued 4/18/06.

1178382363 2006-04-21 Salt Water Injection Well No Violations Accompanied Joe Hoerst, who took a sample of the pit water.
1184529678 2007-07-13 Salt Water Injection Well No Violations No action has been taken since last inspection.
1184535131 2007-06-12 Salt Water Injection Well No Violations No action has been taken since last inspection. Accompanied by Joe Hoerst.
1184898863 2007-04-12 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1202177929 2011-12-30 Salt Water Injection Well No Violations New needle valve had been installed on the annulus.
1208853921 2014-09-22 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, annulus pressure and injection pressure. Identification is posted at the well and on the building. Checked brine logs on trucks unloading on the pad. Collected a brine sample from a Hall Drilling truck UIC # 25-361. 130 barrels from 34-111-2-4405 Hercher 1-H. The Halls truck was labeled with Brine and 25-361. The truck (license # BA525381) and Tanker trailer (license # C258499) did not have a company phone number label. I gave the driver a copy of the brine hauler requirements. The driver called and told their office about the requirement.
1214157965 2015-08-12 Salt Water Injection Well No Violations Inspected the containment pit, injection pump, injection line, injection pressure, annulus pressure and unloading pad. Checked brine truck unloading on the pad, reviewed brine hauling records, collected as brine sample to take to the ODNR lab.
1232876203 2013-03-21 Salt Water Injection Well No Violations Inspected injection pressure and annulus pressure at wellhead. Inspected the unloading pad, containment pit, injection pump and grounds around the containment pit. Collected water sample from injection line between the filter and the injection pump. Water sample was taken to ODNR /DOGRM Lab in Cambridge.
1234106812 2003-03-17 Salt Water Injection Well No Violations No violations at this time.
1240877622 2017-11-16 Salt Water Injection Well No Violations My inspection revealed the salt water injection well is currently not being used. The pit had approximately 18 inches of freeboard space. The annulus had 28 psi and the injection tubing had 18 psi. The identification sticker was not legible. I contacted Carper Well Service and requested they update the information on the identification sticker. They agreed and said they would contact me when the identification was corrected.
1243476525 2018-10-29 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure and annulus pressure. Identification is posted. The containment pit level is 38 inches from the top. The injection line valve and the injection tubing master valve are open.
1250 2002-7-30 0:00: SW No Violations
1251072283 2011-11-29 Salt Water Injection Well No Violations Company gauges had seized up and I was unable to remove them for the test. Companys gauges read 385 psi on annulus and 30 psi on injection. The power had just gone out there at the well and the operator was concerned with getting the power back online. I will return within a couple of days to perform the test again and have the operator remove the company gauges.
1258498324 2011-12-30 Salt Water Injection Well No Violations The injection side and annulus were tested while the pump was off and both registered 0 PSI. The pump was turned on and the injection side and annulus were tested again. Once again they both read 0 PSI. A company pressure gauge located at the pump read 350 psi so I believe there is a malfunction with my gauge.
1259233078 2020-3-3 0:00:0 SW No Violations 2.00
1269i1088 2002-6-3 0:00:0 SW No Violations
1269i1413 2002-10-1 0:00: SW No Violations
1269i1524 2002-11-13 0:00 SW No Violations
1269i209 2000-12-14 0:00 SW No Violations
1269i707 2002-1-22 0:00: SW No Violations
1269i854 2002-3-7 0:00:0 SW No Violations
1269i984 2002-4-22 0:00: SW No Violations
1280422291 2012-03-20 Salt Water Injection Well No Violations Meet with Dylan Harlow. 4 1/2 inch annulus and the 2 7/8 inch annulus have communication. Both have 250 psi on them. A small brine seep was located down slope from the unloading pad. In an effort to determine the source of the brine green dye was mixed with fresh water and poured down the unloading pad drain. No dye was observed at the seep location.
1281370976 2012-02-15 Salt Water Injection Well No Violations Checked unloading pad and storage area with Manager Rocky King, may need gravel and water breaks on lease road in spring.
