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Well ID: 34-103-25048 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: BLEACHTECH LLC | |
Well Pad ID: | |
Farm/Lease Name: BLEACHTECH (SMP #2) | |
License Status: Active Injection | |
License Date: 2014-01-28 | |
Spud Date: 2014-02-10 | |
Spud Drilling Contractor: POULSON DRILLING | |
Final Drill Date: 2014-02-20 | |
Well Total Depth: 2627.00 ft | |
Configuration: Vertical | |
Latitude: 41.020000 | |
Longitude: -81.870000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2014-01-28 | Proposed Formations:SALINA F1 SALT, Issued Date:1/28/2014, Expired Date:1/28/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SM, Proposed Well Class:SMP |
Plugged Back | 2014-02-13 | |
Reached Total Depth | 2014-02-20 | |
Last Compliance Report | 2014-04-16 | |
Completion Report Received | 2014-04-23 | |
Construction Permit Expires | 2016-01-28 | |
Record Last Modified | 2018-11-30 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1328665725 | 2014-2-7 0:00:0 | DD | No Violations | |
-1500950856 | 2014-2-15 0:00: | DD | No Violations | |
-167573315 | 2017-5-18 0:00: | SM | No Violations | |
-180446652 | 2014-2-20 0:00: | DD | No Violations | |
-1862287366 | 2014-2-13 0:00: | DD | No Violations | |
-1864576242 | 2014-2-11 0:00: | DD | No Violations | |
-197949860 | 2014-4-3 0:00:0 | DD | No Violations | |
-272996372 | 2014-2-12 0:00: | DD | No Violations | |
-537961741 | 2014-2-14 0:00: | DD | No Violations | |
-668439424 | 2018-11-29 0:00 | SM | No Violations | 8.00 |
-702483525 | 2014-2-10 0:00: | DD | No Violations | |
0167573315 | 2017-05-18 | Solution Mining Project | No Violations | Inspected well on 05/18/2017 with Inspector Steve Ochs at the request of Andrew Adgate to confirm the well status. The well has been placed into production, and well identification is clearly displayed. The well status (AI) is correct. No problems were noted at the time of the inspection. |
0180446652 | 2014-02-20 | Drill / Deepen / Reopen | No Violations | Visited rig on 02/20/2014 for MIT test for production casing. Pressured up to 500 psi for 15 minutes. Pressure dropped approximately 25 psi, which was within the limits of the test. Test passed. Plan forward is for rig to drill out from under production casing to TD. |
0197949860 | 2014-04-03 | Drill / Deepen / Reopen | No Violations | Visited location on 04/03/2014 to witness logging job on the Bleachtech #14 well. The hole was loaded on 04/02/2014 with pit water (note: drilling operations had been completed the previous week, so solids in pit had settled out and water was taken from top of pit). Appalachian Well Services rigged up and logged the well. Both the top and bottom centralizers on the logging tool were broken during the logging run, but it didnt cause any issues for the job. The cement bond on the 8 5/8 casing looked excellent throughout the entire length of the string. |
0272996372 | 2014-02-12 | Drill / Deepen / Reopen | No Violations | Visited rig on 02/12/2014 to check on status of operations. At time of visit, rig was drilling 14 3/4 hole at 496. Drilled ahead to 502 and ran deviation survey. Deviation survey showed deviation of 7 degrees. Ran survey again to double-check deviation with the same results. Ran survey a third time with a different tool to check deviation with the same results. Plan forward is to drill ahead and try to straighten hole. |
0537961741 | 2014-02-14 | Drill / Deepen / Reopen | No Violations | Visited rig on 02/14/2014 to check-on status of drilling operations. At time of visit, rig was drilling ahead at 412 with a deviation of 2.75 degrees. |
0556709456 | 2014-10-23 | Preliminary Restoration | No Violations | Visited location on 10/23/2014 to check on the restoration status of the well. The well is equipped for production; well identification is clearly displayed next to the wellhead. All pits have been closed and drilling equipment removed. Preliminary Restoration passes. |
