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Well ID: 34-075-22636 | Loading map...
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Country: United States | |
State: Ohio | |
County: Holmes | |
Municipality: Ripley Township | |
Operator Name: H I SMITH OIL & GAS INC | |
Well Pad ID: | |
Farm/Lease Name: MILLER SAMUEL A | |
License Status: Final Restoration | |
License Date: 2011-04-21 | |
Spud Date: 1980-07-08 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-08-06 | |
Well Total Depth: 3398.00 ft | |
Configuration: Vertical | |
Latitude: 40.640000 | |
Longitude: -82.000000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-07-02 | 511 SMITH H I OIL & GAS GeoDate 7/2/80 |
Original Spud | 1980-07-08 | |
Completed | 1980-08-06 | |
Reached Total Depth | 1980-08-06 | |
APP | 2011-04-21 | Proposed Formations:CLINTON, Issued Date:4/21/2011, Expired Date:4/20/2013 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2012-09-14 | |
Construction Permit Expires | 2013-04-20 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3282 | 3356 | 14 |
3282 | 3356 | 14 | |
3282 | 3356 | 14 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1700 Bbl | 26000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | H I SMITH OIL & GAS INC | 2953.00 | 527.00 | 0 |
1985 | H I SMITH OIL & GAS INC | 2894.00 | 651.00 | 0 |
1986 | H I SMITH OIL & GAS INC | 1978.00 | 372.00 | 365 |
1987 | H I SMITH OIL & GAS INC | 1827.00 | 470.00 | 365 |
1988 | H I SMITH OIL & GAS INC | 1938.00 | 360.00 | 260 |
1989 | H I SMITH OIL & GAS INC | 858.00 | 206.00 | 365 |
1990 | H I SMITH OIL & GAS INC | 1326.00 | 339.00 | 365 |
1991 | H I SMITH OIL & GAS INC | 1229.00 | 370.00 | 365 |
1992 | H I SMITH OIL & GAS INC | 1666.00 | 465.00 | 312 |
1993 | H I SMITH OIL & GAS INC | 1058.00 | 376.00 | 365 |
1994 | H I SMITH OIL & GAS INC | 1232.00 | 328.00 | 260 |
1995 | H I SMITH OIL & GAS INC | 843.00 | 280.00 | 260 |
1996 | H I SMITH OIL & GAS INC | 185.00 | 321.00 | 260 |
1997 | H I SMITH OIL & GAS INC | 97.00 | 257.00 | 260 |
1998 | H I SMITH OIL & GAS INC | 127.00 | 151.00 | 260 |
1999 | H I SMITH OIL & GAS INC | 211.00 | 243.00 | 365 |
2000 | H I SMITH OIL & GAS INC | 196.00 | 209.00 | 365 |
2001 | H I SMITH OIL & GAS INC | 210.00 | 68.00 | 365 |
2002 | H I SMITH OIL & GAS INC | 188.00 | 42.00 | 365 |
2003 | H I SMITH OIL & GAS INC | 170.00 | 47.00 | 365 |
2004 | H I SMITH OIL & GAS INC | 192.00 | 224.00 | 365 |
2005 | H I SMITH OIL & GAS INC | 212.00 | 198.00 | 365 |
2006 | H I SMITH OIL & GAS INC | 119.00 | 95.00 | 365 |
2007 | H I SMITH OIL & GAS INC | 0.00 | 60.00 | 365 |
2008 | H I SMITH OIL & GAS INC | 252.00 | 97.00 | 188 |
2009 | H I SMITH OIL & GAS INC | 268.00 | 150.00 | 365 |
2010 | H I SMITH OIL & GAS INC | 223.00 | 77.00 | 365 |
2011 | H I SMITH OIL & GAS INC | 105.00 | 199.00 | 0 |
2012 | H I SMITH OIL & GAS INC | 121.00 | 96.00 | 366 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-511535298 | 2013-5-16 0:00: | FR | No Violations | |
-966181260 | 2012-9-5 0:00:0 | PB | No Violations | |
-967181842 | 2012-9-10 0:00: | PB | No Violations | |
0073257851 | 2012-09-17 | Final Restoration | No Violations | The location has been put to final grade. The water tank remains. Needs seeded. |
0211121252 | 2012-08-30 | Plug / Plug Back | No Violations | No further progress on the plugging job. |
0232674075 | 2012-09-07 | Plug / Plug Back | No Violations | Spotted a 25 sack cement plug thru 1-1/2 tubing. See the plugging report for details. |
0511535298 | 2013-05-16 | Final Restoration | No Violations | Final restoration is passed. |
0966181260 | 2012-09-05 | Plug / Plug Back | No Violations | Pulled 1-1/2 tubing and 2-7/8 tubing and packer. Steamed 1-1/2 tubing and ran it back to spot the bottom cement plug. |
0967181842 | 2012-09-10 | Plug / Plug Back | No Violations | Ripped the 4-1/2 casing at 1270. Pulled one joint. Well kicked off thru the casing and spiled .5 bbls of oil and approx 1 bbl of salt water in the immediate well bore area. Pulled the 4-1/2 casing. |
1228306278 | 2012-09-13 | Plug / Plug Back | No Violations | The top clay plug did not drop back. The well has been plugged and abandoned this date. See the plugging report for details. |
1346237323 | 2012-08-28 | Plug / Plug Back | No Violations | The pump has been unseated and the rods are hanging. No activity. |
211121252 | 2012-8-30 0:00: | PB | No Violations | |
232674075 | 2012-9-7 0:00:0 | PB | No Violations | |
73257851 | 2012-9-17 0:00: | FR | No Violations |
For data sources see[9]