1291447160 2020-4-10 0:00: SW No Violations 4.00
1297685562 2012-02-10 Salt Water Injection Well No Violations Follow-up on Compliance Notice, In-Compliance.
1314071047 2012-03-21 Salt Water Injection Well No Violations Inspected well and storage area with Inspector Dan Goins. We discussed the unloading pad.
1327803523 2012-11-14 Salt Water Injection Well No Violations Collected water sample from a BD Oil Gathering truck. UIC # 306. Water hauled from Ergon Water tank. Washington County Ohio. Lease # 0009. Accompanied by Morgan Button MRI2. Took samples to Jackson Office for shipment to ODNR Lab in Cambridge.
1340897308 2012-06-28 Salt Water Injection Well No Violations Accompanied Jon Scott and Andy Thomas on water sampling inspection. Water samples were taken from the storage pits as well as UIC brine truck #306 which happened to be off loading at the time. Injection pressures and annular pressures were also tested at
1344989843 2020-6-29 0:00: SC No Violations 1.50
1348093088 2012-09-19 Salt Water Injection Well No Violations Inspected site at request of Chief Simmers and inspection revealed that well was in operation and B&D Oil Gathering had tanker truck on unloading pad during inspection it was noted that unloading pad had been recently replaced and new lines going to containment pit has been replaced recently and area around facility has been mowed and area was clear of trash and other debris and several photos were taken of site and will be placed into well file.
1348099328 2012-09-19 Salt Water Injection Well No Violations Met David Ball, UIC inspector, to check the injection well, pits and plumbing from the pits to the well. SI Pressure on injection tubing measured 100 psi, and 150 on annular spacing between the injection tubing and the intermediate 4-1/2-inch csg, and between the 4-1/2 inch csg and 7-inch csg. David wants to replace the pipe between the pits and well and add 1/4-inch nipples on three measuring ports on the injection well tree and a 2-inch plug on a closed port also on the tree.
1348146093 2012-09-19 Salt Water Injection Well No Violations Inspected by request of Robert Worstall. Accompanied Dave Ball on inspection of the facilities and the well. The flow meter was not functioning at the time of inspection, but the operator was able to provide records that showed a total of 91,936 barrels had been received this year. B & D was unloading at the time of the inspection.
1348241852 2012-09-21 Salt Water Injection Well No Violations The line from the pump to the well had been replaced. The identification was corrected. The treatment for the soil was due to arrive early next week.
1351103313 2012-10-22 Salt Water Injection Well No Violations Salt water injection pump was in operation during inspection. Inspected the concrete pit, pump, injection line and unloading pad. No leaks were observed during inspection. The inline flow meter is broken. Brine hauling records were reviewed from the company ledger book.
1351337753 2013-02-06 Salt Water Injection Well No Violations Inspected injection pressure and annulus pressure. Inspected unloading pad and containment pit. Ground was snow covered and showed no signs of contamination. Witnessed Hunter Disposal Truck (UIC 387) unload brine while parked on the unloading pad. I collected a water sample from the truck. I transported the water sample to Jackson office. I sent the water sample to the Cambridge lab.
1354646818 2012-12-04 Salt Water Injection Well No Violations Accompanied Inspector Jon Scott on inspection. Reviewed annular and injection pressures. Because of the low pressure on the annular space between the injection tubing and the casing Jon Scott called for a Mechanical Integrity Test.
1354768478 2012-12-04 Salt Water Injection Well Violations Noted Inspected the surface facility and checked the injection pressure and the annulus pressure. Annulus pressure was zero. I called Dylan Harlow and told him that they need to test the annulus. Injection pumps were shut down until the test could be conducted.
