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Well ID: 34-055-21423 | Loading map...
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Country: United States | |
State: Ohio | |
County: Geauga | |
Municipality: Burton Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: HAUTER UNIT | |
License Status: Producing | |
License Date: 1986-11-24 | |
Spud Date: 1987-10-20 | |
Spud Drilling Contractor: | |
Final Drill Date: 1987-10-25 | |
Well Total Depth: 4060.00 ft | |
Configuration: Vertical | |
Latitude: 41.450000 | |
Longitude: -81.190000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1986-11-24 | 213 LOMAK OPERATING CO GeoDate 11/24/86 |
Oil and Gas | 1986-11-24 | Issued Date 11/24/86 Expired Date 11/24/87 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1987-10-20 | RL 9-26-87, GL=1181.7, KB=1189.7 |
Completed | 1987-10-25 | RL 9-26-87, GL=1181.7, KB=1189.7 |
Reached Total Depth | 1987-10-25 | RL 9-26-87, GL=1181.7, KB=1189.7 |
Construction Permit Expires | 1987-11-24 | RL 9-26-87, GL=1181.7, KB=1189.7 |
Change of Owner | 2000-06-27 | Operator changed from 213, RANGE OPERATING COMPANY to 6674, GREAT LAKES ENERGY PTNSHP LLC |
Change of Owner | 2010-08-25 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
Change of Owner | 2017-05-01 | Operator changed from 7578, ENERVEST OPERATING LLC, to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2017-05-01 | RL 9-26-87, GL=1181.7, KB=1189.7 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3884 | 3920 | 3 |
3884 | 3920 | 3 | |
3884 | 3920 | 3 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 60000 Gal | 40000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-124207637 | 2014-1-9 0:00:0 | PW | No Violations | |
-370458925 | 2006-6-28 0:00: | PW | No Violations | |
-521268015 | 2010-12-20 0:00 | PW | No Violations | |
-566546014 | 2008-4-14 0:00: | PW | No Violations | |
0124207637 | 2014-01-09 | Production Wells | No Violations | My inspection found the well to be equipped with a plunger lift unit. The well and tank battery are in good repair and are surrounded by a chain link fence. The tank battery consists of a 100 BBL production tank and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. |
0370458925 | 2006-06-28 | Production Wells | Violations Noted | line leak company shut well in well in hauter sand and gravel mine operator could have hit line company has their legal working on problem.
Case #06-005 |
0521268015 | 2010-12-20 | Production Wells | No Violations | 100BBl steel tank in the battery and a mechanical separator. Location had 1.5 feet of snow on the ground. |
0566546014 | 2008-04-14 | Production Wells | No Violations | Tom Hill and I performed a random field inspection. The ID sign was posted and the tank battery was in good shape. I found no violations at this time. |
1240858129 | 2006-06-28 | Production Wells | Violations Noted | FOLLOW UP TO NOV # -370458925 line leak company shut well in well in hauter sand and gravel mine operator could have hit line company has their legal working on problem.
Case #06-005 line leak company shut well in well in hauter sand and gravel mine operator could have hit line company has their legal working on problem Case number 06-005 |
1671784753 | 2006-07-06 | Production Wells | No Violations | inspected site for well shut in and found leaking line company talking to hauter sand and gravel to expose line and possible replaced the line. |
1929810145 | 2007-07-26 | Production Wells | No Violations | Well is in production. Contacted John Flemming from Great Lakes, Mr. Haueter has replaced line and re-routed it. Old line that is exposed in the pit is no longer in use. Tank battery and well head are fenced. Tank battery is signed. |
1951946954 | 2008-04-14 | Production Wells | No Violations | Well head and tank battery are in good repair. Spacing is good. Permit sign is up and in good repair. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0370458925 | US-OH-123916 | 2006-07-07 | Well insufficiently equipped to prevent escape of oil and gas | |
1240858129 | US-OH-106422 | 2006-07-07 | Well insufficiently equipped to prevent escape of oil and gas |
For data sources see[9]