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34-115-24683

Well Details

Well ID: 34-115-24683
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Country: United States
State: Ohio
County: Morgan
Municipality: Center Township
Operator Name: UTICA RESOURCE OPERATING LLC
Well Pad ID: US-OH-000823
Farm/Lease Name: PALMER
License Status: Producing
License Date: 2013-11-15
Spud Date: 2013-11-27
Spud Drilling Contractor: H&P DRILLING
Final Drill Date: 2014-04-29
Well Total Depth: 14987.00 ft
Configuration: Horizontal
Latitude: 39.600000
Longitude: -81.660000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2013-11-15 Proposed Formations:POINT PLEASANT, Issued Date:11/15/2013, Expired Date:11/15/2015 12:00:00 PM, Drilling unit acres:627, Proposed Well Type:OG, Proposed Well Class:EDPW
Reached Total Depth 2014-04-29 FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.
Completion Report Received 2014-12-12 FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.
Correction to Well 2015-02-20 CHANGE IN TARGET AND TAKE-POINT INFORMATION (FOOTAGES AND COORDINATES) FROM AS DRILLED SURVEY PLAT. UNIT SIZE DECREASED.
Construction Permit Expires 2015-11-15 FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.
Change of Owner 2018-05-04 Operator changed from 8595, PDC ENERGY INC to 10114, UTICA RESOURCE OPERATING LLC
Record Last Modified 2019-01-22 FORM 8A N/A, COMPLIANCE NOTICE ISSUED TO UTICA RESOURCE OPERATING (Cert#9489009000276059844967), WELLS DRILLED UNDER PDC ENERGY, INFORMATION WAS NOT TRANSFERRED TO NEW OPERATOR/NEW OPERATOR UNABLE TO OBTAIN SURFACE HOLE ADDITIVES-1/22/19 ALE.

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2014-08-06 H2O 15 1993 Bbl 99750 CalFrac STAGE 39B/39B

30 SHOTS

2020-07-16 H2O 15 6096 Bbl 237711 CalFrac STAGE 1/39B

30 SHOTS STAGES 2-39A SEE IMAGES

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2014 PDC ENERGY INC 78620 23164 120
2015 PDC ENERGY INC 208179 22964 363
2016 PDC ENERGY INC 151999 9962 365
2017 PDC ENERGY INC 108850 5978 358
2018 UTICA RESOURCE OPERATING LLC 101429 3534 364
2019 UTICA RESOURCE OPERATING LLC 22719 966 90

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2014 PDC ENERGY INC Brine 16491 120
2015 PDC ENERGY INC Brine 11886 363
2016 PDC ENERGY INC Brine 3855 365
2017 PDC ENERGY INC Brine 2005 358
2018 UTICA RESOURCE OPERATING LLC Brine 1472 273
2019 UTICA RESOURCE OPERATING LLC Brine 405 90