1362694336 2013-02-28 Salt Water Injection Well No Violations Inspected containment dike, unloading pad, injection pressure and annulus pressure. Accompanied by Kip Thompson MRI 2. Witnessed two BD Oil Gathering Trucks at the facility. The first truck (License number PVT 1149) was not labeled with their UIC number the truck was finished unloading when I arrived. The second truck (License number PVR 3634 ) was labeled with the UIC number UIC #306 (1.75 lettering) and Brine (3 lettering) although the lettering was not 4 in height. I called BD Oil Gathering and told the office staff that their trucks must be labeled correctly for all UIC brine hauling with-in the state. I also informed Dylan Harlow (Green Hunter) that they need to make sure that the trucks that are hauling to their facility are registered and labeled for brine hauling.
1371841170 2013-06-20 Salt Water Injection Well No Violations Inspected injection pressure, annulus pressure, containment dike, injection pump, injection line, unloading pad, and collected a brine sample from BD Oil Gathering truck UIC # 306. Brine sample was taken to lab.
1375621380 2019-9-23 0:00: SW No Violations 5.80
137993657 2017-12-4 0:00: SW No Violations 2.00
1380197289 2013-09-23 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection line, annulus pressure, and injection pressure. Witnessed two BD Oil Gathering Trucks (UIC# 306) unloading brine. Both trucks had a completed brine log. The second truck license # PUV 7464 had the UIC # 306 label on the side of the tank. The label was 1.75 inches in height not 4 inches. There was no brine label on this truck. I gave the drive a copy of the brine hauler requirements. I collected a brine sample from the first truck. The brine sample was taken to the Jackson office for shipment to the ODNR Lab.
1386743778 2013-09-19 Salt Water Injection Well No Violations Pump not running at time of inspection. Containment area and unloading pad look good. A 45x1-3 area along the access road and below grade of the unloading pad appears to be scalded and void of vegetation. Quan-tab test strip used to check for CaCl- levels, levels found to be 48 ppm CaCl-.
1387284532 2013-12-16 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, annulus pressure, and injection pressure. Injection pump was not in operation during the inspection. There were zero brine trucks on site during the inspection. Site was snow covered. Good identification at the well and the building next to the unloading pad.
1393000133 2014-02-21 Salt Water Injection Well No Violations Inspected unloading pad, Containment pit, injection pump, injection line, injection pressure and annulus pressure. Good identification on the well and building. There were no brine trucks at the location during the inspection.
1398883768 2014-04-30 Salt Water Injection Well No Violations Inspected the injection pressure, annulus pressure, unloading pad, injection pump, containment pit and injection line. Collected brine sample from the injection line. Checked brine hauler records and truck UIC labeling.
1400266448 2014-05-16 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection line, injection pump, annulus pressure and injection pressure. Injection pump was off during inspection.
1401197926 2014-05-27 Salt Water Injection Well No Violations Pictures of site taken. Injection pressures tested at well while pump was running and while it was off. The injection pressure was 20psi while the pump was off and 380 while it was running, the annulus pressure was tested and found to be steady during both tests. No noted violations.
1405108231 2014-07-11 Salt Water Injection Well No Violations No noted violations.
1409183030 2014-08-27 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, annulus pressure and injection pressure. Good identification posted on the wellhead and building near the unloading pad. Witnessed a Hall Drilling brine truck unloading on the pad. Reviewed the brine hauler records, Collected a brine sample and took the sample to the ODNR Lab.
1416337525 2014-11-18 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, annulus pressure and injection pressure. Reviewed brine hauling logs.
1425929294 2015-03-09 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure, and annulus pressure. Witnessed brine truck unloading on the pad. Collected a brine sample to be transported to the lab. Reviewed brine hauling records. Truck license number PVY9301 Ohio, Tanker license number TPF5986 Ohio.
1427873071 2018-04-05 Salt Water Injection Well No Violations My inspection revealed the salt water injection well was in operation during my inspection. The pit containing fluid was down approximately 12 inches from the top of the containment dike. The injection tubing had 265 psi and the annulus had 225 psi. Legible identification was posted. The well was in compliance with Ohio revised code 1509.
1445266752 2019-01-14 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure and annulus pressure. Identification is posted. The containment pit level is 18 inches from the top.
