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Well ID: 34-059-22610 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Valley Township | |
Operator Name: YOUNGS CARLA E. | |
Well Pad ID: | |
Farm/Lease Name: YOUNGS JACK & SARAH | |
License Status: Final Restoration | |
License Date: 2003-08-20 | |
Spud Date: 1979-08-25 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1979-08-31 | |
Well Total Depth: 5394.00 ft | |
Configuration: Vertical | |
Latitude: 39.920000 | |
Longitude: -81.540000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1979-08-01 | 140 KST OIL & GAS CO INC GeoDate 8/1/79 |
Original Spud | 1979-08-25 | |
Completed | 1979-08-31 | |
Reached Total Depth | 1979-08-31 | |
CO | 1995-12-05 | 182 BELDEN & BLAKE CO GeoDate 8/1/79 |
CO | 1996-04-23 | 5431 YOUNGS CARLA E. GeoDate 8/1/79 |
Plugged/Abandoned | 2003-08-14 | |
APP | 2003-08-20 | Proposed Formations:CLINTON, Issued Date:8/20/2003, Expired Date:8/19/2004 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Construction Permit Expires | 2004-08-19 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1999-06-23 | 5166 | 5260 | 20 |
5166 | 5260 | 20 | |
5166 | 5260 | 20 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 162000 Gal | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | KST OIL & GAS CO INC | 7634.00 | 0.00 | 365 |
1985 | KST OIL & GAS CO INC | 5183.00 | 0.00 | 365 |
1986 | KST OIL & GAS CO INC | 5057.00 | 0.00 | 365 |
1987 | KST OIL & GAS CO INC | 2075.00 | 0.00 | 365 |
1988 | KST OIL & GAS CO INC | 2875.00 | 0.00 | 365 |
1989 | KST OIL & GAS CO INC | 1517.00 | 111.00 | 365 |
1990 | KST OIL & GAS CO INC | 721.00 | 0.00 | 365 |
1991 | KST OIL & GAS CO INC | 172.00 | 0.00 | 365 |
1992 | KST OIL & GAS CO INC | 436.00 | 0.00 | 365 |
1993 | KST OIL & GAS CO INC | 352.00 | 0.00 | 365 |
1994 | KST OIL & GAS CO INC | 166.00 | 0.00 | 365 |
1995 | KST OIL & GAS CO INC | 172.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1985 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1986 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1987 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1988 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1989 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1990 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1991 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1992 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1993 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1994 | KST OIL & GAS CO INC | Brine | 0 | 365 |
1995 | KST OIL & GAS CO INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-217891296 | 2004-1-26 0:00: | FR | No Violations | |
0217891296 | 2004-01-26 | Final Restoration | No Violations | FINAL RESTORATION |
0665143984 | 2003-08-12 | Plug / Plug Back | No Violations | EXPIDITE PERMIT TO PLUG. TIMCO ON HOLE SERVICING WELL.HOLE APPEARS TO BE IN CASING UP HOLE IN AREA OF COAL SEAM.4CASING APPEARS TO BE PARTED SOME WHERE DOWN HOLE. TIM BROWN IS CONCERNED ABOUT COMING OUT OF HOLE DUE TO THE CAVE FACTOR AND THE ABILITY TO GET BACK DOWN HOLE TO SET PLUS IF OWNER DECIDES TO PLUG WELL.WELL SUPPLIES GAS TO B.C.I. INDUSTRIES WITH GAS. PLANT IS LOCATED IN DERWENT, OHIO. 500 PLUG SET FROM 3684-3184 FORMATION CEMENT.MUD PUMP KEPT ON HOLE TO ASSURE CIRCULATION. |
1060875794 | 2003-08-14 | Plug / Plug Back | No Violations | WELL TOPPED OFF TODAY. 4400 PLUG SET. BOTTOM 8 PLUG TAGGED BEFORE PROCEEDING UP TO 400 PLUG. 95 SACKS CEMENT PUMPED ON SURFACE PLUG, PLUG STAYED ON TOP. |
1803993665 | 2003-08-12 | Plug / Plug Back | No Violations | EXPIDITE PERMIT TO PLUG. TIMCO INC. SERVICING WELL, APPEARS TO BE CAVING FROM HOLE IN CASING UP HOLE. HOLE IN SURFACE CASING DUE TO COAL SEAM MAY BE CAUSING DEBRIS TO FALL DOWN HOLE. 4 CASING APPEARS TO PARTED DOWN HOLE AT APPROXIMATELY 3800. METAL SHAVINGS AND CHUNKS OF RUST ARE BEING BROUGHT UP HOLE BY MUD PUMP. CALLED COLUMBUS OFFICE TO EXPIDITE PLUG PERMIT NOTIFIED JIM GLASS. TIM BROWN, CONCURRED ON THEORY IF TOOLS ARE PULLED OUT OF HOLE WE WOULD NOT BE ABLE TO GET BACK IN TO PLUG WELL AT A LATER DATE. FORMATION CEMENT CO. SET PLUG @ 3684-3184. |
665143984 | 2003-8-12 0:00: | PB | No Violations |
For data sources see[9]