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Well ID: 34-077-20182 | Loading map...
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Country: United States | |
State: Ohio | |
County: Huron | |
Municipality: Fitchville Township | |
Operator Name: ORPHAN WELL PROGRAM | |
Well Pad ID: | |
Farm/Lease Name: CRECELIUS-LORCHER | |
License Status: Final Restoration | |
License Date: 2011-07-28 | |
Spud Date: 1985-10-25 | |
Spud Drilling Contractor: BOB HUWER DRLG | |
Final Drill Date: 1985-10-28 | |
Well Total Depth: 930.00 ft | |
Configuration: Vertical | |
Latitude: 41.110000 | |
Longitude: -82.510000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1985-10-15 | 2010 COMGAS INC GeoDate 10/15/85 |
Oil and Gas | 1985-10-15 | Issued Date 10/15/85 Expired Date 10/15/86 Acres 0094170 Tool Type RTAF Proposed Formation SYLVANIA Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1985-10-25
I&O CN 2008 11 052 | |
Completed | 1985-10-28
I&O CN 2008 11 052 | |
Reached Total Depth | 1985-10-28
I&O CN 2008 11 052 | |
CO | 1993-10-22 | 4122 GEMINI ENERGY INC GeoDate 10/15/85 |
APP | 2003-09-12 | Proposed Formations:SYLVANIA, Issued Date:9/12/2003, Expired Date:9/11/2004 6:00:00 AM, Drilling unit acres:94.17, Proposed Well Type:OG, Proposed Well Class: |
APP | 2011-07-28 | Proposed Formations:BIG LIME, Issued Date:7/28/2011, Expired Date:7/27/2013 12:00:00 PM, Drilling unit acres:94.17, Proposed Well Type:OG, Proposed Well Class: |
Plugged by Orphan Well Program | 2012-04-05 | Plugged by Orphan Well Program |
Plugged/Abandoned | 2012-04-05
I&O CN 2008 11 052 | |
Construction Permit Expires | 2013-07-27
I&O CN 2008 11 052 | |
Record Last Modified | 2015-09-24
I&O CN 2008 11 052 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2003-09-12 | 876 | 880 | 5 |
876 | 880 | 5 | |
876 | 880 | 5 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 0 | 0 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1739612785 | 2004-12-8 0:00: | PW | No Violations | |
-1771299879 | 2012-4-2 0:00:0 | PB | No Violations | |
-1964403009 | 2008-4-23 0:00: | PW | No Violations | |
-28930678 | 2006-3-8 0:00:0 | PW | No Violations | |
-303945979 | 2005-11-23 0:00 | PW | No Violations | |
000PL14924 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0028930678 | 2006-03-08 | Production Wells | No Violations | Inspect well. Collect photos of well head. Production casing has rusted off. Incapable of production. |
0303945979 | 2005-11-23 | Production Wells | No Violations | Inspect Well. No ID. Gas Well; the well head has rusted away and fallen to the ground. Open hole. Incapable of production. |
0957477938 | 2012-04-17 | Final Restoration | No Violations | Inspect location. Final restoration complete. Filed has been planted. |
1304527027 | 2011-05-02 | Orphan | No Violations | Wellhead has rotted off. Appears to be no significant gas coming from well casing. |
1474845492 | 2003-04-03 | Production Wells | No Violations | Inspect well. 8 conductor, 4 casing reduced to 2 with valve and tee, valve closed, and cap. No pipe run. No ID. Incapable of production. No pump jack. 4 casing is heavily rusted where the pipe is inside the 8 conductor. |
1605091856 | 2012-04-05 | Plug / Plug Back | No Violations | Plug well, fill borehole with 9 sac grout to surface. Attempt to rip 4.5 inch casing from top of cement at 450 ft to surface to verify 4.5 inch casing was cemented to surface when well was constructed. |
1739612785 | 2004-12-08 | Production Wells | No Violations | INSPECT WELL. THE 4 INCH LONGSTRING HAS ENTIRELY RUSTED AWAY CAUSING THE WELL HEAD TO COLLAPSE. OPEN HOLE. NO IDENTIFICATION. WELL SHOULD BE PLUGGED ASAP. |
1771299879 | 2012-04-02 | Plug / Plug Back | No Violations | Set bottom plug with 50/50 poz. |
1964403009 | 2008-04-23 | Production Wells | No Violations | Inspect well. The well head has rusted off. Open hole. 4 inch long string is rusted off. 7 inch casing rusted off. Leaking gas. |
957477938 | 2012-4-17 0:00: | FR | No Violations | |
PL14924 | PL | No Violations |
For data sources see[5]