1447959922 2015-11-19 Salt Water Injection Well Violations Noted Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure and annulus pressure. Identification posted at the well and near the unloading pad. The pit level has been lowered to the 1st baffle. The injection line valve is closed. The facility gate was locked. The 5 Rumpke dumpster located next to the entrance to the unloading pad has large holes in the bottom portion. This dumpster is used to dispose of used brine filters. The 5 area under and 2 area behind the dumpster is contaminated. A field test of the soil (soil collected and tested with a High Range Quantab) revealed an 8 on the strip which is 4429 ppm Cl. The contaminated soil must be removed and taken to an EPA approved landfill. A water tight container needs to be used to store the used filters prior to disposal.
1449253947 2015-12-04 Salt Water Injection Well No Violations Compliance Notice # 1447959922 Follow up inspection. The dumpster has been removed from the location. No effort has been made to remove the contaminated soil that was below and behind the dumpster. Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure, and annulus pressure. Identification is posted at the well and unloading pad. Pit level is down the baffles. The gate was locked during the inspection.
1454009069 2016-01-27 Salt Water Injection Well No Violations Compliance Notice # 1447959922 Follow up inspection. Contaminated soil has not been removed from the dumpster site. The facility gate is locked . The unloading pad and access road were snow covered. The containment pit fluid level is down to the first baffle. The injection pump has been removed from the location. All valves on the injection line are closed. The master valve on the injection tubing is open. Inspected the injection tubing pressure and annulus pressure. Identification is posted. I called Carper Well Service office and talked to Ryan. I asked about the soil removal at the dumpster site. Ryan said that they will attempt to remove the soil this week (weather permitting). He also told me that the injection pump was removed for service.
1458561646 2016-03-14 Salt Water Injection Well No Violations Inspected the containment area, unloading pad, injection line, injection pressure and annulus pressure. The injection pump is not on site. The injection line valves at the facility are closed. The injection tubing master valve is open. Identification is posted at the well and unloading pad. Containment area fluid level is 18 from the top of the containment wall.
1460148361 2016-04-07 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection line, injection pressure and annulus pressure. Identification posted at the well. The injection pump is not on site. The facility is not capable of injection operations with the injection pump removed. Containment pit fluid level is 14 inches from the top. The pressure on the injection tubing is natural gas. The injection line valve is closed. The injection line is disconnected where the injection pump was removed.
1467806437 2016-07-05 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection line, injection pressure and annulus pressure. The containment pit level is approximately 14 from the top. The injection line is disconnected at the facility. The injection pump is not on site. Injection line valves are closed. Identification posted.
1474304440 2016-09-15 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection line, injection pressure and annulus pressure. Identification posted at the unloading pad. The injection pump is not on location. The injection line valves are closed. The injection tubing master valve is closed. The containment pit level is 40 inches from the top.
1479131047 2016-11-10 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection line, injection pressure and annulus pressure. The injection pump is not on site. All valves on the injection line are closed. The containment pit level is at 36 inches from the top. Identification posted at the unloading pad.
1493384710 2017-04-27 Salt Water Injection Well No Violations While cross training with UIC Inspector Jon Scott, he showed me the picture of the identification tag filled out on this well. Violation has been corrected.
1501731910 2019-12-12 0:00 SC No Violations 3.00
1517671983 2020-6-10 0:00: SC No Violations 5.00
1518543995 2016-12-19 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection line, injection pressure and annulus pressure. The injection line valves are closed. The injection pump is not on location. The containment pit level is at 24 inches from the top and is frozen. Identification is posted at the unloading pad.
1519823646 2009-03-12 Salt Water Injection Well No Violations The well was found without an ID.
1525798435 2018-05-08 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pressure and annulus pressure. The injection pump has been removed from the location. Injection line valves and injection tubing master valve are closed. The containment fluid level is 24 inches below the top edge of containment. Called Aaron Mace (Carper) Aaron stated that the injection pump crank had broken. They pulled the pump for repairs. The repairs are to be completed with in 30 days. I requested to be notified when the pump is installed, to witness injection pump in operation. Identification is posted at the well. The well number is listed as 2407, the correct well number is 2704.
