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Well ID: 34-157-25465 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Oxford Township | |
Operator Name: KIMBLE COMPANY | |
Well Pad ID: | |
Farm/Lease Name: GENERAL CLAY (SWIW #12) | |
License Status: Well Drilled | |
License Date: 2014-03-26 | |
Spud Date: 2010-12-27 | |
Spud Drilling Contractor: WARREN DRLG | |
Final Drill Date: 2011-01-23 | |
Well Total Depth: 8720.00 ft | |
Configuration: Vertical | |
Latitude: 40.280000 | |
Longitude: -81.580000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2010-11-17 | Proposed Formations:CLINTON,ROSE RUN, BEEKMANTOWN, MT. SIMON, Issued Date:11/17/2010, Expired Date:11/16/2012 12:00:00 PM, Drilling unit acres:174.62, Proposed Well Type:OG, Proposed Well Class:EDPW |
Reached Total Depth | 2011-01-23 | CHRIS KIMBLE STATED THE WELL WAS TREATED WITH NO RESULTS. THEY ARE IN TALKS WITH TOM TOMASTIK ABOUT CONVERTING TO STORAGE WELL. 1/31/2012 JG |
Completion Report Received | 2011-12-20 | CHRIS KIMBLE STATED THE WELL WAS TREATED WITH NO RESULTS. THEY ARE IN TALKS WITH TOM TOMASTIK ABOUT CONVERTING TO STORAGE WELL. 1/31/2012 JG |
Change of Owner | 2013-12-02 | Operator changed from 168, RHDK OIL & GAS LLC/DBA RED HIL to 9207, KIMBLE COMPANY |
APP | 2014-03-26 | Proposed Formations:ROSE RUN-MT. SIMON, Issued Date:3/26/2014, Expired Date:3/25/2016 12:00:00 PM, Drilling unit acres:174.62, Proposed Well Type:SWD, Proposed Well Class:SWIW |
Last Compliance Report | 2014-03-27 | CHRIS KIMBLE STATED THE WELL WAS TREATED WITH NO RESULTS. THEY ARE IN TALKS WITH TOM TOMASTIK ABOUT CONVERTING TO STORAGE WELL. 1/31/2012 JG |
Record Last Modified | 2015-09-24 | CHRIS KIMBLE STATED THE WELL WAS TREATED WITH NO RESULTS. THEY ARE IN TALKS WITH TOM TOMASTIK ABOUT CONVERTING TO STORAGE WELL. 1/31/2012 JG |
Construction Permit Expires | 2016-03-25 | CHRIS KIMBLE STATED THE WELL WAS TREATED WITH NO RESULTS. THEY ARE IN TALKS WITH TOM TOMASTIK ABOUT CONVERTING TO STORAGE WELL. 1/31/2012 JG |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2012-01-31 | 7075 | 8720 | 0 |
7075 | 8720 | 0 | |
7075 | 8720 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2011-07-07 | H2O | 15 | 292908 Gal | 0 | Halliburton | ACID: 3000 GAL 15% HCL |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1089907274 | 2016-3-3 0:00:0 | SW | No Violations | |
-1125565052 | 2016-8-31 0:00: | SW | No Violations | |
-1227491291 | 2017-4-7 0:00:0 | SW | No Violations | |
-1318593172 | 2019-12-12 0:00 | SW | No Violations | |
-1658024790 | 2016-2-22 0:00: | SW | No Violations | |
-1691504217 | 2018-7-5 0:00:0 | SW | No Violations | |
-1745646240 | 2020-4-15 0:00: | SW | No Violations | |
-1818092706 | 2016-9-12 0:00: | PL | No Violations | |
-202718901 | 2017-1-4 0:00:0 | SW | No Violations | |
-2065190301 | 2019-11-4 0:00: | SW | No Violations | |
-206865906 | 2016-10-18 0:00 | SW | No Violations | |
-2093646206 | 2017-11-14 0:00 | SW | No Violations | |
-2105222709 | 2018-4-3 0:00:0 | SW | No Violations | |
-436310550 | 2018-4-22 0:00: | SW | No Violations | |
-531467519 | 2017-9-20 0:00: | SW | No Violations | |
-53685333 | 2016-2-25 0:00: | SW | No Violations | |
-615325652 | 2019-7-10 0:00: | SW | No Violations | |
-749265119 | 2016-9-16 0:00: | SW | No Violations | |
-811855281 | 2020-7-10 0:00: | SW | No Violations | |
-855050457 | 2019-6-20 0:00: | SW | No Violations | |
-906904508 | 2016-5-16 0:00: | SW | No Violations | |
