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34-127-23757

Well Details

Well ID: 34-127-23757
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Country: United States
State: Ohio
County: Perry
Municipality: Harrison Township
Operator Name: MIDWEST OIL & GAS
Well Pad ID:
Farm/Lease Name: CANNON ROBERT E
License Status: Producing
License Date: 1976-03-12
Spud Date: 1976-07-06
Spud Drilling Contractor:
Final Drill Date: 1976-08-05
Well Total Depth: 3592.00 ft
Configuration: Vertical
Latitude: 39.790000
Longitude: -82.080000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-03-12 573 MIDWEST OIL & GAS GeoDate 3/12/76
Original Spud 1976-07-06 I.P.NONE RPT. FDT/RED ROCK
Completed 1976-08-05 I.P.NONE RPT. FDT/RED ROCK
Reached Total Depth 1976-08-05 I.P.NONE RPT. FDT/RED ROCK
Record Last Modified 2013-10-03 I.P.NONE RPT. FDT/RED ROCK

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 MIDWEST OIL & GAS 0.00 387.00 365
1986 MIDWEST OIL & GAS 0.00 330.00 365
1987 MIDWEST OIL & GAS 0.00 135.00 365
1988 MIDWEST OIL & GAS 0.00 68.00 365
1989 MIDWEST OIL & GAS 0.00 217.00 365
2008 MIDWEST OIL & GAS 0.00 66.00 365
2009 MIDWEST OIL & GAS 0.00 72.00 365
2010 MIDWEST OIL & GAS 0.00 71.00 365
2011 MIDWEST OIL & GAS 0.00 134.00 365
2012 MIDWEST OIL & GAS 0.00 165.00 366

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 MIDWEST OIL & GAS Brine 35 365
1986 MIDWEST OIL & GAS Brine 103 365
1987 MIDWEST OIL & GAS Brine 165 365
1988 MIDWEST OIL & GAS Brine 0 365
1989 MIDWEST OIL & GAS Brine 0 365
2008 MIDWEST OIL & GAS Brine 0 365
2009 MIDWEST OIL & GAS Brine 0 365
2010 MIDWEST OIL & GAS Brine 0 365
2011 MIDWEST OIL & GAS Brine 110 365
2012 MIDWEST OIL & GAS Brine 80 366

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1898201587 2016-2-3 0:00:0 PW No Violations
-291788356 2016-2-2 0:00:0 PW No Violations 3.00
-413530437 2014-9-25 0:00: PW No Violations 1.00
-730140835 2018-1-26 0:00: PW No Violations 0.50
0277642619 2011-07-28 Production Wells No Violations No violations at this time.
0291788356 2016-02-02 Production Wells No Violations There was a gas leak on 02/02/2016 that evacuated part of Crooksville. The PUCO inspector Mike Purcell that was called out on the job said the cause of the gas smell was coming from this well. During my inspection that today I found no trace of this well being fiscally able to supply enough gas to evacuate a town. The well is shut in and has been for the last two months because the pumper has been sick. The investigation will continue on 02/02/2016.
0413530437 2014-09-25 Production Wells No Violations A Chiefs Order has been issued on this well for Failure to Maintain Liability Insurance. The well is capable of production at this time. The well has a pumping unit on it with rods and 2 tubing in it The production valves coming from the wellhead to the tank pad are open. The identification for this well is located on the well and the tank.
0730140835 2018-01-26 Production Wells No Violations The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The production valves coming from the wellhead to the tank pad are open. The identification for this well is located on the well and the tank. There are no violations at this time.
1318597995 2016-03-07 Production Wells No Violations I returned to this well to do a field inspection on it to see if it was leaking any gas around the well. The production lines are hooked up to the well and are in operation. There is a flare coming off of the well to burn off exes gas. There was no heavy gas smell around the well. There are no violations to report.
1401521953 2008-12-23 Production Wells No Violations No violations.
1450037273 2008-02-11 Production Wells Violations Noted An inspection of the well revealed the well is idle, no production has been reported on well since 1987, and flow line is parted in several places. No ID at the well or tank battery, need a dike around production tanks.
1490472249 2019-01-04 Production Wells No Violations The well has a pumping unit on it with rods and 2 inch diameter tubing in it. The production valves coming from the wellhead to the tank pad are open. The identification for this well is located on the well and the tank. There are no violations at this time.
1597696855 2020-8-17 0:00: PW No Violations 0.30
1724906547 2008-04-17 Production Wells No Violations Follow-up on NOV, In-Compliance.
1898201587 2016-02-03 Production Wells No Violations I returned to this well to continue the investigation of this gas leak with Doug Bennett, Dan Goins and Scott King all from the Division of Oil and Gas. We were accompanied by Todd Altier and Benny Altier. They are the operators of the well. During the inspection we found that this well could not be the cause of the evacuation. We inspected the surrounding area and found where Columbia Gas was working the day before on there lines. The gas smell was still coming from there transmission line and we did find more leaks in that line. We all believe the well in question was not leaking or capable of leaking since the valves are shut at the well.
277642619 2011-7-28 0:00: PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1450037273 US-OH-113054 2008-02-13 General Safety
1450037273 US-OH-113055 2008-02-13 Failure to legibly identify well
1450037273 US-OH-113056 2008-02-13 No SPCC dike/or failure to keep dike free of water or oil
1450037273 US-OH-113057 2008-02-13 Well shall be plugged

For data sources see[7]

References