1528380867 2018-06-07 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection line, injection pressure and annulus pressure. The containment pit level is 16 inches from the top. All injection line valves and the injection tubing master valve are closed. The injection pump is not on location. The identification is posted with the wrong API#. The Id has 2407. The correct API is 3400922704.
1529591563 2018-06-21 Salt Water Injection Well Violations Noted Inspected the unloading pad, containment pit, injection line, injection pressure and annulus pressure. The containment pit level is 15 inches from the top. The injection tubing master valve is closed. The injection pump is not on location. The identification at the well and unloading pad has the wrong API number listed. The identification must list the correct API number 3400922704.
1531499106 2018-07-12 Salt Water Injection Well No Violations Compliance Notice # 1529591563 follow up inspection. The injection pump is on site and connected to the outlet side of the pump. The inlet line is not connected. The containment pit level is at 10 inches from the top. The identification permit numbers have not been corrected. Talked to Aaron Mace from Carper. He told me that they need new fittings to connect the inlet line. He also stated that they will be bringing new identification when they complete the pump connections.
1531761254 2018-07-16 Salt Water Injection Well No Violations Compliance Notice # 1529591563 follow up inspection. The containment pit level is 21 inches from the top. The injection pump is connected to the inlet and outlet sides of the pump. The injection line valve is open. The injection tubing master valve is open. The identification at the well and unloading pad have not been corrected. I talked to Aaron Mace at 11:55 am. He is aware that the identifications need to be corrected.
1536170056 2018-09-05 Salt Water Injection Well No Violations Compliance Notice # 1529591563 follow up inspection. The identification at the unloading pad and well have the correct permit number 2704 listed. The containment pit level is 13 inches from the top. The injection pump is connected to the injection line with all valves open. The injection tubing master valve is open. Inspected the unloading pad, containment pit, injection pump , injection line, injection pressure and annulus pressure.
1538079496 2018-09-26 Salt Water Injection Well No Violations Inspected the containment pit, unloading pad, injection pump, injection line, injection pressure and annulus pressure. Identification is posted. The containment pit level is 42 inches from the top. The injection line valves and injection tubing master valve are open.
156246569 2012-8-2 0:00:0 SW No Violations
1565153251 2004-03-10 Salt Water Injection Well No Violations No violations at the time of inspection. Updated coordinates, which were off significantly.
1568219693 2019-9-10 0:00: SW No Violations 5.00
1568386260 2019-9-12 0:00: SW No Violations 5.00
1573671456 2019-11-5 0:00: SC No Violations 2.70
1578423107 2020-1-6 0:00:0 SW No Violations 3.00
1580889050 2016-02-03 Salt Water Injection Well No Violations Compliance Notice # 1447959922 Follow up inspection. The contaminated area at the dumpster site has been remediated. Site was field tested at two locations using High Range Quantabs. Site #1 had zero chlorides, and Site # 2 had 0.8 on the strip which is 115 ppm Cl. The injection pump is still off site for maintenance.
1582449554 2012-04-02 Salt Water Injection Well No Violations Witnessed Mechanical Integrity Test with Jon Scott.
1583919377 2012-01-25 Salt Water Injection Well No Violations Accompanied Dan Goins.
1592826099 2020-6-8 0:00:0 SC No Violations 6.40
1594645274 2020-7-8 0:00:0 SC No Violations 4.00
1607303759 2013-08-30 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection line, annulus pressure, and injection pressure. Identification at the wellhead.
1614916539 2006-10-19 Salt Water Injection Well No Violations The pit was found full. Notified company. No action has been taken to comply with order.
1644883632 2013-01-22 Salt Water Injection Well No Violations Inspected the injection facility and checked the injection pressure and the annulus pressure. Injection pump is frozen. Green Hunter crew currently working to thaw out the pump.
1647439260 2013-11-21 Salt Water Injection Well No Violations No violations at facility.
1647549609 2019-6-7 0:00:0 SW No Violations 2.30
1649199664 2006-10-23 Salt Water Injection Well No Violations Fluid level in the pit was approximately a foot below the top.