0037454414 | 2016-09-19 | Salt Water Injection Well | No Violations | Frontz drilling on site to install two water monitoring wells in area of proposed facility construction one will be on east side and one on the west side approximately 500 distance in both directions. |
0053685333 | 2016-02-25 | Salt Water Injection Well | No Violations | Inspection today revealed that owner has tubing and mud pump on site preparing to perform required work on said well, in conversation with Chris Kemble stating that they were waiting on float device to be built by Allied Machine it should be on site by the first of next week. |
0094049289 | 2016-02-11 | Salt Water Injection Well | No Violations | Inspection revealed that company personnel on site with equipment to prepare site for service rig to perform setting of bottom hole plug across the Mt. Simon formation and then they plan on testing well for feasibility for SWIW well. |
0144513723 | 2017-11-06 | Salt Water Injection Well | No Violations | No activity at the site today due to extreme wet weather. |
0156237074 | 2016-03-11 | Salt Water Injection Well | No Violations | On site to witness rig crew tag up at 8625 they cleaned up well bore and then pulled out of hole and remove BHA assembly and then run tubing back in hole to 7000 and they will run remaining tubing in hole on Monday to set bottom hole plug as required on permit conditions. |
0173349271 | 2019-03-19 | Salt Water Injection Well | No Violations | Inspection today revealed that well is currently not in operation and the division is still waiting on facility construction.
Positive pressure needs to be applied to annulus of tubing. |
0202718901 | 2017-01-04 | Salt Water Injection Well | No Violations | Inspection today indicated that well is not in operation,owner is waiting on contractors to start work on disposal site in the near future. |
0206865906 | 2016-10-18 | Salt Water Injection Well | No Violations | Well not in operation at this time,owner is planning on starting construction in the near future. |
0256234025 | 2018-08-07 | Salt Water Injection Well | No Violations | Still waiting on owner to start facility construction.
|
0263961039 | 2017-04-20 | Salt Water Injection Well | No Violations | Inspection today revealed that there has been no change in status of well they are still waiting on construction of perminant facility construction to begin. |
0286713515 | 2018-01-16 | Salt Water Injection Well | No Violations | Waiting on facility construction to begin. |
0424097400 | 2018-03-12 | Salt Water Injection Well | No Violations | No change in status of well it is still waiting on construction plan to be submitted. |
0436310550 | 2018-04-22 | Salt Water Injection Well | No Violations | Inspection revealed that we are still waiting on owner to begin facility construction in conversation with owner they stated that they plan on starting on project within the next 30-60 day time frame. |
0531467519 | 2017-09-20 | Salt Water Injection Well | No Violations | On site today to witness changing out of faulty tubing head,Bakerwell Services provided rig for change out of tubing head tubing head was replaced with a 3000 # Lowry head equipped with three seal assemblys and once head was secured we performed a 1720 psi integrity test which passed with no pressure decline. |
0607175780 | 2019-03-08 | Preliminary Restoration | No Violations | Restoration work at site is satisfactory.
