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Well ID: 34-163-20340 | Loading map...
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Country: United States | |
State: Ohio | |
County: Vinton | |
Municipality: Knox Township | |
Operator Name: CLEARWATER OPERATIONS LLC | |
Well Pad ID: | |
Farm/Lease Name: PERRY ORVILLE | |
License Status: Producing | |
License Date: 1967-07-06 | |
Spud Date: 1967-10-02 | |
Spud Drilling Contractor: | |
Final Drill Date: 1967-11-23 | |
Well Total Depth: 1157.00 ft | |
Configuration: Vertical | |
Latitude: 39.210000 | |
Longitude: -82.310000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1967-10-02 | |
Completed | 1967-11-23 | |
Reached Total Depth | 1967-11-23 | |
CO | 1987-02-10 | 566 GRIM PAUL A |
Change of Owner | 2001-11-21 | Operator changed from 566, GRIM PAUL A to 5755, CHIEFTAIN ENERGY CORP. |
Change of Owner | 2011-04-21 | Operator changed from 5755, CHIEFTAIN ENERGY CORP to 6227, HOUGHTON INVESTMENTS, L.L.C. |
Change of Owner | 2016-08-01 | Operator changed from 6227, HOUGHTON INVESTMENTS LLC to 7077, D T ATHA INC |
Change of Owner | 2018-07-31 | Operator changed from 7077, RIVER VALLEY ENERGY INC to 10184, CLEARWATER OPERATIONS LLC |
Record Last Modified | 2018-07-31 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1147 | 1157 | 0 |
1147 | 1157 | 0 | |
1147 | 1157 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 20 Qts | 0 | A.S. 10-BO & 1 BW PER 24 HRS., EST. 75MCFG/AS |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | ISON PROD SERVICES INC | 0.00 | 799.00 | 320 |
1987 | GRIM PAUL A | 0.00 | 127.00 | 365 |
1988 | GRIM PAUL A | 0.00 | 146.00 | 365 |
1989 | GRIM PAUL A | 0.00 | 86.00 | 365 |
1990 | GRIM PAUL A | 0.00 | 37.00 | 365 |
1991 | GRIM PAUL A | 0.00 | 100.00 | 365 |
1992 | GRIM PAUL A | 0.00 | 68.00 | 365 |
1993 | GRIM PAUL A | 0.00 | 0.00 | 365 |
1994 | GRIM PAUL A | 0.00 | 0.00 | 365 |
1995 | GRIM PAUL A | 0.00 | 21.00 | 365 |
1996 | GRIM PAUL A | 0.00 | 0.00 | 365 |
1997 | GRIM PAUL A | 0.00 | 68.00 | 365 |
1998 | GRIM PAUL A | 0.00 | 0.00 | 365 |
1999 | GRIM PAUL A | 0.00 | 0.00 | 365 |
2000 | GRIM PAUL A | 0.00 | 0.00 | 365 |
2001 | GRIM PAUL A | 0.00 | 0.00 | 365 |
2002 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2003 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2004 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2005 | HOCKING HILLS ENERGY AND WELL | 0.00 | 15.00 | 365 |
2006 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2007 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2008 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2009 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2010 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2011 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2012 | HOUGHTON INVESTMENTS LLC | 0.00 | 168.00 | 366 |
2013 | HOUGHTON INVESTMENTS LLC | 0.00 | 127.00 | 365 |
2014 | HOUGHTON INVESTMENTS LLC | 0.00 | 11.00 | 365 |
2015 | HOUGHTON INVESTMENTS LLC | 0.00 | 109.00 | 365 |
2016 | HOUGHTON INVESTMENTS LLC | 0.00 | 33.00 | 365 |
2017 | RIVER VALLEY ENERGY INC | 0.00 | 147.00 | 365 |
2018 | RIVER VALLEY ENERGY INC | 0.00 | 99.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | ISON PROD SERVICES INC | Brine | 3200 | 320 |
1987 | GRIM PAUL A | Brine | 1193 | 365 |
1988 | GRIM PAUL A | Brine | 1389 | 365 |
1989 | GRIM PAUL A | Brine | 1011 | 365 |
1990 | GRIM PAUL A | Brine | 118 | 365 |
1991 | GRIM PAUL A | Brine | 1178 | 365 |
1992 | GRIM PAUL A | Brine | 345 | 365 |
1993 | GRIM PAUL A | Brine | 0 | 365 |
1994 | GRIM PAUL A | Brine | 0 | 365 |
1995 | GRIM PAUL A | Brine | 80 | 365 |
1996 | GRIM PAUL A | Brine | 0 | 365 |
1997 | GRIM PAUL A | Brine | 270 | 365 |
1998 | GRIM PAUL A | Brine | 0 | 365 |
1999 | GRIM PAUL A | Brine | 0 | 365 |
2000 | GRIM PAUL A | Brine | 30 | 365 |
2001 | GRIM PAUL A | Brine | 0 | 365 |
2002 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2003 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2004 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2005 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 365 |
