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Well ID: 34-013-21186 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Somerset Township | |
Operator Name: GULFPORT APPALACHIA LLC | |
Well Pad ID: US-OH-001438 | |
Farm/Lease Name: STARR 210296 | |
License Status: Producing | |
License Date: 2017-02-22 | |
Spud Date: 2017-03-05 | |
Spud Drilling Contractor: H&P DRILLING | |
Final Drill Date: 2017-04-07 | |
Well Total Depth: 18987.00 ft | |
Configuration: Horizontal | |
Latitude: 39.900000 | |
Longitude: -81.220000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2017-02-22 | Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:2/22/2017, Expired Date:2/22/2019 12:00:00 PM, Drilling unit acres:508.713, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2017-04-07 | |
Completion Report Received | 2017-11-21 | |
Correction to Well | 2017-12-22 | UPDATE TARGET/TAKE/ACREAGE PER AS-DRILLED PLAT |
Construction Permit Expires | 2019-02-22 | |
Record Last Modified | 2019-06-07 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2017-11-20 | 9052 | 9197 | 50 |
2017-11-20 | 18667 | 18818 | 30 |
18667 | 18818 | 30 | |
9052 | 9197 | 50 | |
9052 | 9197 | 50 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 06/06/2017 | 07/07/2017 | 8659 | 17,403,900.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Sand (100 Mesh Proppant) | Muskie | Proppant | Silica Substrate | 14808-60-7 | 100 | 1.19296 | 2,271,270.0 |
NEFE-180 | Chemplex SOLVAY | Acid Inhibitor | Olefin | Trade Secret | 2.5 | 0.00002213 | 42.134 | |
2-Popyn-1-ol | 107-19-7 | 2.5 | 0.00002213 | 42.134 | ||||
Fatty acids, tall oil | 61790-12-3 | 2.5 | 0.00002213 | 42.134 | ||||
Aectic Acid | 64-19-7 | 55 | 0.000486868 | 926.946 | ||||
2-Ethylhexanol | 104-76-7 | 7.5 | 0.00006639 | 126.402 | ||||
Methanol | 67-56-1 | 25 | 0.000221304 | 421.339 | ||||
Alcohols, C14-15, Ethoxylated | 68951-67-7 | 2.5 | 0.00002213 | 42.134 | ||||
Coconut oil acid diethanolamine | 68603-42-9 | 2.5 | 0.00002213 | 42.134 | ||||
Hydrochloric Acid (28%) | Oxy | Acidizing | Water | 7732-18-5 | 64 | 0.0915024 | 174211 | |
Hydrochloric Acid (Hydrogen Chloride) | 7732-18-5 | 36 | 0.0514701 | 97993.6 | ||||
Other Chemical(s) | Listed Above | See Trade Name(s) List | Methanol | 67-56-1 | 25 | 0.000221304 | 421.339 | |
Ammonium Chloride ((NH4)Cl) | 12125-02-9 | 1 | 0.000873972 | 1663.95 | ||||
Water | 7732-18-5 | 75 | 0.0655479 | 124796 | ||||
Oleic Acid Diethanolamide | 93-83-4 | 2 | 0.00174794 | 3327.9 | ||||
2-Ethylhexanol | 104-76-7 | 7.5 | 0.00006639 | 126.402 | ||||
Alcohols, C12-16, Ethoxylated | 68551-12-2 | 2 | 0.00174794 | 3327.9 | ||||
Olefin | Trade Secret | 2.5 | 0.00002213 | 42.134 | ||||
Fatty acids, tall oil | 61790-12-3 | 2.5 | 0.00002213 | 42.134 | ||||
Ethanol | 64-17-5 | 3 | 0.000904532 | 1722.14 | ||||
Didecyl dimethyl Ammonium Chloride | 7173-51-5 | 5 | 0.00150755 | 2870.22 | ||||
Quatemary Ammonium Compunds, Benzyl-C12-C16-alkldimethyl,
Chlorides |
68424-85-1 | 5 | 0.00150755 | 2870.22 | ||||
2-Popyn-1-ol | 107-19-7 | 2.5 | 0.00002213 | 42.134 | ||||
Alcohols, C14-15, Ethoxylated | 68951-67-7 | 2.5 | 0.00002213 | 42.134 | ||||
Water | 7732-18-5 | 64 | 0.0915024 | 174211 | ||||
Water | 7732-18-5 | 57 | 0.0171861 | 32720.6 | ||||
Coconut oil acid diethanolamine | 68603-42-9 | 2.5 | 0.00002213 | 42.134 | ||||
Water | 7732-18-5 | 55 | 0.00716425 | 13640 | ||||
B2512 | Aquaserv | Biocide | Ethanol | 64-17-5 | 3 | 0.000904532 | 1722.14 | |
Water | 7732-18-5 | 57 | 0.0171861 | 32720.6 | ||||
Didecyl dimethyl Ammonium Chloride | 7173-51-5 | 5 | 0.00150755 | 2870.22 | ||||
Glutaraldehyde | 111-30-8 | 30 | 0.00904532 | 17221.3 | ||||
Quatemary Ammonium Compunds, Benzyl-C12-C16-alkldimethyl,
Chlorides |
68424-85-1 | 5 | 0.00150755 | 2870.22 | ||||
Water | Gulfport Energy Corporation | Carrier/Base Fluid | Water | 7732-18-5 | 100 | 76.2835 | 145,236,000.0 | |