1683640817 2012-10-01 Salt Water Injection Well No Violations Inspected injection pressure and annulus pressure. Inspected new injection line from the pump to the well. Inspected unloading pad while BD oil gathering tanker (UIC # 306) was unloading brine into containment pit. Reviewed hauling records for the well.
1687875146 2012-10-31 Salt Water Injection Well No Violations Collected brine sample from port on side of brine pump. Inspected unloading pad, concrete pit, injection pump, injection line and injection well. Checked annulus pressure and injection pressure at wellhead. Good identification at wellhead and unloading pad. Transported brine sample to Jackson office for shipment to Lab.
1687940961 2003-12-18 Salt Water Injection Well No Violations No violations at the time of inspection.
1688432579 2003-05-14 Salt Water Injection Well No Violations Follow-up on NOV, In-Compliance.
1705401668 2007-02-21 Salt Water Injection Well No Violations Frac tank was removed. A couple truck loads appear to have been taken from the pit. The well remains in noncompliance.
1718896141 2012-11-15 Salt Water Injection Well No Violations Inspected injection facilities and checked injection pressure and annulus pressure. Collected a water sample from Weavertown Environmental Group (WEG) Truck UIC # 527. Water hauled from a 5000 gallon tank Permit 3 101532 Cecil, Pa. Took water sample to Cambridge lab.
1736505040 2010-08-24 Salt Water Injection Well No Violations Inspection this day found pump not running, vacuum on tubing, 0# on annulus. Good IDs. Oil skim on water in dike area.
1782800456 2014-05-19 Salt Water Injection Well No Violations No noted violations.
1789106354 2018-09-19 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure and annulus pressure. The injection line valves are open, The injection tubing master valve is open. Identification is posted. The containment pit level is 2 3/8 inches from the top. I called Aaron Mace on 9-19-2018 at 2:23 pm. I told him that the pit level is at 2 3/8 inches from the top. Aaron told me that he will send someone out to pump down the fluid.
1810284641 2015-10-19 Salt Water Injection Well No Violations No noted violations. Barrel counter at pump has been removed, well was not operating at time of inspection, no attendant at facility.
1827357313 2012-03-14 Salt Water Injection Well No Violations Accompanied Jon Scott on an injection well inspection. Noticed a couple of small areas of contaminated soils. We spoke to the well operator about remediation.
1830681117 2019-6-18 0:00: SW No Violations 2.50
1839027320 2010-03-09 Salt Water Injection Well No Violations Inspection this day found a nicer, cleaner facility than I am used to in Washington Co. - my 1st visit. Found pump not running, tubing on vacuum, 0# on annulus. Good IDs, said they are using the well small to moderate amount. Fluid about 1/5 down from top.
1847380278 2006-12-15 Salt Water Injection Well No Violations No action has been taken to comply.
1853486313 2016-01-05 Salt Water Injection Well No Violations No noted violations. Concrete dike does not appear to have any leaks, there was no one at the facility at the time of inspection and the well did not appear to be in operation.
1871237260 2006-04-04 Salt Water Injection Well Violations Noted Pit was found completely full. Called operator (4/4/06) and instructed him to take a load out of the pit ASAP.
18816684 2019-10-4 0:00: SW No Violations 2.50
1886897126 2017-02-14 Salt Water Injection Well No Violations Inspection of the unloading pad, containment pit, injection line, injection pressure and annulus pressure. The injection line valves are closed. The injection pump is not on location. The injection line is not connected to anything, it terminates where the pump would have been to an open hammer union. The containment pit level is at 1 foot 2 inches from the top of containment pit and has oily substances floating on top. Identification is posted at the unloading pad and is legible, however the identification posted at the wellhead is blank. There is a closed gate at the unloading pad and a chain across the road going to the containment pit. Pictures were taken.