0668439424 | 2018-11-29 | Solution Mining Project | No Violations | I was on location to witness a Mechanical Integrity Test (MIT). After eight (8) hours the average test well pressure was 189.533 psi and the average reference well pressure was 81.669 with a difference of 107.864 psi. The calculated net pressure change resulted in 0.03 psi/hr., which is well below the maximum net pressure change of 0.05 psi/hr. MIT passed. |
0702483525 | 2014-02-10 | Drill / Deepen / Reopen | No Violations | Visited location on 02/10/2014 to witness well spud. Waited on water truck to arrive. Mixed fresh water mud. Spud well with 7 7/8 PDC bit at approximately 11:15AM. |
1022670895 | 2014-02-18 | Drill / Deepen / Reopen | No Violations | Visited location on 02/18/2014 for production casing cement job. An 11 hole was drilled to 2,427 and 8 5/8, 32# production casing was run to 2,398 with a float shoe and 10 centralizers. Waited on rig to run casing. Rigged up Petroset for cement job. Cement job went well; got 25 bbls good cement returns to surface. Pressured well up to 500 psi over landing pressure and attempted to perform MIT test on production casing, but a leak at the cement head caused pressure to be lost, so the test failed. Plan forward is to wait on cement to set up, and perform test in approximately 18 hours. |
1295201344 | 2019-5-13 0:00: | SM | No Violations | 0.30 |
1328665725 | 2014-02-07 | Drill / Deepen / Reopen | No Violations | Stopped by well location to meet crew and check on progress. Rig in the process of moving in and rigging up at the time of the inspection. Plan forward will be to finish rigging up and then shut-down for the weekend and resume operations Monday. |
1397228584 | 2014-04-10 | Drill / Deepen / Reopen | No Violations | Visited location on 04/10/2014. Crew was working to harden pit for Bleachtech #14 and #13 wells with fly ash from Chem Tech. No problems were noted at the time. |
1494846561 | 2014-02-10 | Drill / Deepen / Reopen | No Violations | Arrived at location on 02/10/2014 to witness conductor casing cement job. A 20 hole was drilled to 185 and 16, 65# conductor casing was run to 169. Waited on rig to run casing prior to cement job. Rigged up Petroset, and pumped 185 sacks of Class A cement with hulls. Cement job went well; got 4 bbls good cement return. Rig will shut-down for 8 hours to wait on cement. |
1500950856 | 2014-02-15 | Drill / Deepen / Reopen | No Violations | Visited location on 02/15/2014 for surface casing cement job. Drilled 14 3/4 hole to 629 and set 11 3/4, 32# surface casing to 600 with a collar on bottom and 3 centralizers. Cement job went well; got 8 bbls good cement returns to surface. |
1522417044 | 2018-03-30 | Solution Mining Project | No Violations | I found the injection well in operation on the day of my inspection. There is calcification build-up on the tubing and wellhead. I observed no leaks or spills around the well. There is an identification sign displayed on a steel post next to the well. There are no problems noted at this time. |
1862287366 | 2014-02-13 | Drill / Deepen / Reopen | No Violations | Visited location on 02/13/2014 for plug-back operations. Rig drilled ahead to 533 but was unable to straighten hole out. Decision made to plug back and set plug from 333-533. Cement job went well; circulation was established and maintained throughout job. Rig will shut-down for 24 hours to wait on cement. |
1864576242 | 2014-02-11 | Drill / Deepen / Reopen | No Violations | Visited location on 02/11/2014 to check on progress. At time of visit, rig was just starting in the hole to drill out from under conductor casing. |
1981647146 | 2017-12-01 | Solution Mining Project | No Violations | I found the injection well in operation on the day of my inspection. There is an identification sign displayed on a steel post next to the well. There are no problems noted at this time. |
556709456 | 2014-10-23 0:00 | PL | No Violations |
For data sources see[3]