Annulus pressure needs to be applied. |
0636579804 | 2015-12-28 | Salt Water Injection Well | No Violations | No activity at the site, talked to Chris Kimble and discussed plug back operations and future plans for said well. |
0645012128 | 2016-03-31 | Salt Water Injection Well | No Violations | Start Baker A -3 set lock packer in hole 3.5 tubing and packer is equipped with a on/off tool above packer and there is one 30 joint of tubing under the packer. |
0749265119 | 2016-09-16 | Salt Water Injection Well | No Violations | Inspection today revealed that third party contractor on site to perform radiology survey of site and mark two location for two ground water monitoring wells to be drilled next week for the purpose of background analytical of present ground water conditions. |
0853600653 | 2018-05-30 | Salt Water Injection Well | No Violations | Inspection revealed that there is no current activity at the site. |
0906904508 | 2016-05-16 | Salt Water Injection Well | No Violations | Inspection revealed that there was no activity at the site today, company is waiting on approval from the division to start construction on there facility and new flow line to wellhead which will be double encased. |
0955425523 | 2018-12-30 | Salt Water Injection Well | No Violations | Inspection revealed that owner still has not started construction of the facility. |
1038376120 | 2019-10-7 0:00: | SW | No Violations | |
1089907274 | 2016-03-03 | Salt Water Injection Well | No Violations | Inspection today revealed that company owned service rig on site running tubing in well to remove obstruction from wellbore at approximately 7300. |
1125565052 | 2016-08-31 | Salt Water Injection Well | No Violations | Facility still under construction and they plan on starting construction in the near future and hope to have well up and in operation by early next year. |
1145302261 | 2017-07-18 | Salt Water Injection Well | No Violations | No activity at site still waiting on owner to build facility and place flowline to well. |
1151152528 | 2016-03-14 | Salt Water Injection Well | No Violations | On site to witness Halliburton set bottom hole plug they ran 105 sacks of Densecem with a weight of16.8 ppg and displaced it to bottom with 43 bbl of water and then operator pulled string up into 5.5 casing and we will tag plug next Monday to confirm cement top.
Note: Plug bottom @8625 and calculated top@8350 will confirm top next week. |
1227491291 | 2017-04-07 | Salt Water Injection Well | No Violations | Inspection today revealed that well is currently waiting on construction of facility to begin. |
1230686993 | 2017-11-02 | Salt Water Injection Well | No Violations | Inspection revealed that we are still waiting on construction to begin on facility . |
1243300770 | 2016-03-30 | Salt Water Injection Well | No Violations | On site along with local inspector for cross training ,Baker Well services on site with wire line truck to perform required spinner test on open section of well bore to confirm which potential injection zone was receiving water the log indicated that the majority of fluid was going into the Rose Run section and minimal was going in to the Rome section of the well bore.
Note: Baker Hughes pump truck pumped at a rate of five barrel per minute with a pressure of 200-600 psi. |
1293541140 | 2017-05-04 | Salt Water Injection Well | No Violations | On site to witness MIT testing of said well they applied 1700 psi to annulus and we monitored it for 15 minutes with no decline in pressure(TEST PASSED). |
1306245776 | 2011-03-03 | Drill / Deepen / Reopen | No Violations | Arrived on location for pit solidification. |
1381149517 | 2013-10-07 | Preliminary Restoration | No Violations | |
1391622150 | 2014-02-05 | Production Wells | No Violations | On site to inspect location of proposed SWIW well tank/pumphouse site and to look over wellhead area to check for any potential problems with converting well to injection well,there were no water wells located within 500 of either site and after revewing owners plan it all appeared to be OK. |
144513723 | 2017-11-6 0:00: | SW | No Violations | |
1457040437 | 2016-03-02 | Salt Water Injection Well | No Violations | Inspection today revealed that company owned service rig was on site and running 2.875 tubing in hole. |
1458243968 | 2016-03-15 | Preliminary Restoration | No Violations | Restoration work at site is satisfactory pits have been filled in and vegetation has been established. |
1458586388 | 2016-03-21 | Salt Water Injection Well | No Violations | On site to witness company owned service rig run in hole to confirm cement top they sat down at 8415 called central office to get approval for owner to continue with completing well. |
1460139440 | 2016-04-07 | Salt Water Injection Well | No Violations | On site again today to witness rig crew run Baker packer and 3.5 tubing in well to a setting depth of 7041 center of elements and attempt to perform MIT testing after several failed attempts pressure testing it was decided to repack tubing head and try again and it passed, we tested at 1775 psi and monitored pressure for 15 minutes with no decline in pressure.