SI-120 | Moon Chemical Products | Scale Inhibitor | Water | 7732-18-5 | 55 | 0.00716425 | 13640 | |
Phosphinocarboxylic Acid | 110224-99-2 | 45 | 0.00586166 | 11160 | ||||
Sand (40/70 Proppant) | Muskie | Proppant | Silica Substrate | 14808-60-7 | 100 | 8.78897 | 16,733,300.0 | |
Plexslick 920 | Chemplex SOLVAY | Friction Reducer | Ammonium Chloride ((NH4)Cl) | 12125-02-9 | 1 | 0.000873972 | 1663.95 | |
Oleic Acid Diethanolamide | 93-83-4 | 2 | 0.00174794 | 3327.9 | ||||
Petroleum Distillate | 69418-26-4 | 20 | 0.0174794 | 33279 | ||||
Water | 7732-18-5 | 75 | 0.0655479 | 124796 | ||||
Alcohols, C12-16, Ethoxylated | 68551-12-2 | 2 | 0.00174794 | 3327.9 | ||||
Production water | Gulfport Energy Corporation | Carrier/Base Fluid | Water | 7732-18-5 | 100 | 13.4602 | 25,626,800.0 |
For data sources see[4]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2017-07-07 | H2O | 15 | 285642 Gal | 275580 | STINGRAY PRESSURE PUMPING LLC | STAGE 54/54
STAGES 2-53 SEE IMAGES |
2017-06-05 | H2O | 15 | 437808 Gal | 500820 | STINGRAY PRESSURE PUMPING LLC | STAGE 1/54
STAGES 2-53 SEE IMAGES |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2017 | GULFPORT ENERGY CORPORATION | 2018121 | 393 | 147 |
2018 | GULFPORT ENERGY CORPORATION | 4389649 | 111 | 363 |
2019 | GULFPORT ENERGY CORPORATION | 739506 | 2 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2017 | GULFPORT ENERGY CORPORATION | Brine | 17295 | 147 |
2018 | GULFPORT ENERGY CORPORATION | Brine | 48022 | 363 |
2019 | GULFPORT ENERGY CORPORATION | Brine | 5153 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1291407315 | 2019-2-6 0:00:0 | PL | No Violations | 0.20 |
-1387600746 | 2017-5-11 0:00: | PL | No Violations | 1.00 |
-426682065 | 2020-10-19 0:00 | PW | No Violations | 0.20 |
-911870508 | 2017-12-6 0:00: | PW | No Violations | 1.00 |
0911870508 | 2017-12-06 | Production Wells | No Violations | This well is equipped with 5.5-inch diameter production casing. The well appears to be free flowing with no artificial lift technology present. There are gas processing units on this site. The production area currently contains four 400- |
1032615291 | 2018-06-19 | Production Wells | No Violations | On the day of my inspection I witnessed that the well was equipped with 5.5 inch diameter production casing that was open flowing. Annular pressure monitoring was in place, the intermediate casing gauge read 0 pounds per square inch, the surface casing gauge read 175 pounds per square inch. Production equipment included a Sand Separator, Gas Processing unit, 4- 400 barrel purge tanks, and a 50 barrel produced water tank shared with 34013211840000, 34013211860000. Identification tags were present, and production was up to date. No violations were found at the time of my inspection. |
1070520151 | 2020-2-20 0:00: | PW | No Violations | 0.20 |
1291407315 | 2019-02-06 | Preliminary Restoration | No Violations | Preliminary restoration status check inspection found well site restoration meets ORC 1509.072 with vegetation established and erosion control in place. The lease road and well pad surface are stone construction and in good repair. 3 wells are present on the pad. Signage is posted a the lease road entrance and at each well head. Emergency shut down devices are present at each critical area of the well pad. |
1387600746 | 2017-05-11 | Preliminary Restoration | No Violations | On the day of my inspection the site passed preliminary restoration according to ORC 1509.072A. |
