X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-053-20613

Well Details

Well ID: 34-053-20613
Loading map...
Country: United States
State: Ohio
County: Gallia
Municipality: Gallipolis Township
Operator Name: HUFFMAN-BOWERS INC
Well Pad ID:
Farm/Lease Name: GILMAN MEMORIAL PRESH CENTER
License Status: Producing
License Date: 1984-05-23
Spud Date: 1984-06-29
Spud Drilling Contractor: GARD DRILLING
Final Drill Date: 1984-07-03
Well Total Depth: 1887.00 ft
Configuration: Vertical
Latitude: 38.830000
Longitude: -82.170000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-10-13 467 BRASEL R GENE GeoDate 10/13/81
Oil and Gas 1981-10-13 Issued Date 10/13/81 Expired Date Acres 0078300 Tool Type RTF Proposed Formation 2ND BEREA Proposed Depth 00000 Proposed Drill Depth 00000
CO 1984-05-23 467 BRASEL R GENE GeoDate 5/23/84
Oil and Gas 1984-05-23 Issued Date 5/23/84 Expired Date 11/19/84 Acres 0078360 Tool Type RTF Proposed Formation BEREA Proposed Depth 01887 Proposed Drill Depth 01887
Original Spud 1984-06-29 R.I. 5-26-84
Completed 1984-07-03 R.I. 5-26-84
Reached Total Depth 1984-07-03 R.I. 5-26-84
Completion Report Received 1984-08-14 R.I. 5-26-84
Construction Permit Expires 1984-11-19 R.I. 5-26-84
Change of Owner 2015-09-25 Operator changed from 467, BRASEL R GENE to 9548, R GENE BRASEL LLC
Change of Owner 2017-01-04 Operator changed from 9548, R GENE BRASEL LLC to 5155, HUFFMAN-BOWERS INC
Record Last Modified 2017-02-15 R.I. 5-26-84

