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| Well ID: 34-059-23807 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Guernsey | |
| Municipality: Wheeling Township | |
| Operator Name: RHDK OIL & GAS LLC/DBA RED HIL | |
| Well Pad ID: | |
| Farm/Lease Name: MATHEWS UNIT | |
| License Status: Producing | |
| License Date: 1990-09-14 | |
| Spud Date: 1990-09-22 | |
| Spud Drilling Contractor: CUBBY DRLG | |
| Final Drill Date: 1990-09-28 | |
| Well Total Depth: 7480.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.210000 | |
| Longitude: -81.570000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| CO | 1990-09-14 | 168 RED HILL DEVELOPMENT GeoDate 9/14/90 |
| Oil and Gas | 1990-09-14 | Issued Date 9/14/90 Expired Date 9/14/91 Acres 0138617 Tool Type RTAF Proposed Formation ROSE RUN Proposed Depth 07480 Proposed Drill Depth 07480 |
| Original Spud | 1990-09-22 | |
| Completed | 1990-09-28 | |
| Reached Total Depth | 1990-09-28 | |
| Completion Report Received | 1991-05-28 | |
| Construction Permit Expires | 1991-09-14 | |
| Record Last Modified | 2017-02-15 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 1997-06-29 | 4704 | 4820 | 0 |
| 4704 | 4820 | 0 | |
| 2006-09-11 | 4768 | 4822 | 6 |
| 4768 | 4822 | 6 | |
| 4704 | 4820 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| ACID | 15 | 1500 Gal | 0 | ACIDIZED W/1500 GAL 15% HCL |
For data sources see[4]
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1224169497 | 2006-9-7 0:00:0 | PW | No Violations | |
| -1478265480 | 2006-3-15 0:00: | PW | No Violations | |
| -1547105846 | 2007-5-21 0:00: | PW | No Violations | |
| -1646638843 | 2006-12-27 0:00 | PW | No Violations | |
| -447817848 | 2018-3-21 0:00: | PW | No Violations | 1.00 |
| -504686875 | 2008-12-9 0:00: | PW | No Violations | |
| -647300396 | 2005-9-28 0:00: | PW | No Violations | |
| 0000007243 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 6/19/92 INSPECTOR MIKE PHELPS DATE 06/1919/92 DATA FROM OLD VAX INFO | |
| 001289i228 | 2001-05-18 | Production Wells | No Violations | status check; noviolations |
| 0063477220 | 2005-04-22 | Production Wells | No Violations | STATUS CHECK |
| 0447817848 | 2018-03-21 | Production Wells | No Violations | On the day of inspection with ground covered with snow, and was accompanied by ODNR Inspector Doug Bennett. I witnessed production equipment included a 210 barrel tank, and a horizontal separator with chart meter system within earthen dike. The well was equipped with 4.5 inch diameter casing, 1.5 inch diameter tubing, a plunger lift system, and domestic gas. Both valves were open on tubing and 1 of 2 valves were open on casing. Proper identification was present and production report was up to date. |
| 0504686875 | 2008-12-09 | Production Wells | No Violations | PRODUCING WELL. ID RECENTLY REDONE. |
| 0647300396 | 2005-09-28 | Production Wells | No Violations | STATUS CHECK |
| 0699586280 | 2008-05-13 | Production Wells | No Violations | PRODUCING WELL |
| 1014263424 | 2018-03-21 | Production Wells | No Violations | On the day of my inspection I accompanied by ODNR Inspector Jeff Adams please see his report for details. |
| 1154458088 | 2004-07-16 | Production Wells | No Violations | STATIS CHECK, WELL IS IN PRODUCTION, 210 TANK IN DIKE AREA |
| 1224169497 | 2006-09-07 | Production Wells | No Violations | PRODUCING WELL |
| 1289i228 | 2001-5-18 0:00: | PW | No Violations | |
| 1478265480 | 2006-03-15 | Production Wells | No Violations | STATUS CHECK |
| 1547105846 | 2007-05-21 | Production Wells | No Violations | POP OFF VALVE REPLACED. |
| 1646638843 | 2006-12-27 | Production Wells | No Violations | ID REPOSTED. |
| 63477220 | 2005-4-22 0:00: | PW | No Violations | |
| 699586280 | 2008-5-13 0:00: | PW | No Violations | |
| 7243 | PL | No Violations |
For data sources see[9]