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1193968809 2014-7-21 0:00: DD No Violations
-397999313 2017-1-23 0:00: PW No Violations 0.50
0397999313 2017-01-23 Production Wells No Violations The inspection this day revealed that this well is equipped with a plunger lift system, a 4 1/2 inch diameter wellhead, 2 inch diameter steel production lines, and 1 1/2 inch diameter production tubing. The valves on the wellhead are open at the time of inspection. The tank battery consist of six (6) 500 barrel steel tanks in a containment dike. Identification for the wells and tanks are posted and in proper order. The well tender for PDC was on site and informed me that they had put a new plunger in this well to help with production. There are no issues to report at this time and this well is in production at the time of inspection.
0583419501 2018-04-09 Preliminary Restoration No Violations I was on location today to do a preliminary restoration on this well. The well has been reporting production since 2014. All of the drilling equipment has been removed and the drilling pits have been filled in. The well is in-compliance at this time.
0775787808 2014-01-05 Drill / Deepen / Reopen No Violations I was on location to witness Allied Oilfield Services cement 378 of 20 the surface casing. PDC is using the H & P Flex rig 385. PDC used 4 centralizers. Plug was down at 9:15pm with good cement returns.
1050357990 2013-11-27 Casing String Witnessed No Violations I am on site to witness the cementing of the conductor casing. Express Energy Services drilled 36 hole to a depth of 100. Express then cemented 100 of 30 casing in place with 315 sks of class A cement with 2% CaCl. 18 bbl of cement returns to surface.
1193968809 2014-07-21 Drill / Deepen / Reopen No Violations PDC is currently in on Stage 10 of their completion operation. The average treating pressure has been around 6800 psi at 78-80 bbls/min. They are no longer completing both wells (2H and 3H) at the same time but will finish the 3H first before completing the 2H.
1385566018 2013-11-27 Drill / Deepen / Reopen No Violations I arrived on location to witness PDC set their conductor casing, however they were having hard time getting the casing into the hole. They have pushed the cement job to the early evening.
1389962172 2014-01-17 Drill / Deepen / Reopen No Violations I arrived on location to witness Halliburton cement 5786 of 9 5/8 intermediate casing with 1340 sacks of cement. PDC is using the H & P 385 Flex Rig. Upon arrival, operator was circulating the hole and Halliburton was still trying to get their equipment rigged up and running properly at the wellhead. PDC used 21 centralizers. Plug was down at 10:20am and landed at 12:15pm, however the pressure gradually backed off possibly indicating a leak in the plug or loss of cement to formation. There were spacer returns but no cement returns at the surface. The decision was made to leave the head on and wait 8 hours for the cement to set then run a temperature log, collar locator, and gyro in order to determine the condition of the cement. 1/18/2014: Temperature log showed top of cement at 410. They ran a gyro and then skid the rig to begin drilling the 2H.
1396440683 2014-04-02 Administrative Inspection No Violations PDC skid the H & P rig to the 3H and ran cement bond log. The top of cement on the 9 5/8 was actually at 2610. They are currently waiting on perf and cement trucks in order to perf at 2580 and set a retainer at 2270.
1397821335 2014-04-18 Drill / Deepen / Reopen No Violations Day Gray called and stated they were unable to get their build rates great enough to land so they pulled back and set a kick plug down to 6200.
1399463346 2014-05-07 Drill / Deepen / Reopen No Violations I arrived on location for the operation and safety meetings. At this time the well is producing very little gas. If it is bridged off they will know once the pull on the drill pipe by drag weight. During the operation meeting, it was discussed that PDC personnel will attempt to kill the well followed by the cutting and tripping out the drill pipe. They will then install a packer to control the well. They plan on using a radial cutting tool. Wild Well Control will be at the wellhead to determine the area of mechanical integrity failure.
1399563777 2014-05-08 Drill / Deepen / Reopen No Violations I was notified en route this morning that the RCT (radial cutting torch) did not succeed in cutting the drill pipe so they set a back off charge and were able to free the drill pipe. They then POOH, installed the packer and TIH. When they were attempting to set the packer, the setting tool failed for unknown reasons, and it fell down hole and is currently on top of the drill pipe (fish). It is currently stuck somewhere around 700-
1405542737 2014-07-16 Drill / Deepen / Reopen No Violations I was on location to witness PDC and CalFrac undergo stimulation operations. For the first stage they hydraulically fractured the formation with a breakdown of 5678 psi. The average treating pressure was around 6160 psi with an average rate of 20bbls/minute.
1411672530 2014-09-25 Production Wells No Violations PDC is currently producing the Palmer 2H and 3H. They were on location hooking up a new separator in order to produce out of the Palmer 44-20 vertical well.
1550587840 2019-02-19 Production Wells No Violations I was on location today to do a field inspection on this well. The well was equipped with gauges for monitoring pressure on the 9.625 and 13.375 casing strings. The well did not have any identification on it and is required to because there is multiple wells producing into the same production tanks. The pumper was on location during my inspection so let him know that the well needed legible identification on it.
1880710286 2014-04-24 Drill / Deepen / Reopen No Violations I stopped by for a rig check. Everything looks good and the H & P flex rig was currently drilling the lateral at a depth of 8795.
2142061850 2018-04-04 Production Wells No Violations I am accompanied by Supervisor Dan Goins. We inspected the site for annular pressure monitoring equipment. The well was equipped with gauges for monitoring pressure on the 9.625 and 13.375 casing strings.
583419501 2018-4-9 0:00:0 PL No Violations 0.50
775787808 2014-1-5 0:00:0 DD No Violations 5.50

For data sources see[8]

References