1928223676 2012-06-13 Surface Facility Construction No Violations Poured new concrete unloading pad. No notification was received on the construction of the pad. Pad has two drains that are connected to new 4 SDR 11 plastic line connected to concrete pit. A new 4 SDR 11 line was ran from the unloading pad to the concrete pit for unloading trucks. A 6 corrugated drain was ran for diversion of surface water around the up slope side of the new unloading pad. Well tender showed me a plastic jug attached to a stick and 2 gloves that were found floating in the pit. I suggested installing additional fencing around pit.
1935659109 2004-10-08 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1941781500 2013-05-21 Salt Water Injection Well No Violations Inspected injection pressure, annulus pressure, containment pit, and unloading pad. There were no trucks during inspection.
1947677268 2012-02-10 Salt Water Injection Well No Violations Met with Dan Goins to check the pressures on the well.
1953759868 2013-03-11 Salt Water Injection Well No Violations Inspected injection pressure and annulus pressure. Inspected the unloading pad, concrete pit, and injection pump. Reviewed the hauling log currently at 11,380 barrels.
1962343430 2014-01-13 Salt Water Injection Well No Violations Inspected unloading pad, Containment pit, injection pump, injection line, injection pressure and annulus pressure. Repairs have been made to the annulus. A 2 ball valve froze and busted on the annulus. The ball valve has been replaced. Accompanied by Andrew Adgate UIC Geologist.
1975458245 2005-05-09 Salt Water Injection Well Violations Noted The fluid level was 4 inches from the top of the storage pit. The well needs tested.
1986797844 2014-01-27 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure and annulus pressure. Site was snow covered. Unloading pad was cleared of snow and ice.
1989508424 2008-10-03 Salt Water Injection Well No Violations There were no violations found, at the time of inspection.
1993940341 2012-03-22 Salt Water Injection Well No Violations Met Jon Scott at well to review records and reports and explain history on well to him before he takes over well for inspections.
2009924170 2012-12-05 Salt Water Injection Well No Violations Tested the annulus at 675 psi for 15 minutes. Initial test failed due to leak in the wellhead. Tightened the wellhead ring and tested again. Well annulus held 675 psi for 15 minutes with no loss. Smitty Vandall and Dylan Harlow were on site.
2039586332 2019-5-15 0:00: SW No Violations 2.50
2050387968 2012-03-14 Salt Water Injection Well No Violations Jim Hubbard has been cleaning outside of dike North West corner. Excavated an area 2 feet by 1 foot and a second area 2 feet by 2.5 feet.
2061282767 2012-09-26 Salt Water Injection Well No Violations A vacuum truck was removing the skim of oil from the top of the fluids in the holding pit. Lime had also been applied to the soil in the area around the new flow line and load line as well as the well head.
2079718712 2014-10-30 Salt Water Injection Well No Violations Manifest checked on 80 bbl truck off loading at time. No noted violations.
2103432780 2019-02-28 Salt Water Injection Well No Violations Inspected the unloading pad, containment pit, injection pump, injection line, injection pressure and annulus pressure. Identification is posted. The containment pit level is at 38 inches from the top. The injection tubing master valve is open. The injection line valves are open. There has been recent excavation up slope (SW) of the unloading pad. The excavation area is diverting surface water runoff away from the unloading pad.
2113127346 2003-05-08 Salt Water Injection Well Violations Noted An inspection of the well site revealed a ditch cut across the lease rd., no way of entering and unloading brine for disposal. Well appears to be idle at this time. A M.I.T. test needs to be done on this well also. CALLED MR. CARPER ABOUT VIOLATIONS HE SAID ATHENS COUNTY CUT THE DITCH ACROSS THE LEASE RD. TO STOP TRUCKS FROM ENTERING SITE. EXPLAINED TO HIM THAT THE WELL WAS IN VIOLATION AND A NOTICE OF VIOALTION WILL BE ISSUED TO PLUG OR PRODUCE WELL, AND A M.I.T. TEST NEEDS DONE.
212813321 2009-2-18 0:00: SW No Violations
2135370973 2008-01-16 Salt Water Injection Well No Violations The service rig was still on the well. No further action appears to have been taken to plug the well.