Note: Annular was calculated at 80 bbl. and the added seven gallon of inhibitor. |
1461102717 | 2016-04-15 | Salt Water Injection Well | No Violations | On site to witness pressure fall off testing, Baker Hughes had two pump trucks on location and there was 4000 bbl. of water on site for testing purposes. |
1469646713 | 2016-07-25 | Salt Water Injection Well | No Violations | No activity at site today according to well owner they plan on starting construction of facility in the near future. |
1515707081 | 2018-01-05 | Salt Water Injection Well | No Violations | Waiting on owner to submit facility plan for construction. |
1522078717 | 2018-03-23 | Salt Water Injection Well | No Violations | On site with company personnel to apply positive pressure to annulus of tubing after replacing 2 valve that failed during the extreme cold weather season.
|
1531515257 | 2018-07-10 | Salt Water Injection Well | No Violations | Inspection revealed that owner is still waiting on facility construction to begin. |
156237074 | 2016-3-11 0:00: | SW | No Violations | |
1568497278 | 2019-9-9 0:00:0 | SW | No Violations | |
1591640666 | 2020-6-8 0:00:0 | SW | No Violations | |
1594837355 | 2020-7-13 0:00: | SW | No Violations | |
1619676439 | 2019-04-03 | Salt Water Injection Well | No Violations | Noted that trees beside of lease road to wellhead have been recently cut down owner claims they are preparing to start construction of facility in the near future. |
1658024790 | 2016-02-22 | Salt Water Injection Well | No Violations | Inspection today revealed that company owned service rig on site and I witnessed then run wireline tool in well to check total depth but they sat down on obstruction at 7250 and after determining that they could not get any deeper decision was made to pull tools from hole and prepare to run 2.875 tubing in hole to clear a path to the bottom of the well bore. |
1673860685 | 2013-10-16 | Preliminary Restoration | No Violations | On the day of my inspection I witnessed that well identification was in place and erosion problems have been addressed. |
1691504217 | 2018-07-05 | Salt Water Injection Well | No Violations | Waiting on facility construction to begin. |
173349271 | 2019-3-19 0:00: | SW | No Violations | |
1818092706 | 2016-09-12 | Preliminary Restoration | No Violations | Restoration work at site satisfactory, and it was noted that owner has had a contractor come in and install bridge deck on bridge that we cross while entering site. |
1869665882 | 2017-03-24 | Salt Water Injection Well | No Violations | No activity at the site they are still waiting on construction of facility to begin. |
1882628799 | 2017-06-21 | Salt Water Injection Well | No Violations | Still waiting on facility construction to begin. |
1921266717 | 2017-01-26 | Salt Water Injection Well | No Violations | Inspection today revealed that company personnel were on site constructing new steel gate at the entrance to the site, construction of the pump house and placement of flowline is too start in the near future. |
1945654882 | 2017-09-25 | Salt Water Injection Well | No Violations | Waiting on contractor to start clearing area for upcoming facility construction. |
204888619 | 2020-7-13 0:00: | SW | No Violations | |
2093646206 | 2017-11-14 | Salt Water Injection Well | No Violations | No activity noted at the site at this time. |
2105222709 | 2018-04-03 | Salt Water Injection Well | No Violations | Inspection today indicated that there is no activity at the site at this present time. |
2123180448 | 2016-08-16 | Salt Water Injection Well | No Violations | Inspection today revealed that there is no activity at the site they just received approval for there facility construction and they hope to start work at the site in the near future. |
256234025 | 2018-8-7 0:00:0 | SW | No Violations | |
263961039 | 2017-4-20 0:00: | SW | No Violations | |
286713515 | 2018-1-16 0:00: | SW | No Violations | |
37454414 | 2016-9-19 0:00: | SW | No Violations | |
424097400 | 2018-3-12 0:00: | SW | No Violations | |
607175780 | 2019-3-8 0:00:0 | PL | No Violations | |
636579804 | 2015-12-28 0:00 | SW | No Violations | |
645012128 | 2016-3-31 0:00: | SW | No Violations | |
757770434 | 2019-11-25 0:00 | SW | No Violations | |
853600653 | 2018-5-30 0:00: | SW | No Violations | |
94049289 | 2016-2-11 0:00: | SW | No Violations | |
955425523 | 2018-12-30 0:00 | SW | No Violations |
For data sources see[5]