1490456631 | 2017-03-25 | Casing String Witnessed | No Violations | On site inspection to witness the surface casing cement job with H&P Drilling rig 608 and Stingray cement service. The well was spudded on 03/05/2017 with HAD Drilling setting the 26 conductor to 117, which was concentric drilled and not cemented. H&P Rig 608 is now on the hole and has drilled a 17.5 surface borehole to a measured depth of 1,508. The rig has ran 1,508 of 54.5 lb/ft J-55 casing with Wyoming Casing Service making up the connections. While running the casing at a depth of 1,462 the rig attempted unsuccessfully to load the hole and establish circulation to surface with 900 barrels of fresh water pumped with a total hole capacity of 490 barrels. At that point casing was ran and set on bottom with no restrictions and the cement company pumped a 25 barrel 6% gel spacer sweep with the hole circulating at 375 barrels. At that point the cement job was commenced by pumping an addition 25 barrels of 6% gel followed by a 280 barrel cement mix consisting of 1312 sacks of class A-1.5% Calcium 0.25 pound per sack flow seal cement. The cement was displaced with 225 barrels of fresh water and the casing was pressure tested to 500 psi over cement displacement pressure upon the landing of the cement plug into the casing float collar with cement returns witnessed to surface inside the cellar. The cement weight was verified by weight of scale. |
1496757873 | 2017-06-06 | Completion Testing | No Violations | Status check inspection on the well stimulation process found Stingray Pressure Pumping Service on location along with Renegade Wireline Service. The well head completion consist is made up of a Cactus Well Head B section and Tubing head assembly rated at 15,000 pound per square inch working pressure (psi) with a Red Dirt master valve isolation tool on top of the well head followed by a manual master valve and then 3 hydraulic master valves. The well bore production casing is 5.5 diameter and consists of 4 pressure activated sleeve assemblies ran in the 5.5 production string between the depths of 18,818 and 18,667. The sleeves have been opened and the 1st stage stimulated. The well bore true vertical depth is 8,636. All stimulation equipment is situated on polymer containment with the well pad perimeter berm serving as the primary containment. |
1535542577 | 2018-08-29 | Production Wells | No Violations | Status check inspection found 3 wells present on the pad all in production. The lease road has proper identification posted at the entry point and has a gate across it at the well pad entry point. The lease road and well pad are of stone surface construction and in good repair. The well pad perimeter is protected by an earthen berm. There is a Mark West mid stream pipeline station along the lease road at the right front corner of the well pad. There is 3 gas processing units on the left side of the pad and the tank battery is at the left rear corner. The tank battery consists of (4) steel construction 400 barrel capacity tanks and one 50 barrel steel tank, all situated inside a polymer lined steel containment dike area. Hazard warning labels are posted on the tank and there is emergency shut down devices situated at all critical areas on the well pad including at the entry point gate. The well head assembly consists of a lower A section and upper B section with 2 diameter riser pipes attached to both section outlet ports with valves and gauges present to monitor annular pressure. The A section gauge which monitors the pressure between the 9.625 and 13.375 diameter casing string reads 240 pounds pressure. The B section gauge which reads the pressure between the 5.5 and 9.625 diameter casing strings reads zero pounds pressure. The 5.5 diameter casing internal pressure gauge reads 1,800 pounds pressure. There is tubing in the well and the tubing head gauge reads 800 pounds pressure and the production flow line downstream of the choke reads 400 pounds pressure, the well is open flowing up the tubing. Identification is present on each well head. |
For data sources see[10]