247974618 2018-7-20 0:00: SW No Violations 1.00
36892046 2013-2-27 0:00: SW No Violations 1.30
38099222 2011-8-3 0:00:0 SW No Violations 2.00
384159073 2018-7-10 0:00: SW No Violations 2.60
55774118 2020-3-5 0:00:0 SW No Violations 2.00
558786308 2014-7-3 0:00:0 SW No Violations 3.50
5609i205 2001-5-31 0:00: SW No Violations
5609i245 2001-7-12 0:00: SW No Violations
566599901 2006-7-14 0:00: SW No Violations
59773602 2012-6-28 0:00: SW No Violations 4.00
631574685 2019-2-11 0:00: SW No Violations
652212545 2008-6-10 0:00: SW No Violations
674592686 2019-7-23 0:00: SW No Violations 2.50
693552892 2005-9-16 0:00: SW No Violations
706327766 2008-6-30 0:00: SW No Violations
716761238 2013-10-29 0:00 SW No Violations 3.00
761390138 2011-12-20 0:00 SW No Violations 1.00
787446481 2006-5-17 0:00: SW No Violations
843845335 2012-6-28 0:00: SW No Violations
868535672 2006-4-27 0:00: SW No Violations
882152013 2008-12-3 0:00: SW No Violations
914182433 2004-2-11 0:00: SW No Violations
924835606 2003-4-22 0:00: SW No Violations
937334548 2019-4-18 0:00: SW No Violations 2.30
976706387 2017-12-1 0:00: SW No Violations 3.00
988178787 2008-9-30 0:00: SW No Violations
iTOMK00013 2001-05-31 Salt Water Injection Well No Violations
iTOMK000134 2001-5-31 0:00: SW No Violations
iTOMK000135 2001-5-31 0:00: SW No Violations
UIC240 1987-6-3 0:00:0 SW No Violations
UIC325 1987-9-14 0:00: SW No Violations
UIC330 1987-3-9 0:00:0 SW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
001269i209 US-OH-107323 2000-12-14 Mechanical failure/contamination
001269i209 US-OH-107324 2000-12-14 Failure to plug
001269i707 US-OH-107435 2002-01-23 Failure to perform Mechanical Integrity Test
001269i854 US-OH-107490 2002-03-07 Pollution/Contamination
005609i205 US-OH-126232 2001-05-31 Violation of injection tubing/fitting requirements
0325960936 US-OH-123419 2001-05-31 Violation of injection tubing/fitting requirements
0410095649 US-OH-124342 2002-03-07 Pollution/Contamination
0590782139 US-OH-126641 2000-12-14 Mechanical failure/contamination
0590782139 US-OH-126642 2000-12-14 Failure to plug
0631574685 US-OH-127163 2019-04-08 NONE Failure to report disposal fees
0761390138 US-OH-128655 2011-12-21 Violation of injection tubing/fitting requirements
0852014890 US-OH-129689 2002-01-23 Failure to perform Mechanical Integrity Test
0929186419 US-OH-130621 2012-01-26 Violation of injection tubing/fitting requirements
1116558229 US-OH-102932 2012-01-05 Violation of injection tubing/fitting requirements
1354768478 US-OH-110262 2012-12-05 Failure to monitor annulus pressure
1447959922 US-OH-113012 2016-02-12 Pollution/Contamination
1529591563 US-OH-114665 2018-09-06 9-3-06(K) Failure to legibly identify well
1871237260 US-OH-118755 2006-04-18 Pollution/Contamination
1871237260 US-OH-118756 2006-04-16 Failure to perform Mechanical Integrity Test
1975458245 US-OH-119963 2005-05-16 Failure to perform Mechanical Integrity Test
2113127346 US-OH-121613 2003-05-12 Well shall be plugged
2113127346 US-OH-121614 2003-05-12 Urban - failure to meet tank battery setbacks from mandatory pooled property
2113127346 US-OH-121615 2003-05-12 Failure to perform Mechanical Integrity Test

For data sources see[5]

References