2006 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2007 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2008 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2009 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2010 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2011 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | |
2012 | HOUGHTON INVESTMENTS LLC | Brine | 1155 | 366 |
2013 | HOUGHTON INVESTMENTS LLC | Brine | 142 | 365 |
2014 | HOUGHTON INVESTMENTS LLC | Brine | 1608 | 365 |
2015 | HOUGHTON INVESTMENTS LLC | Brine | 3094 | 365 |
2016 | HOUGHTON INVESTMENTS LLC | Brine | 107 | 365 |
2017 | RIVER VALLEY ENERGY INC | Brine | 4629 | 365 |
2018 | CLEARWATER OPERATIONS LLC | Brine | 1651 | 153 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1751615899 | 2004-2-19 0:00: | PW | No Violations | |
-576373265 | 2005-8-19 0:00: | PW | No Violations | |
-58636183 | 2004-5-5 0:00:0 | PW | No Violations | |
0058636183 | 2004-05-05 | Production Wells | No Violations | Follow-up on NOV, Non-Compliance, well still idle, accordig to landowner well has not produced for several yrs, spoke with Doug Kitchen on 5-4-04, he has no plans of producing or plugging well. |
0086620270 | 2012-05-03 | Production Wells | No Violations | Permit numbers were still not on the identification tag or on the well head. I left a note with the proper permit numbers on the tank battery. |
0471147110 | 2012-11-01 | Production Wells | No Violations | Identification has been placed on the well. No other violations were observed. Well is in compliance. |
0527548238 | 2004-02-19 | Production Wells | Violations Noted | FOLLOW UP TO NOV # -1751615899 An inspection of the well revealed the well to be idle, according to landowner well has not produced for several years, no house gas being used. According to production statement no production on this well for several years. |
0576373265 | 2005-08-19 | Production Wells | No Violations | Took photographs. |
0744251782 | 2012-04-18 | Production Wells | No Violations | Well is equipped for production, and showed signs of pumping and production. Production records stated zero production for 2010. I spoke with Mr. Lee Atha on 4/19/12 and he stated that the well has been producing. |
0838992365 | 2005-11-22 | Production Wells | No Violations | Follow-up on Chiefs Order and NOV, IN-COMPLIANCE, well in production, house gas being used according to landowner. |
0994061043 | 2008-06-24 | Production Wells | No Violations | A follow-up inspection revealed non-compliance. Also noted was that a steel flowline, in the field, has parted. |
1272416519 | 2008-02-27 | Production Wells | No Violations | A complaint was received alleging non-production. An inspection revealed that this well is idle. The polishing rod shows signs of non-production. The belt for the motor was found missing. Records also indicate that the last year of production was 2005. A Chiefs Order had been issued on the Orlan and James Perry wells in 2004. This case will be handed over to Joe Hoerst. |
1660090738 | 2009-02-23 | Production Wells | No Violations | An inspection revealed that the well contains production equipment. Chieftain Energy has been instructed, on several occassions, to place the Perry wells back into production. The status of this well will be checked at a later date. |
1677204552 | 2005-01-06 | Production Wells | No Violations | Follow-up on NOV, Non-Compliance, well not producing, spoke with Doug Kitchen and explained to him that well must be producing in commercial quantities. |
1751615899 | 2004-02-19 | Production Wells | Violations Noted | An inspection of the well revealed the well to be idle, according to landowner well has not produced for several years, no house gas being used. According to production statement no production on this well for several years. |
471147110 | 2012-11-1 0:00: | PW | No Violations | 1.00 |
527548238 | 2004-2-19 0:00: | PW | No Violations | |
744251782 | 2012-4-18 0:00: | PW | No Violations | 0.50 |
838992365 | 2005-11-22 0:00 | PW | No Violations | |
86620270 | 2012-5-3 0:00:0 | PW | No Violations | 1.00 |
994061043 | 2008-6-24 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0527548238 | US-OH-125761 | 2004-02-20 | Well shall be plugged | |
1751615899 | US-OH-117399 | 2004-02-20 | Well shall be plugged |
For data sources see[9]