Well Details
Well ID: 34-127-26331
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Country: United States
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State: Ohio
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County: Perry
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Municipality: Salt Lick Township
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Operator Name: NORTHWOOD ENERGY CORP
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Well Pad ID:
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Farm/Lease Name: HOCKING VALLEY PRODUCTS
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License Status: Producing
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License Date: 1984-05-18
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Spud Date: 1984-05-21
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Spud Drilling Contractor: MILLER & VERMILLION
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Final Drill Date: 1984-06-10
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Well Total Depth: 3290.00 ft
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Configuration: Vertical
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Latitude: 39.610000
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Longitude: -82.260000
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For data sources see[1]
Well History
Oil and Gas
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1984-05-18
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Issued Date 5/18/84 Expired Date 11/14/84 Acres 0080000 Tool Type CT Proposed Formation CLINTON Proposed Depth 03290 Proposed Drill Depth 03290
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Original Spud
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1984-05-21
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Completed
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1984-06-10
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Reached Total Depth
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1984-06-10
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CO
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1984-06-23
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182 BELDEN & BLAKE CO GeoDate 5/18/84
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Completion Report Received
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1984-09-04
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Construction Permit Expires
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1984-11-14
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CO
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1994-10-25
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4381 PELICAN PRODUCING INC GeoDate 5/18/84
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CO
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1996-07-16
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1512 ALTIER H L SERVICE CO INC GeoDate 5/18/84
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Change of Owner
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2001-05-29
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Operator changed from 1512, ALTIER H L SERVICE CO INC to 1634, NORTHWOOD ENERGY CORP
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Record Last Modified
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2017-02-15
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For data sources see[2]
Perforation Treatments
1997-06-29
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3216
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3280
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0
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3216
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3280
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0
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2006-09-11
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3234
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3248
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16
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3234
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3248
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16
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3216
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3280
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0
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For data sources see[3]
Stimulations Data
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H2O
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0
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84000 Gal
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30000
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FRAC: H2O,SAND
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For data sources see[4]
Production Data
For data sources see[5]
[6]
Waste Data
For data sources see[7]
[8]
Inspection Data
Inspections Performed
-1223699762
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2014-4-30 0:00:
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PW
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No Violations
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1.00
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-1231135760
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2016-11-2 0:00:
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PW
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No Violations
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1.00
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-1253580432
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2020-4-16 0:00:
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PW
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No Violations
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0.50
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-1395723465
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2007-11-14 0:00
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AD
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No Violations
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-1539643583
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2016-3-24 0:00:
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PW
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No Violations
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-552818012
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2014-4-21 0:00:
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PW
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No Violations
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1.00
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-844603004
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2007-9-18 0:00:
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AD
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No Violations
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-876914375
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2014-4-21 0:00:
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PW
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No Violations
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1.00
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0000PL6754
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Preliminary Restoration
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No Violations
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Preliminary Restoration done information from Data Point
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0347734571
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2016-03-21
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Production Wells
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No Violations
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I returned to this well to check on the clean-up of the oil spill. The company is still working on removing contamination at this time.
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0358550638
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2016-03-21
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Production Wells
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No Violations
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I returned to this well to do a follow-up inspection on it. During the time of my inspection no one was onsite. I was on location first thing in the morning. I could see where they have been making progress from the previous day.
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0552818012
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2014-04-21
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Production Wells
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No Violations
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I went out to do a follow up on this well. I was unable to go to the well because there were hunters in the area. It is turkey season this week. I will go to the well again one day this week. If I can not get to the well I will have to wait until next week.
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0789864518
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2014-04-01
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Production Wells
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Violations Noted
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During the field inspection of this well I found contamination around the wellhead. The stuffing box is leaking and will need to be fixed. The contaminated soil will need to be removed from the location. The identification at the well has faded and is not legible The ID will need to be replaced. The ID has to have the following, Owner, well name, well number, permit number, township, county, and emergency contact number.
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0844603004
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2007-09-18
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Annular Disposal
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Violations Noted
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An inspection of the well revealed no ID at the well head.
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0876914375
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2014-04-21
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Production Wells
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No Violations
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I went out to do a follow up on this well. I was unable to go to the well because there were hunters in the area. It is turkey season this week. I will go to the well again one day this week. If I can not get to the well I will have to wait until next week.
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0934906291
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2014-04-22
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Production Wells
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No Violations
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There are hunters in the area again today. I will have to wait until next week to do a follow-up on this well.
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1223699762
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2014-04-30
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Production Wells
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No Violations
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I returned to this well to do a follow-up inspection for the identification and contamination. Both of the violations have been resolved and the well is now in-compliance. No violations at this time.
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1231135760
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2016-11-02
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Production Wells
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No Violations
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I returned to this well today to do a follow-up inspection it. All of the contaminated soil has been removed from the location. At this time there is no violation at this well.
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1263340574
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2007-11-20
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Annular Disposal
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No Violations
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Follow-up on NOV, In-Compliance.
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1364197138
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2016-03-18
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Production Wells
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Violations Noted
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I was contacted by Gordon Farley the inspector for the Wayne National Forrest on 3/17/2016. He let me know that he had found a leak at this well. We scheduled to meet at 8:30am on 3/18/2016 to inspect the well and start the cleanup. Mike Corp from Northwood Energy met us at the well with 2-water trucks and a mini hoe. They have started to cleanup the contamination. A tree had fallen during the wind storm and broke the flow line. The oil escaped from the line into a water based area. The land is not connected to a water way it is an old coal mine land that was not reclaimed. The water is just build up from the rain we have had. The company is currently working on the job. An estimated 5-10bbls of oil has leaked from the line. After talking with Mike Corp it is likely to be 5bbl from the production this well makes.
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1395723465
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2007-11-14
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Annular Disposal
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No Violations
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Follow-up on NOV, Non-Compliance, spoke with Ron Moore about violation.
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1430754465
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2015-05-04
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Production Wells
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No Violations
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This well appears to be capable of production. The well has a pumping unit on it with rods and 2 tubing in it. The identification for this well is located at the well. There are no violations at this time.
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1539643583
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2016-03-24
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Production Wells
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No Violations
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I returned to this well to do a follow-up on the cleanup of this well. I met Inspector Gordon Farley from Wayne National Forrest out on location to go over the progress. During our inspection the company was on location working on the cleanup. They were putting in a new flow line also. The progress is going good at this point. I will be checking back on 3/29/2016.
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347734571
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2016-3-21 0:00:
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PW
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No Violations
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358550638
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2016-3-21 0:00:
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PW
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No Violations
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1.00
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789864518
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2014-4-1 0:00:0
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PW
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No Violations
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1.00
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934906291
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2014-4-22 0:00:
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PW
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No Violations
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1.00
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PL6754
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PL
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No Violations
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Violations Commited
0789864518
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US-OH-128990
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2014-05-05
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Well operation causing pollution and contamination
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0789864518
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US-OH-128991
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2014-05-05
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Failure to legibly identify well
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0844603004
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US-OH-129621
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2007-09-19
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Failure to legibly identify well
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1364197138
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US-OH-110666
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2016-11-04
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9-1-07
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Well operation causing pollution and contamination
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For data sources see[9]
References