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 1718 1746 0
1718 1746 0
2006-09-11 1793 1807 32
1793 1807 32
1718 1746 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2000 Bbl 38000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BRASEL R GENE 418.00 76.00 0
1985 BRASEL R GENE 2999.00 285.00 365
1986 BRASEL R GENE 2161.00 69.00 365
1987 BRASEL R GENE 1041.00 74.00 365
1988 BRASEL R GENE 1488.00 126.00 365
1990 BRASEL R GENE 1205.00 130.00 365
1991 BRASEL R GENE 1684.00 72.00 365
1993 BRASEL R GENE 1116.00 73.00 365
1994 BRASEL R GENE 1443.00 81.00 365
1995 BRASEL R GENE 1243.00 77.00 365
1996 BRASEL R GENE 957.00 63.00 365
1998 BRASEL R GENE 44.00 0.00 365
1999 BRASEL R GENE 698.00 76.00 365
2000 BRASEL R GENE 769.00 0.00 365
2001 BRASEL R GENE 677.00 0.00 365
2002 BRASEL R GENE 596.00 59.00 365
2003 BRASEL R GENE 715.00 59.00 365
2004 BRASEL R GENE 522.00 0.00 365
2005 BRASEL R GENE 422.00 77.00 365
2006 BRASEL R GENE 411.00 53.00 365
2007 BRASEL R GENE 468.00 0.00 365
2008 BRASEL R GENE 498.00 57.00 365
2009 BRASEL R GENE 309.00 48.00 365
2010 BRASEL R GENE 0.00 0.00 365
2011 BRASEL R GENE 491.00 0.00 0
2012 BRASEL R GENE 547.00 63.00 358
2013 BRASEL R GENE 151.00 61.00 365
2014 BRASEL R GENE 705.00 0.00 350
2015 R GENE BRASEL LLC 91.00 55.00 365
2016 HUFFMAN-BOWERS INC 686.00 43.00 365
2017 HUFFMAN-BOWERS INC 534.00 0.00 365
2018 HUFFMAN-BOWERS INC 589.00 91.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BRASEL R GENE Brine 0 0
1985 BRASEL R GENE Brine 0 365
1986 BRASEL R GENE Brine 34 365
1987 BRASEL R GENE Brine 0 365
1988 BRASEL R GENE Brine 0 365
1990 BRASEL R GENE Brine 0 365
1991 BRASEL R GENE Brine 0 365
1993 BRASEL R GENE Brine 0 365
1994 BRASEL R GENE Brine 0 365
1995 BRASEL R GENE Brine 0 365
1996 BRASEL R GENE Brine 0 365
1998 BRASEL R GENE Brine 0 365
1999 BRASEL R GENE Brine 365
2000 BRASEL R GENE Brine 0 365
2001 BRASEL R GENE Brine 0 365
2002 BRASEL R GENE Brine 0 365
2003 BRASEL R GENE Brine 0 365
2004 BRASEL R GENE Brine 0 365
2005 BRASEL R GENE Brine 0 365
2006 BRASEL R GENE Brine 12 365
2007 BRASEL R GENE Brine 0 365
2008 BRASEL R GENE Brine 2 365
2009 BRASEL R GENE Brine 6 365
2010 BRASEL R GENE Brine 0 365
2011 BRASEL R GENE Brine 0
2012 BRASEL R GENE Brine 1 358
2013 BRASEL R GENE Brine 1 365
2014 BRASEL R GENE Brine 0 350
2015 R GENE BRASEL LLC Brine 1 365
2016 HUFFMAN-BOWERS INC Brine 0 365
2017 HUFFMAN-BOWERS INC Brine 0 365
2018 HUFFMAN-BOWERS INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1629540775 2004-2-13 0:00: PW No Violations
1364309431 2013-03-25 UrbanProduction Wells Violations Noted Wellhead and tank battery identification signs comply with production well and tank battery requirements. However Gallia County is considered an urban township based on 2010 US population census. I have provided with this compliance notice the urban regulations information necessary to complete the following tasks in order to conform to the Urban population rules. This well and its tank battery identification signs do not meet the following requirements: 1501:9-9-05E1/1509:3D. Under urban rules signs must meet a certain standard different from normal production wells and tank batteries. Signs must be attached to required fencing. Fences are missing around the wellhead/ pumping unit apparatus, which consists of a pumping unit and associated two-inch production plumbing coming from the wellhead, and tank battery, which consists of two 100-barrel tanks, an oil/gas separator, and a couple of small knock out tanks. According to 1501:9-9-05E2/1509:03D, fencing specifications must be followed surrounding the tank battery and wellheads. Tanks must also be checked to ensure they are in compliance with 1501:9-9-05E4/1509:03D. Locks must be place where specified according to the regulation 1501:9-9-05E3/1509:03D. Wellhead is leaking gas at the wellhead packing between the intermediate casing and the production tubing. The PhD6 measured 0.45 meter reading units of methane, CH4. According to 1501:9-9-05(A)1/1509:20, owner shall repair or replace equipment to prevent the escape of oil and/or gas. Examination of the tank battery revealed there are two breeches in the dike wall that would permit the escape of oil, brine or other wastes from the containment area in the tank battery.
1369946885 2013-05-30 Production Wells No Violations The operator has corrected the leak at the wellhead. The operator has also beefed up the dike walls around the tank battery.
1378991570 2013-04-25 Production Wells No Violations Operator has reported 2012 production for this well. Violation is closed.
1446867771 2013-06-17 Production Wells Violations Noted This well is currently not producing. According to 1501:NONE_ /1509:.062A if there is no production, the well shall be plugged or placed in temporary inactive status until production problems have been resolved. This well was also initially cited Urban Rules violations. These violations have been removed at this time
1629540775 2004-02-13 Production Wells No Violations Could not locate after lenghty thorough search. Will ask company to take me to the well.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1364309431 US-OH-110679 2013-04-19 Well insufficiently equipped to prevent escape of oil and gas
1364309431 US-OH-110680 2013-04-19 Dike or pit not able to prevent escape of brine or other wastes
1446867771 US-OH-112983 2013-10-09 Nonproduction; well shall be plugged or placed in temporary inactive status
1446867771 US-OH-112984 2014-04-23 ID (a-i)
1446867771 US-OH-112985 2014-04-23 FENCING (a-d)
1446867771 US-OH-112986 2014-04-23 LOCKS
1446867771 US-OH-112987 2014-04-23 TANKS (a-i)
1446867771 US-OH-112988 2014-04-23 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[9]

References